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Well ID: 34-055-21944 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Munson Township | |
Operator Name: DAVID OIL COMPANY LLC | |
Well Pad ID: | |
Farm/Lease Name: HILL | |
License Status: Producing | |
License Date: 2007-05-02 | |
Spud Date: 2007-08-26 | |
Spud Drilling Contractor: GREAT PLAINS EXPLORATION LLC | |
Final Drill Date: 2007-09-02 | |
Well Total Depth: 3990.00 ft | |
Configuration: Vertical | |
Latitude: 41.560000 | |
Longitude: -81.260000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2007-05-02 | Proposed Formations:CLINTON, Issued Date:5/2/2007, Expired Date:5/1/2008 6:00:00 AM, Drilling unit acres:21, Proposed Well Type:OG, Proposed Well Class:POOL |
Completed | 2007-09-02 | |
Reached Total Depth | 2007-09-02 | |
Completion Report Received | 2007-10-17 | |
Construction Permit Expires | 2008-05-01 | |
Change of Owner | 2016-12-14 | Operator changed from 7909, JOHN D OIL & GAS COMPANY to 9836, DAVID OIL COMPANY LLC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2008-01-28 | 3780 | 3827 | 18 |
3780 | 3827 | 18 | |
3780 | 3827 | 18 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 540 Bbl | 100000 | 724M SCF NITROGEN ASSIST |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | JOHN D OIL & GAS COMPANY | 939.00 | 0.00 | 77 |
2008 | JOHN D OIL & GAS COMPANY | 2017.00 | 46.00 | 365 |
2009 | JOHN D OIL & GAS COMPANY | 918.00 | 37.00 | 365 |
2010 | JOHN D OIL & GAS COMPANY | 0.00 | 0.00 | 365 |
2011 | JOHN D OIL & GAS COMPANY | 0.00 | 0.00 | 365 |
2012 | JOHN D OIL & GAS COMPANY | 0.00 | 0.00 | 366 |
2013 | JOHN D OIL & GAS COMPANY | 3488.00 | 0.00 | 365 |
2014 | JOHN D OIL & GAS COMPANY | 3779.00 | 0.00 | 365 |
2015 | JOHN D OIL & GAS COMPANY | 2307.00 | 0.00 | 365 |
2016 | DAVID OIL COMPANY LLC | 368.00 | 0.00 | 61 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | JOHN D OIL & GAS COMPANY | Brine | 80 | 77 |
2008 | JOHN D OIL & GAS COMPANY | Brine | 320 | 365 |
2009 | JOHN D OIL & GAS COMPANY | Brine | 220 | 365 |
2010 | JOHN D OIL & GAS COMPANY | Brine | 0 | 365 |
2011 | JOHN D OIL & GAS COMPANY | Brine | 0 | 365 |
2012 | JOHN D OIL & GAS COMPANY | Brine | 0 | 366 |
2013 | JOHN D OIL & GAS COMPANY | Brine | 0 | 365 |
2014 | JOHN D OIL & GAS COMPANY | Brine | 0 | 365 |
2015 | JOHN D OIL & GAS COMPANY | Brine | 0 | 365 |
2016 | JOHN D OIL & GAS COMPANY | Brine | 0 | 304 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1805091985 | 2018-7-13 0:00: | UP | No Violations | |
-1902991845 | 2013-7-31 0:00: | UP | No Violations | |
0153071191 | 2016-03-16 | UrbanProduction Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The annulus valve is closed. The tank battery, separator, and wellhead are surrounded by a wooden fence. The tank battery consists of a 100 BBL production tank. The dike is in good repair. The load lines on the tanks and the man doors on the fences need locks installed. The heat treated separator has the proper spacing from the wellhead and the tank battery. The proper identification is posted on the tank battery fence. The lease road is in stable condition. I have contacted the company about correcting the issues. |
1223047369 | 2008-10-03 | Preliminary Restoration | Violations Noted | Entrance of the lease road, both sides of the road need graded, seeded and mulched to prevent erosion. Site needs final grading, seeded and mulched. Vegetation needs to be established to prevent erosion. Erosion damage behind well to the east needs controlled and repaired. The 210 tank is more than three feet above the highest portion of the fence. Tank battery is in the woods and not causing nay issues, a waiver will need to be submitted. Well ID sign is up. Well is a pump jack well. Well spacing is good. Site needs final grading, seeded and mulched. Drainage from site is causing erosion behind the well head. Stream bank is being washed away by the drainage. Drainage controls need installed to prevent further erosion damage. Erosion damage needs repaired |
1255960147 | 2009-10-19 | Preliminary Restoration | No Violations | Site has been seeded and vegetation is established. Fences up around well head, heat treat separator and tank battery. 210 BBL tank is above the fence more than 3 feet, have contacted company in the past regarding tank. Tank needs removed or fence needs extended. Lease road is stable. |
153071191 | 2016-3-16 0:00: | UP | No Violations | |
1531493624 | 2018-07-13 | UrbanProduction Wells | Violations Noted | On 7/12/2018, I received a call from Marianne Hartman - DOGRM Emergency Response, with a complaint of a gas leak at this location. Mr. Carl Hill, landowner, called in the complaint to DOGRM. I contacted Mr. Hill about the leak and then proceeded to contact David Oil Company, LLC. I spoke with the operator at David Oil and discussed the leak at this well site. The operator stated she would contact the field supervisor to go out to the site and repair the leak.
I was on site on 7/13/2018, to conduct an inspection, regarding the gas leak. The leak at the well location was still present. The well was a plunger lift assembly and the gate valve on the tubing was closed. The 2 inch flow line valve off of the tubing was closed. There was a 2 inch line off of the well, opposite the 2 inch flow line that had a tapped bull plug and pressure gauge on it. The valve on this line was open and the gas leak was coming from the top of the pressure gauge. I contacted David Oil Company and spoke with the operator regarding the leak. She stated that she would call a well tender to come out and remedy the leak. The well was fenced and locked. The tank battery consisted of a 100 BBL tank and a mechanical separator. Valves on the separator were open. The separator was fenced with a locked door. The 100 BBL tank was diked and fenced. The fence did not have lock on the door. The signage was located at the 100 BBL tank fence but needed to be updated to include the new company name and contact information. Lease access was stable. While I was still on site, the well tender arrived and closed the valve on the leaking gauge. Well leak stopped. Compliance notice closed. |
1805091985 | 2018-07-13 | UrbanProduction Wells | No Violations | On site, waiting for company employee to remedy the leak. The well tender arrived and closed the valve on the 2 inch line with the leaking gauge. Well leak stopped. Compliance notice closed. |
1902991845 | 2013-07-31 | UrbanProduction Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The annulus valve is closed. The well and the tank battery are in good repair and are surrounded by a wooden fence. The tank battery consists of a 100 BBL production tank. The heat treated separator has the proper spacing from the tank battery and is surrounded by a wooden fence. The location does not have any identification signs. The lease road is in stable condition. There has not been any production reported since 2009 and the well is shut in. I will contact the company about the issues. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1223047369 | US-OH-106005 | 2008-10-03 | Failure to restore land surface within 9 mos. (CHANGE) (REPLACE) | |
1531493624 | US-OH-114702 | 2018-09-04 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[9]