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Well ID: 34-055-21959 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Auburn Township | |
Operator Name: ALLIED OIL FIELD SERVICES LTD | |
Well Pad ID: | |
Farm/Lease Name: ORAVEC | |
License Status: Final Restoration | |
License Date: 2014-07-10 | |
Spud Date: 2007-06-20 | |
Spud Drilling Contractor: BIG SKY ENERGY INC. | |
Final Drill Date: 2007-07-22 | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 41.420000 | |
Longitude: -81.230000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2007-06-18 | Proposed Formations:CLINTON, Issued Date:6/18/2007, Expired Date:6/17/2008 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
Completed | 2007-07-22 | DTD: 4460' PER WCR |
Reached Total Depth | 2007-07-22 | DTD: 4460' PER WCR |
Completion Report Received | 2007-09-18 | DTD: 4460' PER WCR |
Change of Owner | 2010-01-28 | Operator changed from 3847, HALL & HORNING SERV INC to 8602, ALLIED OIL FIELD SERVICES LTD |
Correction to Well | 2010-01-29 | UNIT SIZE INCREASED FROM 20 TO 40 ACRES. |
Plugged/Abandoned | 2014-07-08 | DTD: 4460' PER WCR |
APP | 2014-07-10 | Proposed Formations:, Issued Date:7/10/2014, Expired Date:7/9/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Construction Permit Expires | 2015-07-10 | DTD: 4460' PER WCR |
Record Last Modified | 2017-02-15 | DTD: 4460' PER WCR |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2007-12-12 | 3916 | 3992 | 167 |
3916 | 3992 | 167 | |
3916 | 3992 | 167 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 15 | 1500 Bbl | 30000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | HALL & HORNING SERV INC | 999.00 | 0.00 | 126 |
2008 | HALL & HORNING SERV INC | 1993.00 | 75.00 | 366 |
2009 | ALLIED OIL FIELD SERVICES LTD | 268.00 | 0.00 | 72 |
2010 | ALLIED OIL FIELD SERVICES LTD | 1324.00 | 89.00 | 365 |
2011 | ALLIED OIL FIELD SERVICES LTD | 527.00 | 45.00 | 365 |
2012 | ALLIED OIL FIELD SERVICES LTD | 450.00 | 75.00 | 366 |
2013 | ALLIED OIL FIELD SERVICES LTD | 323.00 | 0.00 | 365 |
2014 | ALLIED OIL FIELD SERVICES LTD | 243.00 | 69.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | HALL & HORNING SERV INC | Brine | 0 | 126 |
2008 | HALL & HORNING SERV INC | Brine | 969 | 366 |
2009 | HALL & HORNING SERV INC | Brine | 243 | 195 |
2010 | ALLIED OIL FIELD SERVICES LTD | Brine | 378 | 365 |
2011 | ALLIED OIL FIELD SERVICES LTD | Brine | 153 | 365 |
2012 | ALLIED OIL FIELD SERVICES LTD | Brine | 114 | 366 |
2013 | ALLIED OIL FIELD SERVICES LTD | Brine | 109 | 365 |
2014 | ALLIED OIL FIELD SERVICES LTD | Brine | 21 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1588383809 | 2014-7-7 0:00:0 | PB | No Violations | |
-1988174778 | 2007-6-20 0:00: | DD | No Violations | |
-207913520 | 2015-12-15 0:00 | FR | No Violations | |
-250291760 | 2007-7-9 0:00:0 | DD | No Violations | |
-609086573 | 2007-8-20 0:00: | PL | No Violations | |
0108027674 | 2007-08-20 | Preliminary Restoration | No Violations | Operator was solidifying pits at the time of inspection. Two loads of cement fines brought onto site. Operator was mixing cement into pits. Mud on road, operator had a bobcat with a broom on it cleaning the roads. Operator also had a water truck on site working with the bobcat to clean roads. Fresh water was beginning used to wash road. |
0207913520 | 2015-12-15 | Final Restoration | No Violations | My inspection found the company has removed the flow line. The location has been graded and vegtation has been established. The lease road and gate were installed for farm use before the well was drilled. Final restoration can be passed. |
0250291760 | 2007-07-09 | Drill / Deepen / Reopen | Violations Noted | Big skys rig is on site. Drilling has been completed. 10 of linear has slumped of off the north most pit, south side of the pit. Safety fence is not up, it is stockpiled to the south east of the rig. Site is stable. Lease road is in good repair. I spoke to Randy Hall, he said they are pumping pits down at this time and will be closing pits in the next two days. I informed Randy that in the future safety fence needs to be up, per the permit requirements. Trash and litter around the site should be cleaned up. Pits need to be solidified and closed by Wednesday 07/11/2007. Safety fence needs to be installed per the permit requirements, in the future safety fence needs to be installed immediately after pit construction is completed. |
0507118250 | 2007-06-22 | Drill / Deepen / Reopen | No Violations | Performed a rig inspection. Pit liners in good shape. Depth was 410. Location in good shape. I found no violations at this time. |
0609086573 | 2007-08-20 | Preliminary Restoration | No Violations | On site to check the status of Messenger road. Road was clear of mud and was clean. Operator has brought a load of lime stone onsite for the end of the lease road. |
0778074265 | 2013-10-22 | UrbanProduction Wells | No Violations | My inspection found the well to be equipped with a pump jack. The well and tank battery are in good repair and are surrounded by a chain link fence. The tank battery consists of three 210 BBL production tanks, a 50 BBL brine tank, and three mechanical separators. The proper identification is located on the tank battery and the well. The lease road is in stable condition. The lease road and tank battery are being shared by permit numbers 2-1920 and 2-1877. |
108027674 | 2007-8-20 0:00: | PL | No Violations | |
1184766684 | 2007-07-13 | Drill / Deepen / Reopen | No Violations | Operator had repaired pit liner. Liner was pulled up and secured. I spoke with Dan Horning, liner was 6 above water level. He is going to have the rig crew work on getting liner up further above the fluid level. |
1188927378 | 2007-09-04 | Preliminary Restoration | No Violations | Pits have been filled. Operator is actively grading site at the time of inspection. Operator has added gravel to the entrance of the site. |
1191941751 | 2007-10-09 | Preliminary Restoration | No Violations | Well has been fenced, with green chain link fence and three rows of barbed wire. Well is signed. Well is a pump jack well that is in operation. Site has been graded and seeded. Man door on the fence is locked. |
1218738173 | 2008-08-13 | Preliminary Restoration | No Violations | On site with Dan Horning and Ed Schultz. Site has been seeded and vegetation is established. Site has been graded. Well is in production. Well is fenced and locked per HB-278. Lease road gate is not up at this time. Called Ed Schultz from Hall and Horning on 08/14/2008 requested that gate be installed. Lease road is stable. Rock apron at the road has been installed. |
1249672691 | 2009-08-06 | Production Wells | No Violations | Operator has repair graded site from the oil spill. Area needs seeded. Lease road gate was closed. Man door to the pump jack was locked. |
1271687034 | 2010-04-16 | Production Wells | No Violations | On site in regards to an odor complaint in the area. No leaks or odor noted at the well site. Lease road needs improved for an HB-278 site. Gate was closed. Called the pumper at (440) 537-6995 on 04/19/2010 informed him the lease road needs improvement. Gas meter readings zero LEL and H2S. |
1588383809 | 2014-07-07 | Plug / Plug Back | No Violations | I was on location to witness the plugging of this oil and gas well. Nicks Well Plugging is the contractor doing the plug job for Allied Oil Field. Nicks stripped the rods and tubing out of the hole. Nicks set 1.5 tubing in the well to set the clinton plug. Nicks rigged up, and set the Clinton plug through the 1.5 tubing with 25 sacks of cement and 50 pounds of cottonseed hulls. The tubing was removed from the well. Nicks proceeded to rip the casing at 2800. The well was loaded with water and shut in until the following morning. No violations. |
1762569478 | 2014-08-29 | Final Restoration | No Violations | My inspection found no sign of the well leaking. The stone for the pumpjack needs to be removed and the area needs to bee graded and seeded. The pumpjack and fence needs to be removed from the location. I will pass final restoration when the issues are corrected and I obtain a flow line waiver for the well. |
1845390732 | 2007-06-21 | Drill / Deepen / Reopen | No Violations | Rig on site, work pit has been lined and operator is drilling on fluid. Drill depth 44. Blow pit is not lined, small amount of water was leaking in along a clay seem. Operator was advised to plug the leak with clay and seal the pit with soil sealant. Public road had mud on it, tool pusher was asked to get equipment on site to keep road clean. Roadway apron needs a load of larger rock on it to shack mud from trucks. |
1884157305 | 2007-06-20 | Drill / Deepen / Reopen | No Violations | On site to check the pit construction. Soil is clay. Operator was working on construction of work pit. No soil issues at the time of inspection. Operator was reminded to have equipment on site to clean roads. |
1988174778 | 2007-06-20 | Drill / Deepen / Reopen | No Violations | On site because of complaints of mud on the road. Operator had a broom on site before I arrived, equipment had left the site, by the time I arrived 5:30pm. Operator was reminded again to have equipment on site to keep the roads clean. |
507118250 | 2007-6-22 0:00: | DD | No Violations | |
778074265 | 2013-10-22 0:00 | UP | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0250291760 | US-OH-122571 | 2007-07-10 | Dike or pit not able to prevent escape of Brine or other wastes | |
0250291760 | US-OH-122572 | 2007-07-10 | Permit violation |
For data sources see[9]