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Well ID: 34-059-22662 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Wills Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: HOLDERBAUM (NELSON BROTHERS) | |
License Status: Final Restoration | |
License Date: 2013-06-05 | |
Spud Date: 1996-10-31 | |
Spud Drilling Contractor: DOWNHOLE DRILLING | |
Final Drill Date: 1980-02-23 | |
Well Total Depth: 4208.00 ft | |
Configuration: Vertical | |
Latitude: 40.000000 | |
Longitude: -81.360000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-12-31 | 157 LANDPROVEST INC GeoDate 12/31/79 |
Original Spud | 1980-02-20 | |
Completed | 1980-02-23 | |
Reached Total Depth | 1980-02-23 | |
CO | 1992-02-24 | 53 ATWOOD RESOURCES INC GeoDate 12/31/79 |
CO | 1993-02-24 | 4327 SOUND ENERGY CO INC GeoDate 12/31/79 |
CO | 1994-05-23 | 1419 LEVENGOOD OIL & GAS(US)IN GeoDate 12/31/79 |
CO | 1996-08-27 | 1419 LEVENGOOD OIL & GAS(US)IN GeoDate 8/27/96 |
Oil and Gas | 1996-08-27 | Issued Date 8/27/96 Expired Date 8/27/97 Acres 0040000 Tool Type RTA Proposed Formation ROSE RUN Proposed Depth 00000 Proposed Drill Depth 00000 |
Change of Owner | 1997-06-13 | Operator changed from 1419, LEVENGOOD OIL & GAS(US)IN to 43, RESOURCE AMERICA INC |
Change of Owner | 1997-06-23 | Operator changed from 1419, LEVENGOOD OIL & GAS(US)IN to 43, RESOURCE AMERICA INC |
Change of Owner | 2002-06-26 | Operator changed from 43, RESOURCE AMERICA INC to 1634, NORTHWOOD ENERGY CORP |
APP | 2013-06-05 | Proposed Formations:ORISKANY, Issued Date:6/5/2013, Expired Date:6/5/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-05-13 | |
Construction Permit Expires | 2015-06-05 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TIPKA BARTLO OIL & GAS CO | 0.00 | 0.00 | 365 |
1985 | TIPKA BARTLO OIL & GAS CO | 0.00 | 0.00 | 0 |
1987 | PENINSULA GROUP INC | 796.00 | 0.00 | 365 |
1988 | PENINSULA GROUP INC | 978.00 | 0.00 | 365 |
1989 | LANDPROVEST INC | 144.00 | 0.00 | 214 |
1991 | LANDPROVEST INC | 0.00 | 0.00 | 365 |
1996 | LEVENGOOD OIL & GAS(US)IN | 104.00 | 0.00 | 365 |
1997 | LEVENGOOD OIL & GAS(US)IN | 0.00 | 0.00 | 0 |
1998 | RESOURCE AMERICA INC | 39.00 | 0.00 | 365 |
1999 | RESOURCE AMERICA INC | 17.00 | 0.00 | 365 |
2000 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
2001 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
2002 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 365 |
2003 | NORTHWOOD ENERGY CORP | 58.00 | 0.00 | 365 |
2004 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2005 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2006 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2007 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2010 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2011 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2013 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2014 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TIPKA BARTLO OIL & GAS CO | Brine | 0 | 365 |
1985 | TIPKA BARTLO OIL & GAS CO | Brine | 0 | 0 |
1987 | PENINSULA GROUP INC | Brine | 0 | 365 |
1988 | PENINSULA GROUP INC | Brine | 0 | 365 |
1989 | LANDPROVEST INC | Brine | 75 | 214 |
1991 | LANDPROVEST INC | Brine | 35 | 365 |
1996 | LEVENGOOD OIL & GAS(US)IN | Brine | 0 | 365 |
1997 | LEVENGOOD OIL & GAS(US)IN | Brine | 0 | |
1998 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1999 | RESOURCE AMERICA INC | Brine | 70 | 365 |
2000 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2001 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2002 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2003 | NORTHWOOD ENERGY CORP | Brine | 0 | 365 |
2004 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2005 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2006 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2007 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2010 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2011 | NORTHWOOD ENERGY CORP | Brine | 0 | |
2012 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2013 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2014 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1491534590 | 2013-11-21 0:00 | PW | No Violations | |
-1609610209 | 2004-1-27 0:00: | PW | No Violations | |
0604132133 | 2014-05-12 | Plug / Plug Back | No Violations | On the day of my inspection, I witnessed Cemenco Services bull head thirty sacks of Class A cement into the Oriskany formation to set a four hundred foot plug. |
0631297911 | 2005-10-12 | Preliminary Restoration | No Violations | PRELIMENARY RESTORATION |
1302630809 | 2005-05-09 | Production Wells | No Violations | STATUS CHECK |
1367250850 | 2013-04-29 | Production Wells | Violations Noted | Pryor to my field inspection I received a phone call on this date of 04/26/2013 from Debbie Nelson which had a concern of the well being idle and oil laying around the compressor and tank. On the day of my inspection I reviewed the Division of Oil and Gas production records and found them not current for the years of (2002/03/04/05/06/07/2010/2011), there is four inch production casing with a (4x2) swedge and ball valve standing from the ground, the valve on the well is closed. There is a electric power box and line leading into a compressor/ separator and (1) fifty barrel plastic brine tank setting inside a containment dike, the compressor was running on the day of my inspection. I witnessed soil containment ion around the compressor/ separator and tank, I made a phone call to Ron Moore the pumper for Northwood Energy about the well being idle and the soil containment ion, Ron Moore told me that a small steel brine tank was removed and replaced with a plastic fifty barrel brine tank, the pumper also mentioned the well was idle due to a hole in the casing and he also put Pete moss on the areas of contamination to help absorb the oil. I instructed Ron Moore to have the soil removed and replace with limestone, there is no I.D. posted at the well site. The requirements to meet the Division of Oil and Gas Standards will be to have the well capable of commercial production within thirty days or plugging is required within ninety days, failure to comply may result in Forfeiture of Bond. |
1408553044 | 2014-08-20 | Final Restoration | No Violations | On the day of my inspection I witnessed that the site passed final restoration according to ORC 1509.072B. |
1491534590 | 2013-11-21 | Production Wells | No Violations | On the day of my Compliance Agreement Follow-up, I spoke with Bill Arnholt with Northwood Energy on the status and production of the well, Mr. Arnholt informed me that the land owner wants to take ownership of the well and the paper work was at there legal department. |
1609610209 | 2004-01-27 | Production Wells | No Violations | PHONE CALL TO RALPH TALLMEDGE,NORTHWOOD ENERGY,614-457-1024,WELL APPEARS TO BE IDLE.NOT SURE IF WELL IS BEING USED FOR DOMESTIC GAS.MR. TALLMEDGE SAID HE WOULD CHECK TO ASCERTAIN WETHER WELL IS BEING USED FOR DOMESTIC GAS,IF NOT HE WOULD LOOK INTO STATUS |
604132133 | 2014-5-12 0:00: | PB | No Violations | |
631297911 | 2005-10-12 0:00 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1367250850 | US-OH-110822 | 2014-05-27 | General Safety | |
1367250850 | US-OH-110823 | 2014-05-27 | Failure to legibly identify well | |
1367250850 | US-OH-110824 | 2014-05-27 | Well shall be plugged | |
1367250850 | US-OH-110825 | 2014-05-27 | Defective casing, leaking well | |
1367250850 | US-OH-110826 | 2014-05-27 | Statement of annual production not filed |
For data sources see[8]