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34-059-23074

Well Details

Well ID: 34-059-23074
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Country: United States
State: Ohio
County: Belmont
Municipality: Flushing Township
Operator Name: EXCO - NORTH COAST ENERGY INC
Well Pad ID:
Farm/Lease Name: DUVALL K
License Status: Final Restoration
License Date: 2008-09-22
Spud Date: 1982-02-05
Spud Drilling Contractor:
Final Drill Date: 1982-02-10
Well Total Depth: 6272.00 ft
Configuration: Vertical
Latitude: 40.140000
Longitude: -81.220000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-08-17 2143 CARLESS RESOURCES INC GeoDate 8/17/81
Original Spud 1982-02-05 RL 11-26-81
Completed 1982-02-10 RL 11-26-81
Reached Total Depth 1982-02-10 RL 11-26-81
CO 1988-02-08 2143 CARLESS RESOURCES INC GeoDate 2/8/88
Unknown 1988-02-08 Issued Date 2/8/88 Expired Date 2/7/89 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Change of Owner 1998-06-15 Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC
APP 2008-09-22 Proposed Formations:CLINTON, Issued Date:9/22/2008, Expired Date:9/22/2009 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2009-03-06 RL 11-26-81
Construction Permit Expires 2009-09-22 RL 11-26-81
Record Last Modified 2013-03-14 RL 11-26-81

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 6087 6120 2
6087 6120 2
6087 6120 2

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC 6619.00 43.00 363
1987 ZILKHA ENERGY INC 5010.00 36.00 165
1988 CARLESS RESOURCES INC 11.00 0.00 30
1989 CARLESS RESOURCES INC 4083.00 0.00 355
1990 CARLESS RESOURCES INC 6065.00 0.00 365
1991 CARLESS RESOURCES INC 4468.00 0.00 365
1992 CARLESS RESOURCES INC 4007.00 0.00 365
1993 CARLESS RESOURCES INC 3590.00 0.00 365
1994 CARLESS RESOURCES INC 4364.00 94.00 365
1995 CARLESS RESOURCES INC 5846.00 0.00 365
1996 CARLESS RESOURCES INC 2236.00 0.00 365
1997 CARLESS RESOURCES INC 3410.00 0.00 365
1998 EXCO - NORTH COAST ENERGY INC 3243.00 0.00 365
1999 EXCO - NORTH COAST ENERGY INC 2952.00 0.00 365
2000 EXCO - NORTH COAST ENERGY INC 3339.00 0.00 365
2001 EXCO - NORTH COAST ENERGY INC 3530.00 44.00 365
2002 EXCO - NORTH COAST ENERGY INC 3109.00 0.00 365
2003 EXCO - NORTH COAST ENERGY INC 3110.00 0.00 365
2004 EXCO - NORTH COAST ENERGY INC 201.00 0.00 365
2005 EXCO - NORTH COAST ENERGY INC 111.00 0.00 365
2006 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
2007 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2008 EXCO - NORTH COAST ENERGY INC 0.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC Brine 136928 363
1987 ZILKHA ENERGY INC Brine 104 165
1988 CARLESS RESOURCES INC Brine 0 30
1989 CARLESS RESOURCES INC Brine 0 355
1990 CARLESS RESOURCES INC Brine 36 365
1991 CARLESS RESOURCES INC Brine 0 365
1992 CARLESS RESOURCES INC Brine 0 365
1993 CARLESS RESOURCES INC Brine 0 365
1994 CARLESS RESOURCES INC Brine 112 365
1995 CARLESS RESOURCES INC Brine 390 365
1996 CARLESS RESOURCES INC Brine 457 365
1997 CARLESS RESOURCES INC Brine 253 365
1998 EXCO - NORTH COAST ENERGY INC Brine 150 365
1999 EXCO - NORTH COAST ENERGY INC Brine 143 365
2000 EXCO - NORTH COAST ENERGY INC Brine 63 365
2001 EXCO - NORTH COAST ENERGY INC Brine 113 365
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365
2003 EXCO - NORTH COAST ENERGY INC Brine 71 365
2004 EXCO - NORTH COAST ENERGY INC Brine 0 365
2005 EXCO - NORTH COAST ENERGY INC Brine 0 365
2006 EXCO - NORTH COAST ENERGY INC Brine 0 365
2007 EXCO - NORTH COAST ENERGY INC Brine 0 0
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1477027204 2004-1-14 0:00: PW No Violations
-1808717571 2009-3-3 0:00:0 PB No Violations
-646714528 2006-4-21 0:00: PW No Violations
-773547387 2008-9-29 0:00: PW No Violations
-973528607 2003-10-22 0:00 PW No Violations
0646714528 2006-04-21 Production Wells No Violations STATUS CHECK. PRODUCING WELL.
0773547387 2008-09-29 Production Wells No Violations PERMIT TO PLUG. WITH CHIP SMITH TO FIND LOCATION
0829908056 2009-10-09 Final Restoration No Violations Final restoration work at site is satisfactory pit has been filled in and site restored and vegatation has been established.
0973528607 2003-10-22 Production Wells No Violations STATUS CHECK.
1236362701 2009-03-05 Plug / Plug Back No Violations TEMPLE OIL-GAS RIG. KNOCK OFF 1655 4.5PIPE COLLAPSED. PULL OUT LAID DOWN ON TRAILOR. RUN 1.5 BACK IN TO 2610.
1388890155 2005-05-25 Production Wells No Violations STATUS CHECK
1431920983 2006-01-12 Production Wells No Violations STATUS CHECK
1477027204 2004-01-14 Production Wells No Violations STATUS CHECK, DIKE NEEDS WORKED OVER IN HEIGTH.
1808717571 2009-03-03 Plug / Plug Back No Violations BLOW WELL DOWN. STRONG H2S GAS. LOAD HOLE WITH 45 BBL. OF BRINE TO KILL WELL. START TO PULL TUBING, FOUND PACKER AT BOTTOM OF HOLE GOT PACKER FREE AND PULLED 25 JTS. AND LAID DOWN ON TRAILOR.
829908056 2009-10-9 0:00: FR No Violations

For data sources see[8]

References