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Well ID: 34-059-22698 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Richland Township | |
Operator Name: SABRE ENERGY CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: WILSON ETAL | |
License Status: Final Restoration | |
License Date: 2015-05-18 | |
Spud Date: 1980-03-11 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-03-16 | |
Well Total Depth: 5705.00 ft | |
Configuration: Vertical | |
Latitude: 39.930000 | |
Longitude: -81.470000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-12-31 | 182 BELDEN & BLAKE CO GeoDate 12/31/79 |
Original Spud | 1980-03-11 | |
Completed | 1980-03-16 | |
Reached Total Depth | 1980-03-16 | |
CO | 1994-10-25 | 4381 PELICAN PRODUCING INC GeoDate 12/31/79 |
CO | 1996-12-10 | 5244 SABRE ENERGY CORPORATION GeoDate 12/31/79 |
APP | 2015-05-18 | Proposed Formations:CLINTON, Issued Date:5/18/2015, Expired Date:5/17/2017 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-09-02 | |
Record Last Modified | 2017-02-10 | |
Construction Permit Expires | 2017-05-17 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5544 | 5608 | 16 |
5544 | 5608 | 16 | |
5544 | 5608 | 16 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1740 Bbl | 65000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ENTERPRISE ENERGY CORP | 6552.00 | 40.00 | 0 |
1985 | ENTERPRISE ENERGY CORP | 6285.00 | 51.00 | 176 |
1986 | BELDEN & BLAKE CORPORATION | 4900.00 | 39.00 | 365 |
1987 | BELDEN & BLAKE CORPORATION | 2204.00 | 0.00 | 365 |
1988 | BELDEN & BLAKE CORPORATION | 2070.00 | 0.00 | 295 |
1990 | BELDEN & BLAKE CORPORATION | 4256.00 | 92.00 | 349 |
1991 | BELDEN & BLAKE CORPORATION | 2886.00 | 0.00 | 365 |
1992 | BELDEN & BLAKE CORPORATION | 3193.00 | 0.00 | 285 |
1993 | BELDEN & BLAKE CORPORATION | 3495.00 | 0.00 | 355 |
1994 | PELICAN PRODUCING INC | 3197.00 | 87.00 | 365 |
1995 | PELICAN PRODUCING INC | 3296.00 | 0.00 | 365 |
1996 | SABRE ENERGY CORPORATION | 2947.00 | 112.00 | 365 |
1997 | SABRE ENERGY CORPORATION | 2715.00 | 0.00 | 365 |
1998 | SABRE ENERGY CORPORATION | 2961.00 | 0.00 | 365 |
1999 | SABRE ENERGY CORPORATION | 1954.00 | 0.00 | 0 |
2000 | SABRE ENERGY CORPORATION | 2917.00 | 32.00 | 0 |
2001 | SABRE ENERGY CORPORATION | 1062.00 | 0.00 | 365 |
2002 | SABRE ENERGY CORPORATION | 1937.00 | 0.00 | 365 |
2003 | SABRE ENERGY CORPORATION | 1894.00 | 0.00 | 365 |
2004 | SABRE ENERGY CORPORATION | 1544.00 | 0.00 | 365 |
2005 | SABRE ENERGY CORPORATION | 1026.00 | 0.00 | 365 |
2006 | SABRE ENERGY CORPORATION | 867.00 | 0.00 | 364 |
2007 | SABRE ENERGY CORPORATION | 805.00 | 0.00 | 365 |
2008 | SABRE ENERGY CORPORATION | 946.00 | 0.00 | 365 |
2009 | SABRE ENERGY CORPORATION | 186.00 | 0.00 | 365 |
2010 | SABRE ENERGY CORPORATION | 151.00 | 0.00 | 365 |
2011 | SABRE ENERGY CORPORATION | 34.00 | 0.00 | 365 |
2012 | SABRE ENERGY CORPORATION | 0.00 | 0.00 | 0 |
2013 | SABRE ENERGY CORPORATION | 0.00 | 0.00 | 0 |
2014 | SABRE ENERGY CORPORATION | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1157017430 | 2007-8-7 0:00:0 | PW | No Violations | |
-1653568652 | 2015-9-30 0:00: | FR | No Violations | 1.50 |
-2017133182 | 2008-6-18 0:00: | PW | No Violations | |
-614470758 | 2015-9-1 0:00:0 | PB | No Violations | 2.00 |
0425987704 | 2015-08-28 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service had tripped 1.5 inch tubing to 5543 feet. Formation Cementing Services was on site and cleared tubing and was unsuccessful in breaking circulation. Formation pumped a 30 sack 400 foot Class A Clinton plug from 5543 feet to 5143 feet. Cement was displaced with 12.9bbls of fresh water. BWS tripped 1.5 inch tubing out and will rip 4.5 inch casing on Monday. |
0614470758 | 2015-09-01 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service had ripped 4.5 inch casing at 4186 and removed from wellbore. BWS began tripping 1.5 inch tubing in to a depth of 4082 feet in preparation of setting the Big Lime plug tomorrow. |
0944253701 | 2005-08-30 | Production Wells | No Violations | STATUS CHECK. |
1157017430 | 2007-08-07 | Production Wells | No Violations | STATUS CHECK |
1426014160 | 2004-12-16 | Production Wells | No Violations | STATUS CHECK |
1441193156 | 2015-09-02 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Berry Well Service had tripped 1.5 inch tubing to 4082 feet. Formation Cementing was on site and gained circulation with 51bbls, circulated the wellbore with a total of 200bbls and set a 51 sack Class A with 2% Gel Big Lime plug from 4082 feet to 3882 feet. Cement was displaced with 9.7bbls of fresh water. BWS tripped 1.5 inch tubing to 1586 feet and Formation set a 53 sack Class A with 2% Gel Bottom of the surface plug from1586 feet to 1386 feet. Cement was displaced with 3.5bbls of fresh water. BWS tripped 1.5 inch tubing to 200 feet and Formation set a 68 sack Class A with 2% Gel Surface plug from 200 feet to surface. BWS tripped remaining 1.5 inch tubing and cement stayed at the surface. |
1644328253 | 2015-08-27 | Production Wells | No Violations | On the day of my inspection accompanied by ODNR Inspector Brian Sefcik, I witnessed that Berry Well Service was on site rigging in preparation to plug well beginning tomorrow. I met with Consultant Tim Wilson and discussed plugging schedule. |
1653568652 | 2015-09-30 | Final Restoration | No Violations | On the day of my inspection I witnessed that the site passed final restoration according to ORC 1509.072B. |
2017133182 | 2008-06-18 | Production Wells | No Violations | PRODUCING WELL. |
425987704 | 2015-8-28 0:00: | PB | No Violations | 3.00 |
944253701 | 2005-8-30 0:00: | PW | No Violations |
For data sources see[9]