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Well ID: 34-059-23126 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Londonderry Township | |
Operator Name: BETTS WESLEY | |
Well Pad ID: | |
Farm/Lease Name: BETTS D-TURBYFILL UNIT | |
License Status: Domestic Well | |
License Date: 2003-09-09 | |
Spud Date: 1981-11-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-11-18 | |
Well Total Depth: 6311.00 ft | |
Configuration: Vertical | |
Latitude: 40.110000 | |
Longitude: -81.260000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-10-07 | 2143 CARLESS RESOURCES INC GeoDate 10/7/81 |
Original Spud | 1981-11-13 | PRODUCING DOMESTIC GAS PER 8/18/2015 INSPECTION BY DOUG BENNETT |
Completed | 1981-11-18 | PRODUCING DOMESTIC GAS PER 8/18/2015 INSPECTION BY DOUG BENNETT |
Reached Total Depth | 1981-11-18 | PRODUCING DOMESTIC GAS PER 8/18/2015 INSPECTION BY DOUG BENNETT |
CO | 1994-04-06 | 2143 CARLESS RESOURCES INC GeoDate 4/6/94 |
Unknown | 1994-04-06 | Issued Date 4/6/94 Expired Date 4/6/95 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Change of Owner | 1998-06-15 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2003-05-09 | Operator changed from 1388, NORTH COAST ENERGY INC to 1, HOPEWELL OIL & GAS |
APP | 2003-09-09 | Proposed Formations:CLINTON, Issued Date:9/9/2003, Expired Date:9/8/2004 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Construction Permit Expires | 2004-09-08 | PRODUCING DOMESTIC GAS PER 8/18/2015 INSPECTION BY DOUG BENNETT |
Record Last Modified | 2016-03-03 | PRODUCING DOMESTIC GAS PER 8/18/2015 INSPECTION BY DOUG BENNETT |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 6137 | 6173 | 2 |
6137 | 6173 | 2 | |
6137 | 6173 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 70000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1425874466 | 2019-8-28 0:00: | PW | No Violations | 0.60 |
-149151016 | 2020-2-28 0:00: | PW | No Violations | 1.00 |
-1498669468 | 2017-12-12 0:00 | PW | No Violations | 0.60 |
-1638190521 | 2017-12-6 0:00: | PW | No Violations | 2.00 |
-1782012609 | 2007-4-27 0:00: | PW | No Violations | |
-1891304549 | 2018-2-21 0:00: | PW | No Violations | 0.60 |
-1968047872 | 2019-11-20 0:00 | PW | No Violations | 0.30 |
-2073600059 | 2019-8-13 0:00: | PW | No Violations | 0.20 |
-2098099927 | 2019-11-20 0:00 | PW | No Violations | 1.50 |
-213570980 | 2018-2-1 0:00:0 | PW | No Violations | 0.50 |
-2141426597 | 2020-5-11 0:00: | PW | No Violations | 1.00 |
-618288191 | 2017-12-8 0:00: | PW | No Violations | 0.80 |
-949268310 | 2018-2-5 0:00:0 | PW | No Violations | 0.50 |
0101622027 | 2018-01-10 | Production Wells | No Violations | On the day of my inspection accompanied by ODNR Southeast Regional Manager Brent Bear and following up on Compliance Notice- 638190521, readings were taken with ODNR Honeywell PhD6 meter revealing a LEL of 11 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. Patterson UTI Drilling Rig #584 is rigging up on the adjacent Betts Pad with plans to drill to new wells. |
0213570980 | 2018-02-01 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice- 638190521, I witnessed there was no change in the status of the well since the last inspection on 1/19/18. Readings were taken with ODNR Honeywell PhD6 meter revealing a LEL of 20 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. |
0384184515 | 2018-04-09 | Production Wells | No Violations | The purpose of my inspection was a status check on a compliance notice numbered -638190521. During my inspection I witnessed that the well continued to leak gas. While utilizing the Tango Hydrogen Sulfide gas detector I recorded a .5 parts per million. |
0575666061 | 2004-04-21 | Final Restoration | No Violations | FINAL RESTORATION |
0618288191 | 2017-12-08 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice- 638190521, I witnessed no action has been taken to address the leak. Readings were taken with ODNR Honeywell PhD6 meter revealing a LEL of >10 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. There has been no communication from the owner of record concerning this leak. |
0755699399 | 2018-10-04 | Production Wells | No Violations | The purpose of my inspection today was a follow up on compliance notice -638190521. During my inspection the well was equipped with 8.625-inch diameter casing with a casing head, 4.5-inch diameter casing with a tubing head, 1.5-inch diameter tubing, and a plunger lift system. A domestic gas service with two regulators and an open valve were attached to the 4.5-inch diameter casing. While utilizing the Industrial Scientific Ventis Pro 4 gas detector zeros were recorded. |
0890870849 | 2018-01-19 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice- 638190521, readings were taken with ODNR Honeywell PhD6 meter revealing a LEL of 20 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. |
0949268310 | 2018-02-05 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice- 638190521, I witnessed there was no change in the status of the well since the last inspection on 2/1/18. Readings were taken with ODNR Honeywell PhD6 meter revealing a LEL of 8 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. |
101622027 | 2018-1-10 0:00: | PW | No Violations | 1.80 |
1065643619 | 2017-06-06 | Production Wells | No Violations | On the day of my inspection I witnessed the well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, a plunger lift system and domestic gas service with valves in the closed position on the tubing and 1 of 2 open on the casing supplying the domestic gas service. Production equipment included a 210 barrel tank and a horizontal separator all within an earthen dike. Hopewell Oil and Gas remains the owner of record with no gauges present on the wellhead. ODNR Tango Hydrogen Sulfide (H2S) detector revealed no H2S present. |
1082334836 | 2020-8-7 0:00:0 | EX | No Violations | 1.00 |
1456250909 | 2016-02-23 | Production Wells | No Violations | On the day of my inspection I witnessed the well was not plugged and was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing, a plunger lift system and domestic gas service with valves in the closed position on the tubing and 1 of 2 open on the casing supplying the domestic gas service. Production equipment included a 210bbl tank and a horizontal separator all within an earthen dike. Hopewell Oil and Gas remains the owner of record. |
1498669468 | 2017-12-12 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice- 638190521, I witnessed no action has been taken to address the leak with 12/11/17 as date of remedy requested. Readings were taken in very windy conditions with ODNR Honeywell PhD6 meter revealing a LEL of 8 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. There has been no communication from the owner of record concerning this leak. |
1531226594 | 2018-07-10 | Production Wells | No Violations | The purpose of my inspection today was a follow up on compliance notice -638190521. The well was overgrown by vegetation. During my inspection the well was equipped with 8.625 inch diameter casing with a casing head, 4.5 inch diameter casing with a tubing head, 1.5 inch diameter tubing, and a plunger lift system. A domestic gas service with two regulators and an open valve was attached to the 4.5 inch diameter casing. Gas could be heard escaping from near the packing on the 8.625 inch diameter casing head. While utilizing the Industrial Scientific Ventis Pro 4 gas detector, Hydrogen Sulfide and LEL recorded as zeros. |
1550073045 | 2019-02-13 | Production Wells | No Violations | During my inspection following up on compliance notice -638190521 the well was equipped with 8.625-inch diameter casing with a casing head, 4.5-inch diameter casing with a tubing head, 1.5-inch diameter tubing, and a plunger lift system. A domestic gas service with two regulators and an open valve were attached to the 4.5-inch diameter casing. A gas odor was present but with wind gust up to 20 miles per hour today the Industrial Scientific Ventis Pro 4 gas detector recorded zeros. |
1594400888 | 2020-7-10 0:00: | PW | No Violations | 1.00 |
1638190521 | 2017-12-06 | Production Wells | Violations Noted | On the day of my inspection following up from inspection on 12/5/17, I witnessed the well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, a plunger lift system and domestic gas service with valves in the closed position on the tubing and 1 of 2 open on the casing supplying the domestic gas service. The water which was present near the slips on the 8.625 inch diameter wellhead and the 4.5 inch diameter casing had evaporated and a strong smell of gas was present. Readings were taken with ODNR Honeywell PhD6 meter revealing a LEL of 10 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. The distance from the gas combustor on the 34059244820000 Betts 2H to the wellhead is 130 feet. Production equipment included a 210 barrel tank and a horizontal separator all within an earthen dike. Owner/Operator shall make necessary repairs to well to prevent the escape of gas. |
1666304824 | 2018-01-03 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice- 638190521, readings were taken in .5 degrees with ODNR Honeywell PhD6 meter revealing a LEL of 7 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. I received a call from Howard Harrop on 12/18/17, who believes the leak is coming from the stem on a ball valve and also was able to check the pressure on the well at 260 pounds per square inch. He stated that he would relay information to the receiver and to make repairs a rig would have to come in. |
1743954744 | 2015-08-18 | Production Wells | No Violations | On the day of my inspection I witnessed the well was not plugged and was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing, a plunger lift system and domestic gas service with valves in the closed position on the tubing and 1 of 2 open on the casing supplying the domestic gas service. Production equipment included a 210bbl tank and a horizontal separator all within an earthen dike. I spoke with landowner Wes Betts and he stated that he had purchased the well from Hopewell Oil and Gas. |
1782012609 | 2007-04-27 | Production Wells | No Violations | IDLEWELL. JERRY HENDERSON TO PLUG |
1782984230 | 2017-01-10 | Production Wells | No Violations | On the day of my inspection I witnessed the well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, a plunger lift system and domestic gas service with valves in the closed position on the tubing and 1 of 2 open on the casing supplying the domestic gas service. Production equipment included a 210 barrel tank and a horizontal separator all within an earthen dike. Hopewell Oil and Gas remains the owner of record. |
1837324223 | 2019-04-09 | Production Wells | No Violations | The purpose of my inspection was a follow up on compliance notice -638190521. The well was equipped with 8.625-inch diameter casing with a casing head, 4.5-inch diameter casing with a tubing head, 1.5-inch diameter tubing, and a plunger lift system. A domestic gas service with two regulators and an open valve were attached to the 4.5-inch diameter casing. A gas odor was present, but the Industrial Scientific Ventis Pro 4 gas detector recorded zeros. I was accompanied by ODNR inspector Rick Brown. |
1878545373 | 2019-8-13 0:00: | PW | No Violations | 0.30 |
1891304549 | 2018-02-21 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice- 638190521, I witnessed there was no change in the status of the well since the last inspection on 2/5/18. Readings were taken with ODNR Honeywell PhD6 meter revealing a LEL of 10 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. |
1892637700 | 2017-12-05 | Production Wells | No Violations | On the day of my inspection following up on a request from Ascent Resources Production Superintendent Adam Pence for a gas leak, I witnessed the well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, a plunger lift system and domestic gas service with valves in the closed position on the tubing and 1 of 2 open on the casing supplying the domestic gas service. There was visible bubbling coming from the packing on the 8.625 inch diameter wellhead and the 4.5 inch diameter casing near the slips. Readings were taken with ODNR Honeywell PhD6 meter revealing a LEL of 4 and no Hydrogen Sulfide (H2S) detected. Also utilizing ODNR Tango H2S detector revealed no H2S was detected. The distance from the gas combustor on the 34059244820000 Betts 2H to the wellhead is 130 feet. Identification was present but faded and production records were current Production equipment included a 210 barrel tank and a horizontal separator all within an earthen dike. I stopped at the residence and nobody was home. Hopewell Oil and Gas remains the owner of record. |
367831928 | 2020-2-28 0:00: | PW | No Violations | 0.20 |
384184515 | 2018-4-9 0:00:0 | PW | No Violations | 0.20 |
575666061 | 2004-4-21 0:00: | FR | No Violations | |
722913868 | 2020-1-30 0:00: | PW | No Violations | 0.50 |
755699399 | 2018-10-4 0:00: | PW | No Violations | 0.50 |
890870849 | 2018-1-19 0:00: | PW | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1638190521 | US-OH-116109 | 2017-12-29 | General Safety | |
1638190521 | US-OH-116110 | 2017-12-29 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[9]