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Well ID: 34-059-21895 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Valley Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: SMITH-DYER | |
License Status: Final Restoration | |
License Date: 2011-04-13 | |
Spud Date: 1975-10-03 | |
Spud Drilling Contractor: | |
Final Drill Date: 1975-10-17 | |
Well Total Depth: 5255.00 ft | |
Configuration: Vertical | |
Latitude: 39.940000 | |
Longitude: -81.550000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1975-10-01 | 182 BELDEN & BLAKE CO GeoDate 10/1/75 |
Original Spud | 1975-10-03 | |
Completed | 1975-10-17 | |
Reached Total Depth | 1975-10-17 | |
Change of Owner | 2002-08-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC |
Change of Owner | 2009-11-06 | Operator changed from 1966, PETROX, INC to 7681, B & B OIL-N-GAS LLC |
Change of Owner | 2010-05-06 | Operator changed from 7681, B & B OIL-N-GAS LLC to 1634, NORTHWOOD ENERGY CORP |
APP | 2011-04-13 | Proposed Formations:CLINTON, Issued Date:4/13/2011, Expired Date:4/12/2013 12:00:00 PM, Drilling unit acres:40.42, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2011-05-18 | |
Record Last Modified | 2013-03-14 | |
Construction Permit Expires | 2013-04-12 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5102 | 5123 | 2 |
5102 | 5123 | 2 | |
5102 | 5123 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 72000 Gal | 50000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ENTERPRISE ENERGY CORP | 3133.00 | 1124.00 | 0 |
1985 | OXFORD OIL | 2960.00 | 1041.00 | 365 |
1986 | OXFORD OIL | 1945.00 | 917.00 | 365 |
1987 | BELDEN & BLAKE CORPORATION | 2289.00 | 699.00 | 365 |
1988 | OXFORD OIL | 1635.00 | 596.00 | 365 |
1990 | BELDEN & BLAKE CORPORATION | 1113.00 | 391.00 | 352 |
1991 | BELDEN & BLAKE CORPORATION | 832.00 | 427.00 | 365 |
1992 | BELDEN & BLAKE CORPORATION | 1381.00 | 208.00 | 281 |
1993 | BELDEN & BLAKE CORPORATION | 838.00 | 419.00 | 345 |
1994 | BELDEN & BLAKE CORPORATION | 1012.00 | 263.00 | 223 |
1995 | BELDEN & BLAKE CORPORATION | 833.00 | 342.00 | 306 |
1996 | BELDEN & BLAKE CORPORATION | 934.00 | 339.00 | 321 |
1997 | BELDEN & BLAKE CORPORATION | 1196.00 | 205.00 | 309 |
1998 | BELDEN & BLAKE CORPORATION | 450.00 | 116.00 | 174 |
1999 | BELDEN & BLAKE CORPORATION | 2.00 | 49.00 | 35 |
2000 | BELDEN & BLAKE CORPORATION | 0.00 | 43.00 | 7 |
2001 | BELDEN & BLAKE CORPORATION | 0.00 | 0.00 | 161 |
2002 | PETROX, INC | 39.00 | 0.00 | 30 |
2003 | PETROX, INC | 59.00 | 0.00 | 365 |
2004 | PETROX, INC | 71.00 | 0.00 | 365 |
2005 | PETROX, INC | 90.00 | 0.00 | 365 |
2006 | PETROX, INC | 48.00 | 0.00 | 120 |
2007 | PETROX, INC | 0.00 | 0.00 | 0 |
2008 | PETROX, INC | 0.00 | 0.00 | 0 |
2009 | PETROX, INC | 0.00 | 0.00 | 0 |
2010 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ENTERPRISE ENERGY CORP | Brine | 200 | 0 |
1985 | OXFORD OIL | Brine | 0 | 365 |
1986 | OXFORD OIL | Brine | 0 | 365 |
1987 | BELDEN & BLAKE CORPORATION | Brine | 2 | 365 |
1988 | OXFORD OIL | Brine | 0 | 365 |
1990 | BELDEN & BLAKE CORPORATION | Brine | 66 | 352 |
1991 | BELDEN & BLAKE CORPORATION | Brine | 77 | 365 |
1992 | BELDEN & BLAKE CORPORATION | Brine | 6 | 281 |
1993 | BELDEN & BLAKE CORPORATION | Brine | 53 | 345 |
1994 | BELDEN & BLAKE CORPORATION | Brine | 22 | 223 |
1995 | BELDEN & BLAKE CORPORATION | Brine | 46 | 306 |
1996 | BELDEN & BLAKE CORPORATION | Brine | 51 | 321 |
1997 | BELDEN & BLAKE CORPORATION | Brine | 39 | 309 |
1998 | BELDEN & BLAKE CORPORATION | Brine | 38 | 174 |
1999 | BELDEN & BLAKE CORPORATION | Brine | 416 | 35 |
2000 | BELDEN & BLAKE CORPORATION | Brine | 82 | 7 |
2001 | BELDEN & BLAKE CORPORATION | Brine | 0 | 161 |
2002 | PETROX, INC | Brine | 0 | 30 |
2003 | PETROX, INC | Brine | 0 | 365 |
2004 | PETROX, INC | Brine | 0 | 365 |
2005 | PETROX, INC | Brine | 0 | 365 |
2006 | PETROX, INC | Brine | 0 | 120 |
2007 | PETROX, INC | Brine | 0 | |
2008 | PETROX, INC | Brine | 0 | 0 |
2009 | PETROX, INC | Brine | 0 | 0 |
2010 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1049695139 | 2011-5-18 0:00: | PB | No Violations | 1.50 |
-1151034205 | 2010-6-4 0:00:0 | PW | No Violations | |
-1375299585 | 2011-4-25 0:00: | PB | No Violations | |
-538801388 | 2011-4-26 0:00: | PB | No Violations | |
-661531029 | 2010-4-1 0:00:0 | PW | No Violations | |
-774580486 | 2011-5-11 0:00: | PB | No Violations | |
-864116350 | 2005-4-18 0:00: | PW | No Violations | |
-865775819 | 2012-2-2 0:00:0 | FR | No Violations | |
-876640094 | 2004-1-7 0:00:0 | PW | No Violations | |
-884514354 | 2011-4-11 0:00: | PW | No Violations | |
-984300164 | 2011-5-18 0:00: | PB | No Violations | 1.00 |
0423066425 | 2011-04-07 | Production Wells | No Violations | Inspection revealed that service rig operator retrived 1200 of 4.5 out og hole today they will run impression block in tomorrow to see whats in hole they assume that tubing top should be at 600+-. |
0538801388 | 2011-04-26 | Plug / Plug Back | No Violations | Stopped by service rig for update they were still attempting to retrieve tubing from well with no luck as of this afternoon they will try again tomorrow. |
0586950241 | 2005-05-18 | Production Wells | No Violations | ID REPOSTED. |
0661531029 | 2010-04-01 | Production Wells | No Violations | Inspection revealed that well is shut in at present time will call company and discuss future plans for said well.
Well is equipped with pumping unit and tubing and rods all valves at wellhead were shut on the day of my inspection, no production has been reported on well since 2006. |
0774580486 | 2011-05-11 | Plug / Plug Back | No Violations | Stopped by service rig for update they should be ready to set bottom plug tomorrow. |
0864116350 | 2005-04-18 | Production Wells | No Violations | STATUS CHECK |
0865775819 | 2012-02-02 | Final Restoration | No Violations | Well site meets ORC 1509.072. |
0876640094 | 2004-01-07 | Production Wells | No Violations | STATUS CHECK. ADAMS EQUIPMENT SALES, LEE ADAMS. |
0884514354 | 2011-04-11 | Production Wells | No Violations | On site to witness service rig crew attempt to retrieve tubing from well it is parted@638; down the hole and once removed they will bring out another tubing string to set bottom hole plug and possibly plug well. |
0979264199 | 2005-06-03 | Preliminary Restoration | No Violations | STATUS CHECK, ID REPOSTED. |
0984300164 | 2011-05-18 | Plug / Plug Back | No Violations | Accompanied Dave Ball with Josh Garland on inspection. Well bore was topped off with cement. |
1040474209 | 2011-03-29 | Production Wells | No Violations | Stopped by service rig for update,they were still trying to fish parted casing from hole there overshot was not connecting with pipe properly and they were going to Allied Machine Works to inquire about a better type of fishing tool to retrieve pipe with. |
1049695139 | 2011-05-18 | Plug / Plug Back | No Violations | Accompanied D. Ball on clay surface cement job. |
1151034205 | 2010-06-04 | Production Wells | No Violations | Stopped by service rig for update they were trying to fish tubing out of well, they got rods and pump pulled out but tubing is rotted off at approximately 120 down the hole. |
1174339977 | 2011-05-18 | Plug / Plug Back | No Violations | Topped off well with cement 200-0 60 sacks cement. |
1298113467 | 2011-02-18 | Production Wells | No Violations | Stopped by service rig for update on trying to retrieve tubing from well it was rotted off in hole@400 rig operator has overshot on tubing trying to work it free, will check back later on progress. |
1299267413 | 2011-03-04 | Production Wells | No Violations | Stopped by service rig for update they were trying to pull parted tubing down in well and it parted again they were in process of coming out of hole to see what they recovered from well bore. |
1302631480 | 2011-04-12 | Production Wells | No Violations | Stopped by service rig for update they were still trying to get overshot on fish they were@1220 once attached they will try and retrieve tubing from well. |
1303344937 | 2011-04-20 | Plug / Plug Back | No Violations | Stopped by service rig to check on progress on fishing job rig crew had 2.875 over 1.5 tubing but overshot would not bite on tubing so decision was made to pull 2.875 and replace grapple in fishing tools and try and get back on it tomorrow. |
1375299585 | 2011-04-25 | Plug / Plug Back | No Violations | Stopped by service rig for update the rig crew was still trying to retrieve parted tubing from well so they could run plugging string in well to set bottom hole plug. |
1492137133 | 2011-05-10 | Plug / Plug Back | No Violations | Inspection revealed that operator is still attempting to mill up tubing so they can get a better hold of it but as of this afternoon all efforts have failed. |
1610842196 | 2011-04-27 | Plug / Plug Back | No Violations | Stopped by service rig for update on upcoming plugging operation, rig crew stated that they have 4.5 back together and will attempt to fish for tubing tomorrow. |
1885008487 | 2011-05-09 | Production Wells | No Violations | Stopped by service rig for update they were still trying to fish tubing from hole. |
1997322787 | 2011-04-28 | Plug / Plug Back | No Violations | Stopped by service rig for update they were still trying to recover tubing from well rig operator stated that they would attempt to retrieve more tubing tomorrow. |
2067764441 | 2011-04-21 | Plug / Plug Back | No Violations | Stopped by service rig for update they were still trying to recover lost tubing downhole 4.5 is parted@1230 and top of tubing string is@approximatly 1400+-. |
423066425 | 2011-4-7 0:00:0 | PW | No Violations | |
586950241 | 2005-5-18 0:00: | PW | No Violations | |
979264199 | 2005-6-3 0:00:0 | PL | No Violations |
For data sources see[9]