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Well ID: 34-055-21799 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Troy Township | |
Operator Name: EXCALIBUR EXPLORATION INC | |
Well Pad ID: | |
Farm/Lease Name: SODO | |
License Status: Producing | |
License Date: 2004-09-20 | |
Spud Date: 2004-10-25 | |
Spud Drilling Contractor: CAPSTAR DRILLING | |
Final Drill Date: 2004-10-29 | |
Well Total Depth: 4253.00 ft | |
Configuration: Vertical | |
Latitude: 41.370000 | |
Longitude: -81.130000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2004-09-20 | Proposed Formations:ORISKANY, CLINTON, Issued Date:9/20/2004, Expired Date:9/20/2005 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Original Spud | 2004-10-25 | RBDMS Rec |
Completed | 2004-10-29 | RBDMS Rec |
Reached Total Depth | 2004-10-29 | RBDMS Rec |
Completion Report Received | 2005-02-17 | RBDMS Rec |
Construction Permit Expires | 2005-09-20 | RBDMS Rec |
Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2005-04-07 | 4082 | 4165 | 40 |
4082 | 4165 | 40 | |
4082 | 4165 | 40 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 15 | 66423 Gal | 37000 | 500 GALLONS HCL ACID |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2004 | EXCALIBUR EXPLORATION INC | 0.00 | 0.00 | 0 |
2005 | EXCALIBUR EXPLORATION INC | 0.00 | 0.00 | 0 |
2006 | EXCALIBUR EXPLORATION INC | 328.00 | 438.00 | 210 |
2007 | EXCALIBUR EXPLORATION INC | 1402.00 | 1362.00 | 365 |
2008 | EXCALIBUR EXPLORATION INC | 2548.00 | 1248.00 | 366 |
2009 | EXCALIBUR EXPLORATION INC | 3307.00 | 1340.00 | 365 |
2010 | EXCALIBUR EXPLORATION INC | 3230.00 | 1093.00 | 365 |
2011 | EXCALIBUR EXPLORATION INC | 2609.00 | 1008.00 | 365 |
2012 | EXCALIBUR EXPLORATION INC | 3643.00 | 1284.00 | 366 |
2013 | EXCALIBUR EXPLORATION INC | 3423.00 | 995.00 | 365 |
2014 | EXCALIBUR EXPLORATION INC | 2780.00 | 932.00 | 365 |
2015 | EXCALIBUR EXPLORATION INC | 3049.00 | 897.00 | 365 |
2016 | EXCALIBUR EXPLORATION INC | 3023.00 | 856.00 | 365 |
2017 | EXCALIBUR EXPLORATION INC | 3437.00 | 728.00 | 365 |
2018 | EXCALIBUR EXPLORATION INC | 3244.00 | 806.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2004 | EXCALIBUR EXPLORATION INC | Brine | 0 | 0 |
2005 | EXCALIBUR EXPLORATION INC | Brine | 1120 | 0 |
2006 | EXCALIBUR EXPLORATION INC | Brine | 1408 | 210 |
2007 | EXCALIBUR EXPLORATION INC | Brine | 1320 | 365 |
2008 | EXCALIBUR EXPLORATION INC | Brine | 931 | 366 |
2009 | EXCALIBUR EXPLORATION INC | Brine | 695 | 365 |
2010 | EXCALIBUR EXPLORATION INC | Brine | 809 | 365 |
2011 | EXCALIBUR EXPLORATION INC | Brine | 395 | 365 |
2012 | EXCALIBUR EXPLORATION INC | Brine | 123 | 366 |
2013 | EXCALIBUR EXPLORATION INC | Brine | 36 | 365 |
2014 | EXCALIBUR EXPLORATION INC | Brine | 19 | 365 |
2015 | EXCALIBUR EXPLORATION INC | Brine | 27 | 365 |
2016 | EXCALIBUR EXPLORATION INC | Brine | 54 | 365 |
2017 | EXCALIBUR EXPLORATION INC | Brine | 30 | 365 |
2018 | EXCALIBUR EXPLORATION INC | Brine | 144 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1369028661 | 2014-10-23 0:00 | PW | No Violations | |
0531094235 | 2015-12-21 | Production Wells | No Violations | My inspection found no changes since my last inspection. No violations found. |
0563538287 | 2007-11-02 | Production Wells | No Violations | Site needs seeded and vegetation established. Operator has recently completed work on the well. The well is past due on reclamation. Well is a pump jack well. Site has been graded, vegetation is not established at this time. Erosion is contained on site. Contacted John from the company informed him that the site needs work. Well head is also leaking gas. Called John, he knows about the leak., well head needs blown down and new rubber on the 4.5 inch needs replaced. |
1216468634 | 2013-10-01 | Production Wells | No Violations | My inspection found the well to be equipped with a pump jack. The annulus valve was open. The well and tank battery are in good repair. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery and the well. The lease road is in stable condition. |
1322055671 | 2011-11-21 | Preliminary Restoration | No Violations | The affected area from drilling has been reclaimed. The well is equipped with a pumping unit. There are two wells producing into the tank battery. The dike is in good repair and is lined with a plastic. The operator has installed a black plastic gas line from the drips at the meter which run into the 210 barrel production tank. This line sits on the surface of the ground going through a horse pasture. The hatch on the production tank is open with the gas line going into it. There is oil and residual product splashed on the outside of the tank and hatch. The land owner stated he gets an odor from the tank when wind shifts. The tank battery also contains compressor unit which was giving off a high pitched noise noticeable from 200 feet away. An identification sign needs to be posted at the well. The owner/operator will be contacted to trench in the black gas line, change the connection to the 210 barrel tank and clean up around the wellhead. The operator should take steps to reduce the noise from the compressor. The lease road going to the well was rutted, blocked by water and extremely soft. I spoke to the land owner in regards to the lease road and he stated that the majority of the damage was caused by the recent combine work on the farm and not from the oil and gas operations. |
1369028661 | 2014-10-23 | Production Wells | No Violations | My inspection found no changes since my last inspection. No violations found. |
1778299504 | 2013-05-02 | Production Wells | No Violations | My inspection found the well to be equipped with a pump jack. The annulus valve was open. The tank battery and well are in good repair. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. |
531094235 | 2015-12-21 0:00 | PW | No Violations | |
563538287 | 2007-11-2 0:00: | PW | No Violations |
For data sources see[9]