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Well ID: 34-055-21607 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Burton Township | |
Operator Name: BOCOR HOLDINGS, LLC | |
Well Pad ID: | |
Farm/Lease Name: KAUFMAN B & J | |
License Status: Producing | |
License Date: 1989-08-10 | |
Spud Date: 1989-11-02 | |
Spud Drilling Contractor: [[EPC [EASTERN PETROLEUM]]] | |
Final Drill Date: 1989-11-09 | |
Well Total Depth: 4078.00 ft | |
Configuration: Vertical | |
Latitude: 41.460000 | |
Longitude: -81.190000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1989-08-10 | Issued Date 8/10/89 Expired Date 8/10/90 Acres 0020000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04078 Proposed Drill Depth 04078 |
Original Spud | 1989-11-03 | |
Completed | 1989-11-09 | |
Reached Total Depth | 1989-11-09 | |
Completion Report Received | 1990-01-24 | |
CO | 1990-02-06 | 773 FORTUNE GAS & OIL GeoDate 8/10/89 |
Construction Permit Expires | 1990-08-10 | |
Change of Owner | 2002-06-11 | Operator changed from 773, FORTUNE GAS & OIL to 4939, ENERGY RESOURCES AMERICA |
Change of Owner | 2003-10-06 | Operator changed from 4939, ENERGY RESOURCES AMERICA to 7525, J & T EXPLORATION LLC |
Change of Owner | 2015-02-11 | Operator changed from 7525, J & T EXPLORATION LLC to 935, BOCOR HOLDINGS, LLC/BOCOR PROD |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3873 | 3875 | 28 |
3868 | 3968 | 0 | |
1997-06-29 | 3868 | 3968 | 0 |
0 | 16 | ||
0 | 16 | ||
2006-09-11 | 0 | 16 | |
2006-09-11 | 3913 | 3928 | 6 |
2006-09-11 | 3890 | 3900 | 3 |
2006-09-11 | 3883 | 3885 | 3 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 70000 Gal | 50000 | FRAC:WATER/SAND/ACID | ||
ACID | 0 | 500 Gal | 0 | FE |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | FORTUNE GAS & OIL | 15007.00 | 671.00 | 328 |
1991 | FORTUNE GAS & OIL | 5608.00 | 293.00 | 365 |
1992 | FORTUNE GAS & OIL | 3788.00 | 146.00 | 365 |
1993 | FORTUNE GAS & OIL | 3021.00 | 247.00 | 365 |
1994 | FORTUNE GAS & OIL | 3904.00 | 191.00 | 365 |
1995 | FORTUNE GAS & OIL | 2901.00 | 47.00 | 365 |
1996 | FORTUNE GAS & OIL | 1069.00 | 92.00 | 365 |
1997 | FORTUNE GAS & OIL | 809.00 | 0.00 | 365 |
1998 | FORTUNE GAS & OIL | 1011.00 | 0.00 | 365 |
1999 | FORTUNE GAS & OIL | 534.00 | 0.00 | 365 |
0 | 0 | 0 | ||
2000 | FORTUNE GAS & OIL | 400.00 | 88.00 | 365 |
2001 | FORTUNE GAS & OIL | 752.00 | 124.00 | 365 |
2002 | FORTUNE GAS & OIL | 75.00 | 0.00 | 59 |
2006 | J & T EXPLORATION LLC | 869.00 | 54.00 | 365 |
2007 | J & T EXPLORATION LLC | 980.00 | 75.00 | 0 |
2008 | J & T EXPLORATION LLC | 802.00 | 72.00 | 0 |
2009 | J & T EXPLORATION LLC | 633.00 | 79.00 | 0 |
2010 | J & T EXPLORATION LLC | 864.00 | 14.00 | 0 |
2011 | J & T EXPLORATION LLC | 731.00 | 35.00 | 0 |
2015 | BOCOR HOLDINGS, LLC | 155.00 | 32.00 | 133 |
2016 | BOCOR HOLDINGS, LLC | 3350.00 | 18.00 | 365 |
2017 | BOCOR HOLDINGS, LLC | 5796.00 | 102.00 | 365 |
2018 | BOCOR HOLDINGS, LLC | 1618.00 | 66.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | FORTUNE GAS & OIL | Brine | 0 | 328 |
1991 | FORTUNE GAS & OIL | Brine | 0 | 365 |
1992 | FORTUNE GAS & OIL | Brine | 0 | 365 |
1993 | FORTUNE GAS & OIL | Brine | 0 | 365 |
1994 | FORTUNE GAS & OIL | Brine | 0 | 365 |
1995 | FORTUNE GAS & OIL | Brine | 0 | 365 |
1996 | FORTUNE GAS & OIL | Brine | 0 | 365 |
1997 | FORTUNE GAS & OIL | Brine | 0 | 365 |
1998 | FORTUNE GAS & OIL | Brine | 0 | 365 |
1999 | FORTUNE GAS & OIL | Brine | 0 | 365 |
2000 | FORTUNE GAS & OIL | Brine | 0 | 365 |
2001 | FORTUNE GAS & OIL | Brine | 0 | 365 |
2002 | FORTUNE GAS & OIL | Brine | 0 | 59 |
2006 | J & T EXPLORATION LLC | Brine | 0 | 365 |
2007 | J & T EXPLORATION LLC | Brine | 0 | 0 |
2008 | J & T EXPLORATION LLC | Brine | 0 | 0 |
2009 | J & T EXPLORATION LLC | Brine | 0 | 0 |
2010 | J & T EXPLORATION LLC | Brine | 0 | 0 |
2011 | J & T EXPLORATION LLC | Brine | 0 | 0 |
2015 | BOCOR HOLDINGS, LLC | Brine | 0 | 133 |
2016 | BOCOR HOLDINGS, LLC | Brine | 68 | 365 |
2017 | BOCOR HOLDINGS, LLC | Brine | 148 | 365 |
2018 | BOCOR HOLDINGS, LLC | Brine | 40 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1415238680 | 2007-9-24 0:00: | PW | No Violations | |
-71049254 | 2014-8-7 0:00:0 | PW | No Violations | |
0071049254 | 2014-08-07 | Production Wells | No Violations | My inspection today found no changes since my last inspection. |
0144977718 | 2015-04-07 | Production Wells | No Violations | The sale of J&T Exploration to Bocor Holdings LLC was completed on 2/11/2015. J&T Exploration had a compliance notice on this well for not reporting annual production. The compliance notice can be lifted now that the well is under new ownership. |
0580507237 | 2013-07-16 | Production Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The well and tank battery are in good repair. The tank battery consists a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. The production of this well has not been reported for 2012. I spoke with the well tender Jim about the issue. The company contact information is not valid. |
1179761052 | 2007-05-21 | Production Wells | No Violations | One 110 BBL and one 210 BBL tank on site, mechanical separator. Well head is just north of the shop building. 210 tank has over flowed. There is oil down the side of the tank. Oil on the ground around the tank. Oil is contained within he dike. |
1239718071 | 2009-04-14 | Production Wells | No Violations | Well head is in good repair. Tank battery dike as been repaired. Small spill of oil under the separator, approximately 1/2 gallon of crude. Called number on tank battery left message to clean up spill and return call. Crude is contained in the battery. No chance of the small amount leaving battery. Requested that peat sorb be mixed into crude. |
1324031837 | 2015-05-28 | Production Wells | No Violations | My inspection found the company has installed a new sales line from the tank battery to the meter station. The dike around the tank battery has been rebuilt. No other changes to the location since my last inspection. |
1411559462 | 2014-09-23 | Production Wells | Violations Noted
-- | |
1415238680 | 2007-09-24 | Production Wells | No Violations | Well head is in good repair. There is a small oil spill in the tank battery below the clean out valve. It appears that a gallon or less of oil was spilled when operator was draining the tank. I called J&T and asked that they add some peat or peat dry to the spill to help break down the oil. The 210 bbl tank has over flowed in the past. Operator informed me that they tank had, had a bad riser pipe on it. The pipe has been repaired. |
1418311002 | 2014-12-11 | Production Wells | No Violations | My inspection found the contaminated stone and soil has been removed. The well has been repaired and is currently shut in. No other changes to the well since my last inspection. |
1442847535 | 2015-09-17 | UrbanProduction Wells | No Violations | I was on location for the clean up of the tank battery. The company has hired Canton Oil Well Services to perform the clean up. They have removed both the 100 BBL and the 210 BBL tanks from inside the tank battery and plan on removing them from the location. They will replace both tanks with a new 100 BBL production tank. The company has stacked all of the oil contaminated stone and soil on a liner next to the lease road until a container arrives to remove it from the location. The company is currently in the process of building a new containment dike for the production tank with a liner installed under the stone base. I will check back on 9/18/2015 to see if the oil contaminated stone has been removed from the location. |
144977718 | 2015-4-7 0:00:0 | PW | No Violations | |
1454682214 | 2016-02-04 | UrbanProduction Wells | No Violations | My inspection found the company has installed a new 100 BBL production tank. The 210 BBL production tank and the 100 BBL brine tank are sitting on the lease road. I contacted Tom Huffman, the well tender for Bocor about having the tanks hauled away. The well was placed back into production. No other changes to the location since my last inspection. |
1462829380 | 2015-09-18 | UrbanProduction Wells | No Violations | My inspection found the oil contaminated soil and stone has been removed from the location. The new dike for the tank battery is lined and completed. The new tank will not be installed until the week of 9/21/2015. The well is shut in until the new production tank arrives. The 210 BBL production tank and the 100 BBL brine tank are set off to the side of the lease road and are due to be hauled off location by Canton Oil Well Services the week of 9/21/2015. |
1650807970 | 2015-09-16 | Production Wells | Violations Noted | My inspection found a hole that is 3 ft above the base of the tank was actively leaking oil and brine from the tank. Bocor hired a company to flip and repair the 210 BBL production tank and 100 BBL brine tanks two weeks prior to this incident. There is oil saturated stone that is 2 ft by 5 ft next to the base of the tank. After further investigation I noticed the base stone to the East of the tank, inside the tank battery, was saturated with oil. On the North side of the tank battery the is evidence of oil and brine making it through the sandy soil used for the containment dike and making it 50 ft down the hill heading East of the tank battery. Tom Huffman from Bocor is on location and is currently having a vac truck empty both tanks. The company will have an excavator on location to remove the 210 BBL production tank by the end of the day. A container will be on location in the morning and the company will remove all saturated stone and soil from the affected areas and replaced with new. I will be on location 9/17/2015 to observe the clean up. |
580507237 | 2013-7-16 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1411559462 | US-OH-112107 | 2014-10-14 | Well operation causing pollution and contamination | |
1411559462 | US-OH-112108 | 2014-10-14 | General Safety | |
1411559462 | US-OH-112109 | 2014-10-14 | Well insufficiently equipped to prevent escape of oil and gas | |
1411559462 | US-OH-112110 | 2014-10-14 | Defective casing, leaking well | |
1411559462 | US-OH-112111 | 2014-10-14 | Statement of annual production not filed | |
1650807970 | US-OH-116284 | 2015-11-25 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[9]