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34-059-23330

Well Details

Well ID: 34-059-23330
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Country: United States
State: Ohio
County: Guernsey
Municipality: Liberty Township
Operator Name: GAS ACQUISITION COMPANY LTD
Well Pad ID:
Farm/Lease Name: VANDERHILL A
License Status: Final Restoration
License Date: 2002-03-25
Spud Date: 1982-05-19
Spud Drilling Contractor: PROD. WELL SERVICE
Final Drill Date: 1982-05-27
Well Total Depth: 5187.00 ft
Configuration: Vertical
Latitude: 40.140000
Longitude: -81.530000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-05-18 Issued Date 5/18/82 Expired Date 11/15/82 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05187 Proposed Drill Depth 05187
Original Spud 1982-05-19
Completed 1982-05-27
Reached Total Depth 1982-05-27
CO 1983-06-01 213 LOMAK OPERATING CO GeoDate 5/18/82
Completion Report Received 1983-06-03
Change of Owner 2000-06-27 Operator changed from 213, RANGE OPERATING COMPANY to 6674, GREAT LAKES ENERGY PTNSHP LLC
Change of Owner 2002-03-18 Operator changed from 6674, GREAT LAKES ENERGY PTNSHP LLC to 6805, GAS ACQUISITION COMPANY LTD
APP 2002-03-25 Proposed Formations:CLINTON, Issued Date:3/25/2002, Expired Date:3/25/2003 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2003-03-25
Record Last Modified 2014-09-10

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4994 5085 16
4994 5085 16
4994 5085 16

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 72000 Gal 42500 FRAC: 72MG FLUID, 42.5 SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 APPALACHIAN EXPL INC 33050.00 97.00 0
1985 APPALACHIAN EXPL INC 36427.00 0.00 128
1986 APPALACHIAN EXPL INC 40843.00 92.00 145
1987 APPALACHIAN EXPL INC 20265.00 0.00 135
1988 APPALACHIAN EXPL INC 32269.00 0.00 184
1989 APPALACHIAN EXPL INC 29423.00 107.00 264
1990 RANGE OPERATING COMPANY 20524.00 0.00 303
1991 RANGE OPERATING COMPANY 14528.00 11.00 335
1992 RANGE OPERATING COMPANY 8115.00 0.00 366
1993 RANGE OPERATING COMPANY 6467.00 0.00 365
1994 RANGE OPERATING COMPANY 3725.00 0.00 365
1995 RANGE OPERATING COMPANY 2065.00 0.00 365
1996 RANGE OPERATING COMPANY 826.00 0.00 365
1997 RANGE OPERATING COMPANY 608.00 45.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 APPALACHIAN EXPL INC Brine 0 0
1985 APPALACHIAN EXPL INC Brine 0 128
1986 APPALACHIAN EXPL INC Brine 14 145
1987 APPALACHIAN EXPL INC Brine 14 135
1988 APPALACHIAN EXPL INC Brine 0 184
1989 APPALACHIAN EXPL INC Brine 92 264
1990 RANGE OPERATING COMPANY Brine 0 303
1991 RANGE OPERATING COMPANY Brine 70 335
1992 RANGE OPERATING COMPANY Brine 130 366
1993 RANGE OPERATING COMPANY Brine 0 365
1994 RANGE OPERATING COMPANY Brine 0 365
1995 RANGE OPERATING COMPANY Brine 0 365
1996 RANGE OPERATING COMPANY Brine 0 365
1997 RANGE OPERATING COMPANY Brine 36 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1060634153 2002-01-18 Production Wells Violations Noted FOLLOW UP TO NOV # 1289i25 COMPLAINT BY ANNONYMOUS CALL; INSPECTED WELL REVEALED WELL IS INCAPABLE OF PRODUCING. WELLHEAD HAS BASICALLY BEEN STRIPPED. PRODUCTION REPORTS CHECKED HAVE SHOWN WELL HAS NOT BEEN PRODUCED SINCE 1995. VIOLATION OF 1509.12, NOV#22627.
1289i25571 2002-01-18 Production Wells No Violations COMPLAINT BY ANNONYMOUS CALL; INSPECTED WELL REVEALED WELL IS INCAPABLE OF PRODUCING. WELLHEAD HAS BASICALLY BEEN STRIPPED. PRODUCTION REPORTS CHECKED HAVE SHOWN WELL HAS NOT BEEN PRODUCED SINCE 1995. VIOLATION OF 1509.12, NOV#22627.
1289i2557124 2002-1-18 0:00: PW No Violations
2063431366 2003-07-14 Final Restoration No Violations FINAL RESTORATION

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1060634153 US-OH-101181 2002-01-18 Well shall be plugged

For data sources see[9]

References