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34-057-20004

Well Details

Well ID: 34-057-20004
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Country: United States
State: Ohio
County: Greene
Municipality: Ross Township
Operator Name: TATUM PETROLEUM CO LLC
Well Pad ID:
Farm/Lease Name: KELLY GREENE
License Status: Dry and Abandoned
License Date: 2010-04-15
Spud Date: 2010-08-09
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2010-08-17
Well Total Depth: 3343.00 ft
Configuration: Vertical
Latitude: 39.730000
Longitude: -83.690000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2010-04-15 Proposed Formations:UTICA THRU PRE CAMBRIAN, Issued Date:4/15/2010, Expired Date:4/15/2011 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EDPW
Plugged/Abandoned 2010-08-17
Reached Total Depth 2010-08-17
Completion Report Received 2010-12-03
Construction Permit Expires 2011-04-15
Record Last Modified 2013-04-24

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1404609372 2010-8-19 0:00: PB No Violations
1065556811 2010-08-10 Drill / Deepen / Reopen No Violations - Received phone call of surface casing to be set and cemented. Cementer to be on location at 7:30 PM.

- Left home at 5:15 PM and on location 6:15 PM, 8 5/8 inch casing starting to be installed into 11 inch borehole. 4 joints of casing installed and tighten with cathead, next joint unable to tighten properly, contact Mike Power Tong Service to complete tightening joints of casing. Wait for power tong to arrive on site. Install 406.05 feet of 8 5/8 inch casing and tighten joints with power tongs. 117 sacks of cement with 350 lbs of accelerator and 250 lbs of cotton seed hulls pumped into borehole annulus. Plug down at 1:30 AM 8/11/2010 arrive home at 2:30 AM

1281970354 2010-08-09 Drill / Deepen / Reopen No Violations - Drill rig up, pits dug and lined, 3 water tanks on site, water being hauled in and drill mud being mixed. Operator plans to start drilling this afternoon.

- Kilbarger rig number 5 doing the drilling, Gary Smith tool pusher.

1281982835 2010-08-11 Drill / Deepen / Reopen No Violations - On site for BOP test, several attempts were made but test failed. BOP was tighten down more on the 8 5/8 inch casing, all lines connected to BOP were tighten. Foam was flushed from the drill string and fresh water pumped down. BOP retested at 500 psi and passed.
1282236431 2010-08-16 Plug / Plug Back No Violations - Received phone call to plug well (Dry Hole). Cementer to arrive at 10:30, left at 9:30 arrive on location at 10:15. Formation Cementing contactor on location and laying out lines. Drilling contactor circulation well, 3 inch drill pipe run into well at a depth of 3,313 feet.

- plugs were set at - the bottom which will cover the Mt. Simon, the Knox & Trempealeau, the Trenton, at the surface casing (100 out and 100 in) and the surface (ground level). Before the last plug was pump waited to see if spacer would settle, place bridge plug into borehole to help hole plug into place.

1282840591 2010-08-24 Drill / Deepen / Reopen No Violations - The drill and drilling support equipment has been removed from drill site. All the pits have been drained, backfilled and rough graded with topsoil mounted on top of the filled in pits. Notices hydraulic oil filters and trash on location, contacted Gary Smith of Kilbarger to clean up and remove filters.

- One portable water tank, one large track hoe and one dozer still on location. - The hydralic oil filter and trash was removed from location by drilling companys tool pusher and was contacted on this matter.

1285599078 2010-09-14 Preliminary Restoration No Violations - The area has been final graded, with all drill equipment removed from the site. The drill site area will revert back to agricultural farming.

- Most of the lease road has been removed, the area of the road left will be used for access to the agricultural farm field.

1404609372 2010-08-19 Plug / Plug Back No Violations - Drilling support equipment being remove from site, rig tower down. One of the pit has been drained, filled in and rough graded.

For data sources see[4]

References