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Well ID: 34-055-21837 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Newbury Township | |
Operator Name: ALLIANCE PETROLEUM CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: SURCKLA P | |
License Status: Final Restoration | |
License Date: 2010-07-30 | |
Spud Date: 2005-09-29 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2005-10-04 | |
Well Total Depth: 4030.00 ft | |
Configuration: Vertical | |
Latitude: 41.480000 | |
Longitude: -81.270000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2005-07-18 | Proposed Formations:CLINTON, Issued Date:7/18/2005, Expired Date:7/18/2006 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
Original Spud | 2005-09-29 | RBDMS Rec |
Completed | 2005-10-04 | RBDMS Rec |
Reached Total Depth | 2005-10-04 | RBDMS Rec |
Completion Report Received | 2006-05-10 | RBDMS Rec |
APP | 2010-07-30 | Proposed Formations:CLINTON, Issued Date:7/30/2010, Expired Date:7/29/2012 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2012-06-15 | RBDMS Rec |
Construction Permit Expires | 2012-07-29 | RBDMS Rec |
Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-07-28 | 3834 | 3916 | 80 |
3834 | 3916 | 80 | |
3834 | 3916 | 80 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 80000 Gal | 0 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1197273229 | 2005-10-1 0:00: | DD | No Violations | |
-1717459095 | 2007-1-2 0:00:0 | PL | No Violations | |
-2126319946 | 2007-6-7 0:00:0 | PW | No Violations | |
-400059374 | 2013-7-16 0:00: | FR | No Violations | |
-827435874 | 2006-1-4 0:00:0 | DD | No Violations | |
-931054791 | 2007-6-13 0:00: | PL | No Violations | |
0385410254 | 2013-10-08 | Final Restoration | No Violations | My inspection today found no changes since my last inspection. |
0400059374 | 2013-07-16 | Final Restoration | No Violations | Final Restoration not passed. Well site has large patches of dry-hard soil with no vegetation growing. Tank battery site is still present. Tank batterys dike is still largely intact with the gravel bottom still present. The piping is still present at Tank battery site, with some staining of the gravel. Access road is covered with native vegetation. |
0437848965 | 2015-10-13 | Final Restoration | No Violations | My inspection found the flow line and the tank battery has been removed. The location has been graded, seeded, and strawed. The company still has a sales line riser inside where the tank battery was previously, due to a pipeline right of way on the property. The meter for the pipeline is at the entrance to the location on Pekin Rd. Once vegetation is established on the location, final restoration can be passed. |
0820922727 | 2016-05-31 | Final Restoration | No Violations | My inspection found the flow line and the tank battery has been removed. The location has been graded, seeded, and strawed. The company still has a sales line riser inside where the tank battery was previously, due to a pipeline right of way on the property. The meter for the pipeline is at the entrance to the location on Pekin Rd. Vegetation has been established on the location. Final restoration can be passed. |
0827435874 | 2006-01-04 | Drill / Deepen / Reopen | No Violations | |
0902216777 | 2006-08-24 | Drill / Deepen / Reopen | No Violations | status check |
0924008186 | 2012-06-14 | Plug / Plug Back | No Violations | I was on site today to witness plugging operations. Well had 400 pounds per square inch (psi) pressure on it. Nicks Plugging blew down the well. The well blew down within 5 minutes. During fracturing, this well broke down at 3,800psi and the operator was unable to run sand during the frac job. The operator was going to trip tubing in and spot bottom plug but decided to attempt bull heading bottom plug in. Operator mixed cement and attempted to displace but 20 barrels into the 57.78 barrels of displacement the well locked up. Operator pressured up to 2700psi, and shut down. At 2:18 pm this day, the operator is tripping tubing into the hole to flush cement plug out and spot bottom plug. Operator tripped tubing below the cement and flushed the cement out. Operator will complete tripping tubing into the hole, pack off the well and complete plugging on 06/15/2012. |
0931054791 | 2007-06-13 | Preliminary Restoration | No Violations | On site at the request of the operator. Lease road has been restored and topped with 57s. Drainage has been installed on the east and west side of the lease road. Affected area has been graded, seeded and mulched. Restoration will be passed once vegetation is established. |
1144167252 | 2006-01-13 | Drill / Deepen / Reopen | No Violations | drilling checking for mud on road none found. |
1167422728 | 2006-12-29 | Production Wells | No Violations | On site to check the status of reclamation work. No new work has been completed. Drainage is blocked along the lease road. Lease road is soft and in poor condition. Per operator reclamation will start 01/02/2007. NOV will be issued that day if work is not started. |
1179850797 | 2007-05-22 | Preliminary Restoration | Violations Noted | Lease road has not been restored. Lease road is still bare earth. Lease road is blocking drainage and causing water to accumulate on the adjacent landowners property. Tank battery is not completed. Sink hole to the south of the well head. Tracks from and excavator have not been graded out and area seeded. Edges of affected area have not been blended in. Culvert 100 east of the well head is blocked., larger culvert needs to be installed. Final grading needs completed. Culverts installed and sufficient drainage established. Area seeded. Any debris removed, |
1180115674 | 2007-05-24 | Preliminary Restoration | No Violations | On site with adjacent landowner, Ted and Bruce Close from Alliance Petroleum Corp. Lease road has not been restored. Lease road is blocking drainage and allowing drainage to accumulate on the landowner to the east. Tank battery is not complete, fencing is not up. Sink hole 8X10 south east of the well head is present. Culvert between the well head and tank battery is blocked and not of sufficient size to handle drainage for the area. A pipe line was installed from well #1842 to #1837, affected area from the installation of the pipe line has not been graded and seeded. |
1197273229 | 2005-10-01 | Drill / Deepen / Reopen | No Violations | Company had trouble running 85/8 |
1444761620 | 2015-10-09 | Final Restoration | No Violations | I was on location with Bruce Close a supervisor with Alliance Petroleum. The company has hired CES to remove the flow line and the tank battery. The flow line has been removed and the company is in the process off cutting it into sections for removal. I will return on 10/13/2015 to check the status of the work being performed. |
1717459095 | 2007-01-02 | Preliminary Restoration | No Violations | Operator on site installing culvert at the entrance of the road. Operator is continuing to work on reclamation of the site. |
1797174307 | 2013-09-03 | Final Restoration | No Violations | My inspection today found the well to be plugged. The area around the well has spots where vegetation has not been established. There is pieces of pit liner showing up through the soil. The tank battery has had the equipment removed from the location. The stone is still present in the tank battery as well as the flow line and the sales line portions are above ground. I will need a line waiver and lease road waiver before I can pass the final restoration. I spoke with Bruce Close a supervisor with Alliance about the issues. He stated he will have it taken care of this month. |
2100370253 | 2006-01-13 | Drill / Deepen / Reopen | No Violations | checking road for mud NO MUD no violation |
2126319946 | 2007-06-07 | Production Wells | No Violations | Operator is in the process of restoring the lease road. Operator has installed drainage along the east and west side of the lease road. Ruff grading has been completed south end of the lease road. Site still needs to be seeded and graded. |
385410254 | 2013-10-8 0:00: | FR | No Violations | |
437848965 | 2015-10-13 0:00 | FR | No Violations | |
820922727 | 2016-5-31 0:00: | FR | No Violations | |
902216777 | 2006-8-24 0:00: | DD | No Violations | |
924008186 | 2012-6-14 0:00: | PB | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1179850797 | US-OH-104791 | 2007-05-22 | Failure to restore land surface within 9 mos. (CHANGE) (REPLACE) |
For data sources see[5]