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Well ID: 34-055-21313 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Bainbridge Township | |
Operator Name: BAAY OIL LLC | |
Well Pad ID: | |
Farm/Lease Name: HOWARD V UNIT | |
License Status: Producing | |
License Date: 1985-12-09 | |
Spud Date: 1986-01-18 | |
Spud Drilling Contractor: PEP DRLG | |
Final Drill Date: 1986-01-24 | |
Well Total Depth: 4048.00 ft | |
Configuration: Vertical | |
Latitude: 41.380000 | |
Longitude: -81.300000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1985-10-18 | Issued Date 10/18/85 Expired Date 10/18/86 Acres 0020890 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1985-12-09 | 28 CGAS EXPLORATION,INC GeoDate 12/9/85 |
Oil and Gas | 1985-12-09 | Issued Date 10/18/85 Expired Date 10/18/86 Acres 0020890 Tool Type RTF Proposed Formation CLINTON Proposed Depth 04048 Proposed Drill Depth 04048 |
Original Spud | 1986-01-18 | RL 12-14-85 |
Completed | 1986-01-24 | RL 12-14-85 |
Reached Total Depth | 1986-01-24 | RL 12-14-85 |
Completion Report Received | 1986-01-27 | RL 12-14-85 |
CO | 1986-03-11 | 28 CGAS EXPLORATION,INC GeoDate 10/18/85 |
Construction Permit Expires | 1986-10-18 | RL 12-14-85 |
Change of Owner | 2002-11-21 | Operator changed from 28, CGAS EXPLORATION to 1198, PIPES PURSIE E |
Change of Owner | 2008-09-03 | Operator changed from 1198, PIPES PURSIE E to 1304, SEAGULL DEVELOPMENT CORP |
Change of Owner | 2012-02-03 | Operator changed from 1304, SEAGULL DEVELOPMENT CORP to 8560, BAAY OIL LLC |
Record Last Modified | 2017-02-15 | RL 12-14-85 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3872 | 3924 | 21 |
3872 | 3924 | 21 | |
3872 | 3924 | 21 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1406 Bbl | 70000 | PRELIMINARY |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | CGAS EXPLORATION | 8324.00 | 349.00 | 365 |
1987 | CGAS EXPLORATION | 8648.00 | 274.00 | 365 |
1988 | CGAS EXPLORATION | 6080.00 | 160.00 | 365 |
1989 | CGAS EXPLORATION | 5748.00 | 126.00 | 365 |
1990 | CGAS EXPLORATION | 4895.00 | 73.00 | 365 |
1991 | CGAS EXPLORATION | 4320.00 | 124.00 | 365 |
1992 | CGAS EXPLORATION | 3757.00 | 56.00 | 366 |
1993 | CGAS EXPLORATION | 3872.00 | 101.00 | 366 |
1994 | CGAS EXPLORATION | 3180.00 | 71.00 | 365 |
1995 | CGAS EXPLORATION | 3107.00 | 0.00 | 365 |
1996 | CGAS EXPLORATION | 3813.00 | 69.00 | 365 |
1997 | CGAS EXPLORATION | 4003.00 | 65.00 | 365 |
1998 | CGAS EXPLORATION | 3017.00 | 0.00 | 365 |
1999 | CGAS EXPLORATION | 2432.00 | 106.00 | 365 |
2000 | CGAS EXPLORATION | 1779.00 | 0.00 | 365 |
2001 | CGAS EXPLORATION | 942.00 | 51.00 | 365 |
2002 | CGAS EXPLORATION | 396.00 | 0.00 | 324 |
2003 | SEAGULL DEVELOPMENT CORP | 462.00 | 0.00 | 365 |
2004 | SEAGULL DEVELOPMENT CORP | 1880.00 | 55.00 | 365 |
2005 | SEAGULL DEVELOPMENT CORP | 1508.00 | 23.00 | 365 |
2006 | SEAGULL DEVELOPMENT CORP | 1685.00 | 0.00 | 365 |
2007 | SEAGULL DEVELOPMENT CORP | 1460.00 | 25.00 | 365 |
2008 | SEAGULL DEVELOPMENT CORP | 272.00 | 0.00 | 365 |
2009 | SEAGULL DEVELOPMENT CORP | 526.00 | 31.00 | 365 |
2010 | SEAGULL DEVELOPMENT CORP | 863.00 | 0.00 | 300 |
2011 | SEAGULL DEVELOPMENT CORP | 778.00 | 22.00 | 300 |
2012 | BAAY OIL LLC | 992.00 | 0.00 | 366 |
2013 | BAAY OIL LLC | 1846.00 | 39.00 | 365 |
2014 | BAAY OIL LLC | 1636.00 | 70.00 | 365 |
2015 | BAAY OIL LLC | 1565.00 | 0.00 | 365 |
2016 | BAAY OIL LLC | 1462.00 | 29.00 | 365 |
2017 | BAAY OIL LLC | 1465.00 | 30.00 | 365 |
2018 | BAAY OIL LLC | 1421.00 | 41.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | CGAS EXPLORATION | Brine | 396 | 365 |
1987 | CGAS EXPLORATION | Brine | 242 | 365 |
1988 | CGAS EXPLORATION | Brine | 178 | 365 |
1989 | CGAS EXPLORATION | Brine | 70 | 365 |
1990 | CGAS EXPLORATION | Brine | 111 | 365 |
1991 | CGAS EXPLORATION | Brine | 67 | 365 |
1992 | CGAS EXPLORATION | Brine | 28 | 366 |
1993 | CGAS EXPLORATION | Brine | 48 | 366 |
1994 | CGAS EXPLORATION | Brine | 56 | 365 |
1995 | CGAS EXPLORATION | Brine | 0 | 365 |
1996 | CGAS EXPLORATION | Brine | 0 | 365 |
1997 | CGAS EXPLORATION | Brine | 113 | 365 |
1998 | CGAS EXPLORATION | Brine | 56 | 365 |
1999 | CGAS EXPLORATION | Brine | 0 | 365 |
2000 | CGAS EXPLORATION | Brine | 0 | 365 |
2001 | CGAS EXPLORATION | Brine | 0 | 365 |
2002 | CGAS EXPLORATION | Brine | 0 | 324 |
2003 | SEAGULL DEVELOPMENT CORP | Brine | 0 | 365 |
2004 | SEAGULL DEVELOPMENT CORP | Brine | 0 | 365 |
2005 | SEAGULL DEVELOPMENT CORP | Brine | 30 | 365 |
2006 | SEAGULL DEVELOPMENT CORP | Brine | 0 | 365 |
2007 | SEAGULL DEVELOPMENT CORP | Brine | 0 | 365 |
2008 | SEAGULL DEVELOPMENT CORP | Brine | 0 | 365 |
2009 | SEAGULL DEVELOPMENT CORP | Brine | 0 | 365 |
2010 | SEAGULL DEVELOPMENT CORP | Brine | 0 | 300 |
2011 | SEAGULL DEVELOPMENT CORP | Brine | 0 | 300 |
2012 | BAAY OIL LLC | Brine | 0 | 366 |
2013 | BAAY OIL LLC | Brine | 165 | 365 |
2014 | BAAY OIL LLC | Brine | 80 | 365 |
2015 | BAAY OIL LLC | Brine | 0 | 365 |
2016 | BAAY OIL LLC | Brine | 22 | 365 |
2017 | BAAY OIL LLC | Brine | 26 | 365 |
2018 | BAAY OIL LLC | Brine | 67 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1217469790 | 2018-8-24 0:00: | UP | No Violations | |
-1238116977 | 2018-7-5 0:00:0 | UP | No Violations | |
-2144789612 | 2015-7-22 0:00: | UP | No Violations | |
-33654827 | 2016-9-14 0:00: | UP | No Violations | |
-347999675 | 2009-5-8 0:00:0 | PW | No Violations | |
0033654827 | 2016-09-14 | UrbanProduction Wells | No Violations | I conducted an inspection on this well. The well is equipped with a plunger lift unit and the valves on the wellhead were open. The well was fenced and man door locked. There has been identification posted at the well. The tank battery consisted of two, 100 BBL production tanks, one, 50 BBL steel brine tank, and a mechanical separator. The 100 BBL production tank nearest the man door that was seeping at the base has been repaired and the oil stained stone was removed. The tank battery is diked with proper, legible indentification. The tank battery is fenced and the man door locked. Tank battery is shared with well 21312. Lease access is stable. No violations found. |
0347999675 | 2009-05-08 | Production Wells | No Violations | Pop off on separator venting. Called Lynn Strazi requested repairs to be made immediately. Per Lynn, Dominion has been changing and shutting in lines, which has been causing over pressurizing. Fence needs cleaned up around well head. Brush and weeds need removed. |
1217469790 | 2018-08-24 | UrbanProduction Wells | No Violations | I conducted a compliance notice follow-up inspection for compliance notice 1528463689. At the time of this inspection, the diked tank battery has had one 100 BBL tank and one 50 BBL poly tank reinstalled. The fencing has been reinstalled around the tank battery and the man door locked. The well was in production at the time of this inspection. The impacted soil and stone within the tank battery has been removed and replaced with new stone. Compliance notice closed. |
1238116977 | 2018-07-05 | UrbanProduction Wells | No Violations | I conducted a compliance notice follow-up inspection for compliance notice 1528463689. At the time of this inspection, the two 100 BBL tanks have been disconnected from the other production equipment and removed from the tank battery location. They were emptied and staged outside of the dike. The cleanup of the impacted stone and soil within the tank battery had started. The well has been shut-in. Signage has been added to the well location.
BAAY Oil needs to: 1) Complete the removal of the impacted soil and stone within the tank battery, and dispose of the material at a proper disposal facility. 2) Remove the tanks from the site. 3) Reinstall the fence around the tank battery. |
1249326937 | 2009-07-29 | Production Wells | No Violations | Well needs weeds removed from around it. Weeds have grown up inside well head cage. New fence has been put up. Locks were on the man doors. ID sign needs posted at the well head. Called Lynn Strazi regarding ID sign. He has them in the back of his truck, has been meaning to get them up. Leaks at the well head and at the tank battery have been repaired. |
1367929605 | 2013-05-07 | UrbanProduction Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The well and tank battery are in good repair and surrounded by a locked chain link fence. The tank battery consists of two 100 BBL production tanks, a 50 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. The lease road and tank battery are being shared by permit number 2-1312. |
1473379147 | 2018-07-24 | UrbanProduction Wells | No Violations | I conducted a compliance notice follow-up inspection for compliance notice 1528463689. At the time of this inspection, the two 100 BBL tanks have been moved offsite. The impacted stone and soil within the tank battery have been removed. The dike has been reinstalled on the north side of the tank battery. The well was still shut-in at the time of this inspection. The fencing around the tank battery still needs reinstalled.
BAAY Oil needs to: 1) Reinstall the fence around the tank battery. |
1528463689 | 2018-06-08 | UrbanProduction Wells | Violations Noted | During my inspection, the well was equipped with a plunger lift assembly and the gate valve on the tubing and 2 inch flow line was open. The well was fenced with a locked man door. The tank battery consisted of two 100 BBL tanks, one 50 BBL tank and a mechanical separator. Valves on the separator were open and the chart showed production. There was a Dominion sales line within the existing diked tank battery. The 100 BBL tank on the east side of the battery had leaked from the base. An area approximately 9.5X11 feet was stained with oil. Some free oil was observed directly under the leaking tank. The area of impact was within the diked tank battery. The 100 BBL tank had been emptied and disconnected from the other production equipment. The tank battery was fenced and shared with well 2-1312. The fence around the tank battery on the north side was starting to lean and needs to be restabilized. Signage was located at the tank battery but needs to be installed at the well location. Lease access was stable. I contacted BAAY Oil, LLC and spoke with Brooks Yarborough, company owner to discuss items needing addressed.
BAAY Oil needs to: 1) Install signage at the well. 2) Remove impacted soil and stone within the tank battery and dispose at a proper facility. Remove the leaking 100 BBL tank. 3) Repair the leaning fence. |
2121564500 | 2016-07-26 | UrbanProduction Wells | No Violations | I conducted an inspection on this well. The well was equipped with a plunger lift unit and the valves on the wellhead were open. The well was fenced and man door locked. The well needs identification. The tank battery consisted of two, 100 BBL production tanks, one, 50 BBL steel brine tank, and a mechanical separator. The 100 BBL production tank nearest the man door was seeping at the base and oil stained stone was observed. The tank battery is diked with proper, legible indentification. The tank battery is fenced and the man door locked. Tank battery is shared with well 21312. Lease access is stable. I called Brooks Yarbrough from Baay Oil, to discuss the additional signage needed at the well and removing the leaking production tank along with removing any impacted medium within the tank battery. |
2144789612 | 2015-07-22 | UrbanProduction Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The well and tank battery are in good repair and surrounded by a locked chain link fence. The tank battery consists of two 100 BBL production tanks, a 50 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. The lease road and tank battery are being shared by permit number 2-1312. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1528463689 | US-OH-114639 | 2018-09-04 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[9]