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Well ID: 34-055-20988 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Huntsburg Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: HUNTSBURG TWP TRUSTEES | |
License Status: Producing | |
License Date: 1984-09-28 | |
Spud Date: 1984-10-26 | |
Spud Drilling Contractor: MOSS CREEK DRLG | |
Final Drill Date: 1984-11-03 | |
Well Total Depth: 3921.00 ft | |
Configuration: Vertical | |
Latitude: 41.530000 | |
Longitude: -81.030000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-09-28 | 9 EDC GeoDate 9/28/84 |
Oil and Gas | 1984-09-28 | Issued Date 9/28/84 Expired Date 3/27/85 Acres 0030000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 03921 Proposed Drill Depth 03921 |
Original Spud | 1984-10-26 | |
Completed | 1984-11-03 | |
Reached Total Depth | 1984-11-03 | |
Completion Report Received | 1984-12-05 | |
Construction Permit Expires | 1985-03-27 | |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Change of Owner | 2017-05-01 | Operator changed from 7578, ENERVEST OPERATING LLC, to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2017-05-01 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3730 | 3839 | 0 |
3730 | 3839 | 0 | |
2006-09-11 | 3737 | 3784 | 3 |
3737 | 3784 | 3 | |
3730 | 3839 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 174 Mscf | 0 | |||
H2O | 0 | 68000 Gal | 80000 | FRAC;H2O,SAND,N2 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1775796042 | 2015-2-20 0:00: | PW | No Violations | |
-2041144960 | 2013-2-6 0:00:0 | PW | No Violations | |
-434848863 | 2017-8-29 0:00: | PW | No Violations | |
0434848863 | 2017-08-29 | Production Wells | No Violations | During this inspection, the well was equipped with a plunger lift assembly and the valves on the annulus and flow lines were open at the wellhead. Production records for this well were up to date. The well was fenced with a locked man door. The tank battery consisted of one 100 BBL production tank and a mechanical separator. Valves on the separator were open and the chart showed production. The heater tube on the 100 BBL production tank had been plugged with a plastic cap but salt crystals had formed at the base of the cap and heater tube. The tank battery was diked and fenced with proper, legible signage. The lease access was stable. I contacted John Raber of M&R Investments to repair the leaking heater tube. |
1260518273 | 2013-02-13 | Production Wells | No Violations | This inspection was a follow up inspection on a previous inspection. The dump line leading into the 100 barrel production tank had been properly repaired and was not leaking any more. The oil had been cleaned off of the side of the tank. The gravel around the base of the tank that had been saturated with oil had been removed. |
1775796042 | 2015-02-20 | Production Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The well and tank battery are in good repair and are surrounded by a chain link fence. The tank battery consists of a 100 BBL production tank and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. |
2041144960 | 2013-02-06 | Production Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The well head was surrounded by a locked chain link fence. The tank battery was surrounded by a locked chain link fence and a proper dike. The tank battery consists of a 100 barrel steel production tank and a mechanical separator. The separator had a seven day production chart in the meter box. The union on the dump line at the top of the 100 barrel tank is leaking. There is a small amount of crude oil running down the side of the tank and a little on the ground at the base of the tank. The company was notified and I told them to have the line fixed and the area cleaned up. They were given until 2/11/13 to do so. The lease road was in good condition. |
2145895208 | 2014-01-21 | Production Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The well and tank battery are in good repair and are surrounded by a chain link fence. The tank battery consists of a 100 BBL production tank and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. |
For data sources see[9]