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34-055-21170

Well Details

Well ID: 34-055-21170
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Country: United States
State: Ohio
County: Geauga
Municipality: Newbury Township
Operator Name: HUNTER BRUCE C
Well Pad ID:
Farm/Lease Name: JACKSON D
License Status: Domestic Well
License Date: 1993-06-03
Spud Date: 1986-08-04
Spud Drilling Contractor:
Final Drill Date: 1986-08-07
Well Total Depth: 4110.00 ft
Configuration: Vertical
Latitude: 41.450000
Longitude: -81.220000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1985-02-26 213 LOMAK OPERATING CO GeoDate 2/26/85
Oil and Gas 1985-02-26 Issued Date 2/26/85 Expired Date 8/25/85 Acres 0020000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1985-07-26 213 LOMAK OPERATING CO GeoDate 7/26/85
Oil and Gas 1985-07-26 Issued Date 7/26/85 Expired Date 7/26/86 Acres 0020000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1986-08-04 R.I. 7-27-85, R.I. 7-19-86
Completed 1986-08-07 R.I. 7-27-85, R.I. 7-19-86
Reached Total Depth 1986-08-07 R.I. 7-27-85, R.I. 7-19-86
CO 1993-06-03 1634 NORTHWOOD ENERGY CORP GeoDate 6/3/93
Unknown 1993-06-03 Issued Date 6/3/93 Expired Date 6/3/94 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Construction Permit Expires 1994-06-03 R.I. 7-27-85, R.I. 7-19-86
CO 1994-10-21 4587 PASCOE JAMES L & JENNIE GeoDate 6/3/93
Change of Owner 2005-10-19 Operator changed from 4587, PASCOE JAMES L & JENNIE to 7932, HUNTER BRUCE C
Record Last Modified 2009-12-11 R.I. 7-27-85, R.I. 7-19-86

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3926 3971 30
3926 3971 30
3926 3971 30

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 65000 Gal 40000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 RANGE OPERATING COMPANY 2012.00 0.00 92
1987 RANGE OPERATING COMPANY 9459.00 180.00 365
1988 RANGE OPERATING COMPANY 4099.00 96.00 366
1989 RANGE OPERATING COMPANY 2233.00 0.00 365
1990 RANGE OPERATING COMPANY 623.00 100.00 120
1991 NORTHWOOD ENERGY CORP 18.00 43.00 365
1992 NORTHWOOD ENERGY CORP 1308.00 0.00 365
1993 NORTHWOOD ENERGY CORP 459.00 39.00 365
1995 NORTHWOOD ENERGY CORP 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 RANGE OPERATING COMPANY Brine 2660 92
1987 RANGE OPERATING COMPANY Brine 347 365
1988 RANGE OPERATING COMPANY Brine 210 366
1989 RANGE OPERATING COMPANY Brine 200 365
1990 RANGE OPERATING COMPANY Brine 240 120
1991 NORTHWOOD ENERGY CORP Brine 106 365
1992 NORTHWOOD ENERGY CORP Brine 0 365
1993 NORTHWOOD ENERGY CORP Brine 15 365
1995 NORTHWOOD ENERGY CORP Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1427110931 2015-03-23 Production Wells No Violations I was notified by Nick Well Plugging that they were able to retrieve all of the 1/2 sand line that was in the well. The swab tool was not able to be retrieved and had fallen below the perforations and into the rat hole.
1996748998 2015-03-11 Production Wells No Violations I was on location to provide information about the well to the service company performing maintenance on the well for the landowner. The landowner had Glen Spencer well service swab the well approximately four years ago and in the process of doing so, lost his swab tools and 3200 of 1/2 sand line in the 4.5 casing. Nicks well plugging was the service contractor attempting to retrieve the line and the tools from the well. Nicks was able to retrieve about 600 of sand line while I was on location.

For data sources see[9]

References