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Well ID: 34-059-22455 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Wheeling Township | |
Operator Name: JOHN F WILLIAMS OIL FIELD SER | |
Well Pad ID: | |
Farm/Lease Name: KINNER | |
License Status: Final Restoration | |
License Date: 2014-01-10 | |
Spud Date: 1978-11-16 | |
Spud Drilling Contractor: GREAT LAKES DRILLING | |
Final Drill Date: 1979-04-07 | |
Well Total Depth: 5055.00 ft | |
Configuration: Vertical | |
Latitude: 40.210000 | |
Longitude: -81.610000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1978-11-16 | |
Completed | 1979-04-07 | |
Reached Total Depth | 1979-04-07 | |
CO | 1980-12-04 | 2074 OIL & GAS SERVICES INC GeoDate 12/4/80 |
Completion Report Received | 1981-11-06 | |
CO | 1993-12-15 | 4664 HOCHSTETLER RAYMD WL SRV GeoDate 12/4/80 |
Change of Owner | 2000-04-13 | Operator changed from 4664, HOCHSTETLER RAYMD WL SRV to 503, WILLIAMS J F OILFIELD SER |
APP | 2014-01-10 | Proposed Formations:CLINTON, Issued Date:1/10/2014, Expired Date:1/10/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-07-01 | |
Construction Permit Expires | 2016-01-10 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 46000 Gal | 45000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | HOCHSTETLER RAYMD WL SRV | 144.00 | 0.00 | 365 |
2000 | JOHN F WILLIAMS OIL FIELD SER | 665.00 | 0.00 | 365 |
2001 | JOHN F WILLIAMS OIL FIELD SER | 628.00 | 0.00 | 365 |
2002 | JOHN F WILLIAMS OIL FIELD SER | 311.00 | 0.00 | 365 |
2003 | JOHN F WILLIAMS OIL FIELD SER | 139.00 | 0.00 | 365 |
2004 | JOHN F WILLIAMS OIL FIELD SER | 495.00 | 0.00 | 365 |
2005 | JOHN F WILLIAMS OIL FIELD SER | 280.00 | 0.00 | 365 |
2006 | JOHN F WILLIAMS OIL FIELD SER | 259.00 | 0.00 | 365 |
2007 | JOHN F WILLIAMS OIL FIELD SER | 247.00 | 0.00 | 365 |
2008 | JOHN F WILLIAMS OIL FIELD SER | 152.00 | 0.00 | 365 |
2009 | JOHN F WILLIAMS OIL FIELD SER | 172.00 | 10.00 | 365 |
2010 | JOHN F WILLIAMS OIL FIELD SER | 123.00 | 0.00 | 365 |
2011 | JOHN F WILLIAMS OIL FIELD SER | 116.00 | 0.00 | 365 |
2012 | JOHN F WILLIAMS OIL FIELD SER | 219.00 | 0.00 | 366 |
2013 | JOHN F WILLIAMS OIL FIELD SER | 371.00 | 0.00 | 365 |
2014 | JOHN F WILLIAMS OIL FIELD SER | 489.00 | 6.00 | 365 |
2015 | JOHN F WILLIAMS OIL FIELD SER | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | HOCHSTETLER RAYMD WL SRV | Brine | 0 | 365 |
2000 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2001 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2002 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2003 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2004 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2005 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2006 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2007 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2008 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2009 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2010 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2011 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2012 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 366 |
2013 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2014 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
2015 | JOHN F WILLIAMS OIL FIELD SER | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1667743982 | 2008-11-21 0:00 | PW | No Violations | |
-2059741839 | 2007-7-24 0:00: | PW | No Violations | |
-226331343 | 2011-10-14 0:00 | PW | No Violations | |
0028165282 | 2011-10-14 | Production Wells | Violations Noted | Received complaint of idle well on Edna Schrok property. Inspected site, with landowner, and determined that well is incapable of production in its present state of repair. Well is equipped with 8 5/8 surface casing and 4.5 production casing. There is a plug in top of casing collar and the 2 plumbing at well head is rotted beyond repair. There is no identification on the tank or wellhead.
Plug or produce well or file for Temporary Inactive status. Failure to comply may result in bond forfeiture. If well is placed back into production the well location must be properly identified and production must be reported. |
0221066072 | 2006-12-28 | Production Wells | No Violations | ID REPOSTED. WELL BACK IN PRODUCTION |
0226331343 | 2011-10-14 | Production Wells | No Violations | FOLLOW UP TO NOV # 28165282 Received complaint of idle well on Edna Schrok property. Inspected site, with landowner, and determined that well is incapable of production in its present state of repair. Well is equipped with 8 5/8 surface casing and 4.5 production casing. There is a plug in top of casing collar and the 2 plumbing at well head is rotted beyond repair. There is no identification on the tank or wellhead.
Plug or produce well or file for Temporary Inactive status. Failure to comply may result in bond forfeiture. If well is placed back into production the well location must be properly identified and production must be reported. |
0232969011 | 2005-09-27 | Production Wells | No Violations | STATUS CHECK. WELL IN PRODUCTION. |
0292078053 | 2011-10-14 | Production Wells | No Violations | FOLLOW UP TO NOV # 28165282 Received complaint of idle well on Edna Schrok property. Inspected site, with landowner, and determined that well is incapable of production in its present state of repair. Well is equipped with 8 5/8 surface casing and 4.5 production casing. There is a plug in top of casing collar and the 2 plumbing at well head is rotted beyond repair. There is no identification on the tank or wellhead.
Plug or produce well or file for Temporary Inactive status. Failure to comply may result in bond forfeiture. If well is placed back into production the well location must be properly identified and production must be reported. |
0454194602 | 2015-03-24 | Production Wells | No Violations | On the day of my inspection following up on NOV-28165282, I witnessed the production equipment included a 100bbl tank and a horizontal separator shared with the Kinner 2 - 34059226520000 within an earthen dike. The well was equipped with 8.625 inch casing and 4.5 inch casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. I made call to JF Williams Oilfield Services requesting an update. Mr. Williams stated that he has a plugging permit and is not sure when he will be able to plug said well and he may possibly try to get the well back into production. Proper identification was in place with production records up to date. |
0737838190 | 2014-03-17 | Production Wells | No Violations | My inspection at the well reveals, the 4x2 swedge and valve has been replaced and is closed, the well still remains idle, the permit to plug was issued on 01/10/2014 and expires on 01/10/2016. |
0824769404 | 2015-07-02 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed top of cement was at 5 feet from surface and restoration was underway with pit closure scheduled for this afternoon. |
1126089412 | 2015-06-24 | Production Wells | No Violations | On the day of my inspection following up on NOV-28165282 and complaint ID 5003, I received a call from JF Williams Oil Field Services and John stated that they plan on beginning plugging of the well in the next week. Upon arrival I witnessed that equipment is being spotted for plug job. |
1429621524 | 2015-04-21 | Production Wells | No Violations | On the day of my inspection following up on NOV-28165282 and complaint ID 5003, I witnessed the production equipment included a 100bbl tank, a horizontal separator and domestic gas service shared with the Kinner 2 - |
1435660658 | 2015-06-30 | Plug / Plug Back | No Violations | On the day of my inspection following up on NOV-28165282 and complaint ID 5003, I witnessed that Matheny Well Service had ran 2.375 inch tubing to 4816 and Petroset Cementing Services was on site gained circulation and pumped a 500 foot Class A 2% Gel bottom hole plug from 4816 feet to 4316 feet. Cement was displaced with 16.5bbls of fresh water. Matheny Well Service tripped out 2.375 inch tubing out and prepared to rip 4.5 inch casing. |
1510230191 | 2016-06-21 | Final Restoration | No Violations | On the day of my inspection I met with JF Williams representatives John Williams and Dennis Williams and discussed the restoration that was approved on 8/17/15. The land is owned by Edna Shrock and is farmed by Larry Priestly. Mr. Williams stated that Mr. Priestly is not happy with the restoration. The site was reclaimed and seeded with 75lbs of Alfalfa Hay and Pasture Mixture. Inspection revealed that the crop has not been removed from the reclaimed area with good growth and three areas of light vegetation. Recommendation was made to Mr. Williams to have the crop removed and take a closer look. Mr. Williams was advised that the site met ORC 1509.072B as the equipment, debris were removed and excavations were filled. The soil had been graded, terraced with the soil being bound to prevent substantial erosion and sedimentation. |
1667743982 | 2008-11-21 | Production Wells | No Violations | PRODUCING WELL. STRIP MINE AREA. |
1724357179 | 2015-08-17 | Final Restoration | No Violations | On the day of my inspection I witnessed that the site passed final restoration according to ORC 1509.072B. |
1956066356 | 2013-12-05 | Production Wells | No Violations | On the day of my follow-up inspection, I found the well to be idle also incapable of production, there is four inch and a half inch production casing with a 4x2 swedge and valve, the top of the swedge was broke off, no gas was venting, I made contact with the company to address the issues of the compliance and the broken valve, I was informed the valve was being replaced and they would apply for a plugging permit. |
1976188144 | 2015-07-01 | Plug / Plug Back | No Violations | On the day of my inspection following up on NOV-28165282 and complaint ID 5003, I witnessed that Matheny Well Service had ripped 4.5 inch casing at 3611 feet and tripped casing from wellbore. Matheny Well Service tripped 2.375 inch tubing to 3550 feet and Petroset Cementing Services was on site gained circulation and pumped a 50 sack 200 foot Class A 2% Gel Big Lime plug from 3550 feet to 3350 feet. Matheny Well Service pulled 72 joints of 2.375 inch tubing and Petroset Cementing Services pumped a 50 sack 207 foot Class A 2% Gel Berea plug from 1332 feet to 1125 feet. Matheny Well Service pulled 17 joints of 2.375 inch tubing and Petroset Cementing Services pumped a 50 sack 200 foot Class A 2% Gel Bottom of the surface plug from 758 feet to 558 feet. Matheny Well Service pulled 18 joints of 2.375 inch tubing and Petroset Cementing Services pumped an 80 sack 200 foot Class A 2% Gel surface plug from 200 feet to surface. Instructed operator to cut casing off 30 inches below grade and install metal plate identifying well and reclaim according to ORC 1509.072B. NOV-28165282 and complaint ID 5003 are resolved. |
2059741839 | 2007-07-24 | Production Wells | No Violations | STATUS CHECK |
221066072 | 2006-12-28 0:00 | PW | No Violations | |
232969011 | 2005-9-27 0:00: | PW | No Violations | |
28165282 | 2011-10-14 0:00 | PW | No Violations | |
292078053 | 2011-10-14 0:00 | PW | No Violations | |
454194602 | 2015-3-24 0:00: | PW | No Violations | 1.00 |
737838190 | 2014-3-17 0:00: | PW | No Violations | |
824769404 | 2015-7-2 0:00:0 | PB | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0028165282 | US-OH-122925 | 2011-10-15 | Well insufficiently equipped to prevent escape of oil and gas | |
0028165282 | US-OH-122926 | 2011-10-15 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
0028165282 | US-OH-122927 | 2011-10-15 | Defective casing, leaking well |
For data sources see[8]