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34-059-20711

Well Details

Well ID: 34-059-20711
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Country: United States
State: Ohio
County: Guernsey
Municipality: Richland Township
Operator Name: MILEY GAS COMPANY
Well Pad ID:
Farm/Lease Name: OK RICH-OIL
License Status: Final Restoration
License Date: 2016-06-07
Spud Date: 1955-07-09
Spud Drilling Contractor:
Final Drill Date: 1955-07-02
Well Total Depth: 405.00 ft
Configuration: Vertical
Latitude: 39.930000
Longitude: -81.400000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1955-07-02 IP. NAT OIL-15 BBLS/24 HRS. ? FDT SHALE / Change in location per doug bennett inspection 3-8-16 ALE CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER #9998 TO OWNER ON 6/2/2016 CM.
Reached Total Depth 1955-07-02 IP. NAT OIL-15 BBLS/24 HRS. ? FDT SHALE / Change in location per doug bennett inspection 3-8-16 ALE CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER #9998 TO OWNER ON 6/2/2016 CM.
Original Spud 1955-07-09 IP. NAT OIL-15 BBLS/24 HRS. ? FDT SHALE / Change in location per doug bennett inspection 3-8-16 ALE CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER #9998 TO OWNER ON 6/2/2016 CM.
Change of Owner 2016-06-02 Operator changed from 9998, HISTORIC OWNER to 5429, MILEY GAS COMPANY
APP 2016-06-07 Proposed Formations:SHALE, Issued Date:6/7/2016, Expired Date:6/7/2018 12:00:00 PM, Drilling unit acres:100, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-08-24 IP. NAT OIL-15 BBLS/24 HRS. ? FDT SHALE / Change in location per doug bennett inspection 3-8-16 ALE CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER #9998 TO OWNER ON 6/2/2016 CM.
Record Last Modified 2017-05-25 IP. NAT OIL-15 BBLS/24 HRS. ? FDT SHALE / Change in location per doug bennett inspection 3-8-16 ALE CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER #9998 TO OWNER ON 6/2/2016 CM.
Construction Permit Expires 2018-06-07 IP. NAT OIL-15 BBLS/24 HRS. ? FDT SHALE / Change in location per doug bennett inspection 3-8-16 ALE CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER #9998 TO OWNER ON 6/2/2016 CM.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2016 MILEY GAS COMPANY 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2016 MILEY GAS COMPANY Brine 0 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1484858527 2016-3-29 0:00: PW No Violations 1.00
-801380358 2016-9-7 0:00:0 PB No Violations
0312986791 2016-08-18 Production Wells No Violations On the day of my inspection I witnessed Miley Gas Co. rigged up over the 6.625 inch casing. Appalachian Well Surveys was onsite and perforated the 6.625 inch casing at 325 feet with 4 shots and at 150 feet with 4 shots. MGC will trip tubing back in and commence plugging on Monday.
0394996848 2016-03-07 Production Wells No Violations On the day of my inspection I witnessed the well was equipped with 6.625 inch casing, 2 inch tubing and rods with valves in the closed position. Production equipment included 2-100bbl tanks shared with 22381, 20602 and 22159 within an earthen dike. Jeff Miley of Miley Gas Co. claims he is the owner of the said well and is trying to get it transferred into his name so that it can be plugged.
0801380358 2016-09-07 Plug / Plug Back No Violations On the day of my inspection I witnessed the location has been graded with seed and straw in place.
1145061519 2016-08-25 Plug / Plug Back No Violations On the day of my inspection I witnessed cement remained at the surface. Instructed operator to cut casing off 30 inches below grade and install metal plate identifying well and reclaim according to ORC 1509.072B.
1472079337 2016-08-24 Plug / Plug Back No Violations The purpose of my inspection today is to witness plugging operations for the OK Rich-Oil, well number 7, with the permit number 3405920711. The well is owned by Miley Gas Company. Producing formation is Shale and the total depth is 505 feet. Miley Gas Company, Cemenco, and the Muskingum County Watershed District Representative Brad Janssen were on location. During my inspection Cemenco set a plug from 505 feet to 255 feet with 44 sacks of Class A cement through the 2 inch diameter tubing. Circulation was achieved. Following the plug, .75 barrels of fresh water were pumped for displacement Miley Gas Company pulled 11 joints of the 2 inch diameter tubing out of the hole. Cemenco set a plug from 255 feet to surface with 37 sacks of Class A cement with 2% Gel through the 2 inch tubing. Miley Gas Company pulled the remaining 12 joints of the 2 inch diameter tubing out of the hole. Cemenco topped the well off with 3 sacks of Class A cement and the cement stayed at surface.
1484858527 2016-03-29 Production Wells No Violations On the day of my inspection I met with Muskingum County Watershed District Representatives Mark Swiger, John Watkins and Brad Janssen along with Miley Gas Co. Owner Jeff Miley to discuss upcoming plugging of well, pit placement and erosion control measures for the location.
1798452871 2016-12-05 Final Restoration No Violations On the day of my inspection I witnessed that the site passed final restoration according to ORC 1509.072B.
312986791 2016-8-18 0:00: PW No Violations 2.50
394996848 2016-3-7 0:00:0 PW No Violations 1.50

For data sources see[7]

References