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Well ID: 34-059-24363 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Oxford Township | |
Operator Name: ECLIPSE RESOURCES I LP | |
Well Pad ID: US-OH-000912 | |
Farm/Lease Name: ANDY YODER D | |
License Status: Producing | |
License Date: 2014-04-21 | |
Spud Date: 2014-06-16 | |
Spud Drilling Contractor: PATTERSON DRILLING | |
Final Drill Date: 2014-07-04 | |
Well Total Depth: 14749.00 ft | |
Configuration: Horizontal | |
Latitude: 40.030000 | |
Longitude: -81.310000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2014-04-21 | Proposed Formations:POINT PLEASANT, Issued Date:4/21/2014, Expired Date:4/20/2016 12:00:00 PM, Drilling unit acres:415.879, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2014-07-04 | |
Completion Report Received | 2015-04-28 | |
Correction to Well | 2015-11-27 | CHANGE IN TARGET AND TAKE-POINT INFORMATION (FOOTAGES AND COORDINATES) FROM AS DRILLED SURVEY PLAT. |
Construction Permit Expires | 2016-04-20 | |
Record Last Modified | 2017-10-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2016-03-22 | 8260 | 14515 | 780 |
8260 | 14515 | 780 | |
8260 | 14515 | 780 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 10/08/2014 | 10/24/2014 | 7769 | 9,585,700.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | CI-14 | Baker Hughes | Corrosion Inhibitor | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0008413 | 754 |
Ferrotrol 300L | Baker Hughes | Iron Control | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0030477 | 2731.46 | |
Sand, White, 40/70 | Baker Hughes | Proppant | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 3.47467 | 3,114,100.0 | |
Water | Operator | Carrier | Water | 7732-18-5 | 100 | 89.1423 | 79,923,700.0 | |
Scaletrol 720 | Baker Hughes | Scale Inhibitor | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0092663 | 8304.7 | |
Scaletrol 720, 330 gl tote | Baker Hughes | Scale Inhibitor | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.003133 | 2807.92 | |
Sand, White, 100 mesh | Baker Hughes | Proppant | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 1.09671 | 982900 | |
HCl, 10.1 - 15% | Baker Hughes | Acidizing | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.532052 | 476840 | |
MaxPerm-20A, 265 gallon tote | Baker Hughes | Friction Reducer | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0414103 | 37113.1 | |
Ingredients in Additive(s) (MSDS and non-MSDS) | Baker Hughes | See Trade Name(s) List | Modified Thiourea Polymer | 68527-49-1 | 7 | 0.00005890 | 52.78 | |
Formaldehyde | 50-00-0 | 1 | 0.00000840 | 7.54 | ||||
Alcohols, C12-16, ethoxylated | 68551-12-2 | 2 | 0.001136 | 1018.54 | ||||
Citric Acid | 77-92-9 | 60 | 0.0018279 | 1638.88 | ||||
Methanol | 67-56-1 | 100 | 0.000841 | 754 | ||||
1-Propanesulfonic acid, 2-methyl-2-[(1-oxo-2-propen-1-yl)amino],
polymer with 2-propenamide, sodium |
83446-68-8 | 60 | 0.0248363 | 22267.8 | ||||
Sorbitan Monooleate | 1338-43-8 | 0.5 | 0.000284 | 254.636 | ||||
Hydrochloric Acid | 7647-01-0 | 15 | 0.0797844 | 71533.5 | ||||
Polyoxyalkylenes | 68951-67-7 | 30 | 0.0002523 | 226.2 | ||||
Potassium Chloride | 7447-40-7 | 1 | 0.0001239 | 111.126 | ||||
Polyoxythylene Sorbitan Monooleate | 9005-65-6 | 0.5 | 0.000284 | 254.636 | ||||
Poly (acrylamide-co-acrylic acid) partial sodium salt | 62649-23-4 | 30 | 0.0170404 | 15278.2 | ||||
Ammonium Persulphate | 7727-54-0 | 100 | 0.000764 | 685 | ||||
Propargyl Alcohol | 107-19-7 | 5 | 0.00004200 | 37.7 | ||||
Sorbitan, mono-(9Z)-9-octadecenoate | 1338-43-8 | 5 | 0.0020697 | 1855.65 | ||||
Fatty Acids | 61790-12-3 | 10 | 0.00008410 | 75.4 | ||||
Olefin | 64743-02-8 | 5 | 0.00004200 | 37.7 | ||||
Water | 7732-18-5 | 85 | 0.50735 | 454882 | ||||
Hydrotreated Light Distillate | 64742-47-8 | 30 | 0.0294586 | 26412.1 | ||||
Oleamide DEA | 93-83-4 | 2 | 0.001136 | 1018.54 | ||||
Crystalline Silica (Quartz) | 14808-60-7 | 100 | 10.1707 | 9,118,900.0 | ||||
Polyoxyethylene sorbitan monooleate | 9005-65-6 | 5 | 0.0020697 | 1855.65 | ||||
2-Propenoic, Polymer with Sodium Phosphinate, Sodium Salt | 71050-62-9 | 20 | 0.0024789 | 2222.52 | ||||
Ammonium Chloride | 12125-02-9 | 3 | 0.001704 | 1527.82 | ||||
Ethylene Glycol | 107-21-1 | 45 | 0.0055775 | 5000.68 | ||||
Sodium Chloride | 7647-14-5 | 5 | 0.0050337 | 4513.14 | ||||
Oxyalkylated alcohol | 78330-21-9 | 5 | 0.0020697 | 1855.65 | ||||
Calcium Chloride | 10043-52-4 | 5 | 0.0006197 | 555.631 | ||||
Sand, White, 30/50 | Baker Hughes | Proppant | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 5.60337 | 5,021,900.0 | |
GBW-5 | Baker Hughes | Breaker | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0007643 | 685 | |
FRW-18 | Baker Hughes | Friction Reducer | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.056824 | 50927.2 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2015 | ECLIPSE RESOURCES I LP | 758664 | 102667 | 278 |
2016 | ECLIPSE RESOURCES I LP | 636250 | 35181 | 360 |
2017 | ECLIPSE RESOURCES I LP | 392621 | 20385 | 364 |
2018 | ECLIPSE RESOURCES I LP | 324514 | 13680 | 362 |
2019 | ECLIPSE RESOURCES I LP | 69215 | 2668 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2015 | ECLIPSE RESOURCES I LP | Brine | 7047 | 278 |
2016 | ECLIPSE RESOURCES I LP | Brine | 4689 | 360 |
2017 | ECLIPSE RESOURCES I LP | Brine | 2818 | 364 |
2018 | ECLIPSE RESOURCES I LP | Brine | 3948 | 362 |
2019 | ECLIPSE RESOURCES I LP | Brine | 418 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1214280256 | 2020-6-11 0:00: | PW | No Violations | |
-1216550509 | 2017-9-12 0:00: | PW | No Violations | 1.50 |
-1687874084 | 2019-2-12 0:00: | PW | No Violations | 0.30 |
-353166966 | 2017-9-12 0:00: | PW | No Violations | 0.50 |
-911297408 | 2015-3-26 0:00: | CT | No Violations | 1.00 |
-941080693 | 2016-8-16 0:00: | PW | No Violations | 0.50 |
-974786596 | 2016-6-17 0:00: | PW | No Violations | 0.50 |
0217309055 | 2018-08-16 | Production Wells | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with a plunger lift system with valves in the open position. Pressure gauges were present on all casing strings. The production equipment consisted of six sand traps, six gas production units, and two 400-barrel tanks. The identification was present at the wellhead. |
0353166966 | 2017-09-12 | Production Wells | No Violations | On the day of my inspection, I accompanied ODNR Inspector Doug Bennett, and I witnessed that Parco Wireline Services was onsite retrieving a stuck plunger which was tagged at 7398 feet. A meeting with Eclipse production personnel was held discussing the well and the pad features. The well was equipped with a plunger lift system with valves in the closed position and annular pressure monitoring was in place. Gauges presently read 615 pounds per square inch on the tubing and 715 pounds per square inch on the casing with annular pressure monitoring in place. The production equipment included a sand trap and a GP unit. Also present a blow case skid and 2-400 barrel purge tanks shared with the 1H, 2H, 3H, 4H and the 5H. Nacelle fuel skid was also onsite providing fuel for the Fineran frac job. |
0911297408 | 2015-03-26 | Completion Testing | No Violations
-in for twenty four hours and then all six wells flowing to the Borton CGF. | |
0941080693 | 2016-08-16 | Production Wells | No Violations | On the day of my inspection of the Borton Central Gathering Facility (CFG) accompanied by ODNR Customer Service Assistant Jimmy Wiles, I witnessed the remediation of the affected area around the flare stack was completed and the facility was online. Repairs were completed yesterday at 22:00 with restart at that time. Inspection of the well pad found the well to be equipped with a plunger lift system with valves in the open position. Gauges present read 1060 pounds per square inch on the tubing and 1350 pounds per square inch on the casing with annular pressure monitoring in place. The production equipment included a line heater, a sand trap, a GP unit and 2-400 barrel purge tanks. Fluids and gas are separated at the GP unit and then transferred to the Borton CGF for sales. |
0974786596 | 2016-06-17 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with a Sweco wellheads and a production tree with valves in the open position. The production equipment included a line heater, a sand trap, a GP unit and 2-400bbl purge tanks. Tubing pressure was at 600psi and Casing pressure was at 810psi with annular pressure monitoring in place. Fluids and gas are separated at the GP unit and then transferred to the Borton CGF. |
0989041192 | 2015-09-21 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with Sweco wellheads and production trees. The production equipment included a sand trap; a GP unit and 2-400bbl purge tanks. Tubing pressure was at 1700psi and Casing pressure was at 1850psi. Fluids and gas are separated at the GP unit and then transferred to the Borton CGF. |
1216550509 | 2017-09-12 | Production Wells | No Violations | On the day of my inspection accompanied by ODNR Inspector Tom Thomas, I witnessed that Parco Wireline Services was onsite retrieving a stuck plunger which was tagged at 7398 feet. A meeting with Eclipse production personnel was held discussing the well and the pad features. The well was equipped with a plunger lift system with valves in the closed position and annular pressure monitoring was in place. Gauges present read 615 pounds per square inch on the tubing and 715 pounds per square inch on the casing with annular pressure monitoring in place. The production equipment included a sand trap and a GP unit. Also present a blow case skid and 2-400 barrel purge tanks shared with the 1H, 2H, 3H, 4H and the 5H. Nacelle fuel skid was also onsite providing fuel for the Fineran frac job. |
1304101665 | 2015-01-07 | Preliminary Restoration | No Violations | On the day of my inspection I witnessed that the site passed preliminary restoration according to ORC 1509.072A. |
1489081575 | 2017-03-09 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with a plunger lift system with valves in the open position and annular pressure monitoring in place. Gauges present read 435 pounds per square inches on the tubing and 695 pounds per square inches on the casing with annular pressure monitoring in place. The production equipment included a sand trap and a GP unit. Also present a blow case skid and 2-400 barrel purge tanks shared with the 1H, 2H, 3H, 4H and the 5H. |
1521461876 | 2016-07-26 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with a Sweco wellheads and a production tree with valves in the open position and annular pressure monitoring in place. Tubing pressure was at 615 pounds per square inches and casing pressure was at 785 pounds per square inches with annular pressure monitoring in place. The production equipment included a line heater, a sand trap, a GP unit and 2-400 barrel purge tanks. Eclipse personnel were onsite preparing to install a plunger lift system to the well and shutting it in for 24 hours as an additional compressor is being installed at the Borton Central Gathering Facility. |
1687874084 | 2019-02-12 | Production Wells | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with a plunger lift system with valves in the open position. The 13.375-inch diameter surface casing had 0 pounds per square inch, the 9.625-inch diameter intermediate had 0 pounds per square inch, the 5.5-inch diameter production casing had 400 pounds per square inch, and the production tubing had 380 pounds per square inch. The production equipment consisted of six sand traps, six gas production units, and two 400-barrel tanks. The identification was present at the wellhead. |
217309055 | 2018-8-16 0:00: | PW | No Violations | 0.20 |
989041192 | 2015-9-21 0:00: | PW | No Violations | 0.30 |
For data sources see[9]