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Well ID: 34-059-21649 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Washington Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: COLE DECAR UNIT | |
License Status: Final Restoration | |
License Date: 2013-11-18 | |
Spud Date: 1973-03-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1973-03-29 | |
Well Total Depth: 5825.00 ft | |
Configuration: Vertical | |
Latitude: 40.180000 | |
Longitude: -81.380000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1973-03-13 | |
Completed | 1973-03-29 | |
Reached Total Depth | 1973-03-29 | |
CO | 1980-07-11 | 2143 CARLESS RESOURCES INC GeoDate 7/11/80 |
Change of Owner | 1998-06-15 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2013-11-18 | Proposed Formations:CLINTON, Issued Date:11/18/2013, Expired Date:11/18/2015 12:00:00 PM, Drilling unit acres:135, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-03-27 | |
Construction Permit Expires | 2015-11-18 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5648 | 5684 | 0 |
5648 | 5684 | 0 | |
5648 | 5684 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2036 Bbl | 23400 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | ZILKHA ENERGY INC | 3951.00 | 1.00 | 299 |
1987 | ZILKHA ENERGY INC | 3110.00 | 1.00 | 212 |
1989 | CARLESS RESOURCES INC | 5383.00 | 0.00 | 355 |
1990 | CARLESS RESOURCES INC | 3913.00 | 0.00 | 365 |
1991 | CARLESS RESOURCES INC | 2384.00 | 35.00 | 365 |
1992 | CARLESS RESOURCES INC | 1563.00 | 0.00 | 365 |
1993 | CARLESS RESOURCES INC | 3775.00 | 0.00 | 365 |
1994 | CARLESS RESOURCES INC | 4206.00 | 0.00 | 365 |
1995 | CARLESS RESOURCES INC | 3505.00 | 0.00 | 365 |
1996 | CARLESS RESOURCES INC | 2587.00 | 0.00 | 365 |
1997 | CARLESS RESOURCES INC | 1762.00 | 0.00 | 365 |
1998 | EXCO - NORTH COAST ENERGY INC | 2464.00 | 0.00 | 365 |
1999 | EXCO - NORTH COAST ENERGY INC | 2027.00 | 0.00 | 365 |
2000 | EXCO - NORTH COAST ENERGY INC | 1556.00 | 0.00 | 365 |
2001 | EXCO - NORTH COAST ENERGY INC | 1019.00 | 0.00 | 365 |
2002 | EXCO - NORTH COAST ENERGY INC | 1254.00 | 0.00 | 365 |
2003 | EXCO - NORTH COAST ENERGY INC | 3566.00 | 0.00 | 365 |
2004 | EXCO - NORTH COAST ENERGY INC | 1442.00 | 0.00 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | 1247.00 | 0.00 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | 1950.00 | 0.00 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | 563.00 | 0.00 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1207077732 | 2006-12-13 0:00 | PW | No Violations | |
-1353807882 | 2006-1-13 0:00: | PW | No Violations | |
-1432965705 | 2014-3-24 0:00: | PB | No Violations | |
-2025606893 | 2004-1-15 0:00: | PW | No Violations | |
-676336116 | 2005-6-14 0:00: | PW | No Violations | |
-698726723 | 2014-3-26 0:00: | PB | No Violations | |
0534268449 | 2014-08-12 | Final Restoration | No Violations | On the date of inspection I witnessed that a 100bbl steel tank and a steel section of catwalk were still present on the site. The site will also need further grading and seeding. At this time the well does not pass final restoration per ORC 1509.072 (B). |
0676336116 | 2005-06-14 | Production Wells | No Violations | STATUS CHECK. OIL WELL(BIG OIL PRODUCTION.) |
0698726723 | 2014-03-26 | Plug / Plug Back | No Violations | On the day of my inspection, I witnessed Appalachian Well Service run there wire line down the 1.5 tubing to a depth of 4712 and shot the tubing, then Chipco pulled all the tubing, at that point Appalachian Well Service ran there wire line down to the Big Lime formation and placed ten shots from 4012 to 4022. Chipco ran the 1.5 tubing back in the well to a depth of 4660, at that point I witnessed Chipco LLC displace a 400 Class A cement bottom hole plug, then the rig hands pulled twenty joints of the 1.5 tubing and Chipco LLC displaced a 200 Class A cement plug in the Big Lime formation. I instructed the operator to tag the plug in Big Lime formation on the following day. |
0971256122 | 2004-02-26 | Production Wells | No Violations | STATUS CHECK |
1140717499 | 2006-02-23 | Production Wells | No Violations | STATUS CHECK |
1207077732 | 2006-12-13 | Production Wells | No Violations | PRODUCING WELL |
1353807882 | 2006-01-13 | Production Wells | No Violations | STATUS CHECK |
1432965705 | 2014-03-24 | Plug / Plug Back | No Violations | On the day of my inspection the operator for Chipco reported to me the well was reading sixty parts per million of H2S gas from there Drager dector, I witnessed Chipco pump thirty barrels of sulfur kill down the back side of the well, I then checked the parts per million of H2S gas with my Sperian gas dector and no reading was present. |
1546265750 | 2006-02-08 | Production Wells | No Violations | STATUS CHECK |
1595798158 | 2014-09-25 | Final Restoration | No Violations | On the day of my inspection I witnessed that the site passed final restoration according to ORC 1509.072B. |
2001662764 | 2014-03-25 | Plug / Plug Back | No Violations | On the day of my inspection, I witnessed the welder for Chipco weld ears on the 8.625 surface casing so the rig could pull tension and make an attempt to stand the casing back up straight. Appalachian Well Service then ran there wire line down the 1.5 tubing and set down at 4712, at that point Appalachian Well Service made two attempts to shot the tubing but there gun failed, another wire line truck was coming to the location on the following morning. |
2025606893 | 2004-01-15 | Production Wells | No Violations | DIKE WILL NEED RE-WORKED |
534268449 | 2014-8-12 0:00: | FR | No Violations | 1.50 |
971256122 | 2004-2-26 0:00: | PW | No Violations |
For data sources see[9]