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Well ID: 34-059-24520 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Millwood Township | |
Operator Name: ECLIPSE RESOURCES I LP | |
Well Pad ID: US-OH-001546 | |
Farm/Lease Name: JUPITER B UNIT | |
License Status: Producing | |
License Date: 2018-04-06 | |
Spud Date: 2018-01-30 | |
Spud Drilling Contractor: H&P DRILLING | |
Final Drill Date: 2018-05-16 | |
Well Total Depth: 27535.00 ft | |
Configuration: Horizontal | |
Latitude: 39.970000 | |
Longitude: -81.340000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2017-09-28 | Proposed Formations:TRENTON, Issued Date:9/28/2017, Expired Date:9/28/2019 12:00:00 PM, Drilling unit acres:, Proposed Well Type:ST, Proposed Well Class:STRT |
APP | 2018-04-06 | Proposed Formations:UTICA/POINT PLEASANT, Issued Date:4/6/2018, Expired Date:4/5/2020 12:00:00 PM, Drilling unit acres:1178.185, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2018-05-16 | |
Correction to Well | 2018-08-24 | TAKE TARGET UPDATE AS-DRILLED |
Completion Report Received | 2018-11-28 | |
Record Last Modified | 2018-12-13 | |
Construction Permit Expires | 2020-04-05 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2018-12-12 | 7953 | 8067 | 0 |
2018-12-12 | 27275 | 27380 | 0 |
27275 | 27380 | 0 | |
7953 | 8067 | 0 | |
7953 | 8067 | 0 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 07/18/2018 | 08/18/2018 | 7483.6 | 37,136,100.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Produced Water | Operator | Base Fluid | Water | 7732-18-5 | 100 | 9.18165 | 34,363,500.0 |
HP-9601 | One AquaSource Inc. | Breaker | Listed Below | Listed Below | 0 | 0 | 0 | |
FE-2A | Halliburton | Additive | Listed Below | Listed Below | 0 | 0 | 0 | |
SAND-COMMON WHITE-100 MESH | Halliburton | Proppant | Listed Below | Listed Below | 0 | 0 | 0 | |
MC B-8614 | Halliburton | Biocide | Listed Below | Listed Below | 0 | 0 | 0 | |
HP-2814 | One AquaSource Inc. | Friction Reducer | Listed Below | Listed Below | 0 | 0 | 0 | |
HYDROCHLORIC ACID | Halliburton | Solvent | Listed Below | Listed Below | 0 | 0 | 0 | |
SCALECHEK LP-50 | Halliburton | Scale Inhibitor | Listed Below | Listed Below | 0 | 0 | 0 | |
LD-2850 | Multi-chem | Friction Reducer | Listed Below | Listed Below | 0 | 0 | 0 | |
OILPERM A | Halliburton | Non-ionic Surfactant | Listed Below | Listed Below | 0 | 0 | 0 | |
HP-2220 | One AquaSource Inc. | Scale Inhibitor | Listed Below | Listed Below | 0 | 0 | 0 | |
HP-2816 | One AquaSource Inc. | Friction Reducer | Listed Below | Listed Below | 0 | 0 | 0 | |
LD-2550 | Multi-chem | Friction Reducer | Listed Below | Listed Below | 0 | 0 | 0 | |
HAI-OS ACID INHIBITOR | Halliburton | Corrosion Inhibitor | Listed Below | Listed Below | 0 | 0 | 0 | |
SAND-PREMIUM WHITE-30/50 | Halliburton | Proppant | Listed Below | Listed Below | 0 | 0 | 0 | |
MB-7532 | One AquaSource Inc. | Biocide | Listed Below | Listed Below | 0 | 0 | 0 | |
Ingredients | Listed Above | Listed Above | Water | 7732-18-5 | 100 | 0.289571 | 1,083,760.0 | |
Ammonium chloride | 12125-02-9 | 1.5 | 0.000822961 | 3081 | ||||
Distillates (petroleum, hydrotreated light) | 64742-47-8 | 18 | 0.00987554 | 36961 | ||||
Ethanol | 64-17-5 | 60 | 0.000323121 | 1210 | ||||
Naphthalene | 91-20-3 | 5 | 0.00002636 | 99 | ||||
Sodium hydroxide | 7647-14-5 | 10 | 0.00116198 | 4350 | ||||
Methanol | 67-56-1 | 60 | 0.000508609 | 1905 | ||||
Propargyl alcohol | 107-19-7 | 10 | 0.00005187 | 195 | ||||
1-Propanaminium, 3-amino-n-(carboxymethyl)-n,
n-dimethyl-n-coco alkyl derivatives, hydroxides and inner salts |
61789-40-0 | 60 | 0.000939515 | 3517 | ||||
Phosphate of a Diamine, Sodium Salt | Proprietary | 30 | 0.000196412 | 736 | ||||
Glycerine | 56-81-5 | 5 | 0.00007829 | 294 | ||||
Poly(oxy-1,2-ethanediyl), alpha-(4-nonylphenyl)-omega-hydroxy-,
branched |
127087-87-0 | 5 | 0.00002636 | 99 | ||||
Phosphoric acid | 7664-38-2 | 0.1 | 0.00000068 | 3 | ||||
Organic phosphate copolymer | 71050-62-9 | 25 | 0.00287658 | 10766 | ||||
Sodium chloride | 7647-14-5 | 30 | 0.000751075 | 2811 | ||||
Olefins | Proprietary | 5 | 0.00006225 | 236 | ||||
Hydrotreated light petroleum distillates | 64742-47-8 | 30 | 0.000751075 | 2811 | ||||
Quaternary ammonium compounds,
benzyl-C12-16-alkyldimethyl chlorides |
68424-85-1 | 5 | 0.00003421 | 129 | ||||
Citric acid | 77-92-9 | 60 | 0.00216943 | 8120 | ||||
Poly(oxy-1,2-ethanediyl), a-tridecyl-w-hydroxy-, branched | 69011-36-5 | 5 | 0.000380677 | 1425 | ||||
9-Octodecenamide, n, n-bis-2 (hydroxy-ethyl)-, (Z) | 93-83-4 | 5 | 0.000125179 | 469 | ||||
1,2,4 Trimethylbenzene | 95-63-6 | 1 | 0.00000527 | 20 | ||||
Distillate (petroleum), hydrotreated light) | 64742-47-8 | 20 | 0.00152271 | 5699 | ||||
Crystalline silica, quartz | 14808-60-7 | 100 | 9.47304 | 35,454,000.0 | ||||
Hydrochloric acid | 7647-01-0 | 15 | 0.0429661 | 160806 | ||||
Heavy aromatic petroleum naphtha | 64742-94-5 | 30 | 0.00015814 | 592 | ||||
Ethoxylated alcohols | Proprietary | 30 | 0.00015562 | 583 | ||||
Fatty acids, tall oil | Proprietary | 30 | 0.00015562 | 583 | ||||
Oxyalkylated phenolic resin | Proprietary | 30 | 0.000210853 | 790 | ||||
Alcohols, C12-16, ethoxylated | 68551-12-2 | 5 | 0.000125179 | 469 | ||||
Modified thiourea polymer | Proprietary | 30 | 0.00015562 | 583 | ||||
Ammonium persulfate | 7727-54-0 | 95 | 0.00179104 | 6704 | ||||
Glutaraldehyde | 111-30-8 | 30 | 0.000205252 | 769 | ||||
Dazomet | 533-74-4 | 24 | 0.00603234 | 22577 | ||||
Fresh Water | Operator | Base Fluid | Water | 7732-18-5 | 100 | 80.9478 | 302,957,000.0 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2018-07-18 | H2O | 15 | 334158 Gal | 274800 | Halliburton | STAGE 1/130
STAGES 2-129 SEE IMAGES |
2018-08-18 | H2O | 15 | 300941 Gal | 272660 | Halliburton | STAGE 130/130
STAGES 2-129 SEE IMAGES |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | ECLIPSE RESOURCES I LP | 568759 | 168583 | 93 |
2019 | ECLIPSE RESOURCES I LP | 561457 | 147565 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | ECLIPSE RESOURCES I LP | Brine | 38837 | 93 |
2019 | ECLIPSE RESOURCES I LP | Brine | 25441 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1006008437 | 2018-1-30 0:00: | CS | No Violations | 2.00 |
-709172815 | 2019-3-12 0:00: | PW | No Violations | 0.30 |
0212186130 | 2018-10-09 | Preliminary Restoration | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with valves in the open position. The production equipment consisted of four sand traps, 4 gas production units, and two 400-barrel tanks. Identification was posted at the wellhead. Southern Fencing company was on location installing chain link fencing around the pad. Location meets requirements for preliminary restoration. |
0500703194 | 2018-01-29 | Casing String Witnessed | No Violations | On the day of my inspection after receiving a call from Eclipse Consultant Charlie Frazier concerning the wellbore caving in after spudding the well on 1/27/18, I witnessed the below the cellar the sand based material had collapsed into the wellbore with drilling ceased. A meeting with Mr. Frazier and Cement Specialist Lex Cook was held where they propose to clean the wellbore up with a 42 inch diameter bit and install 36 inch drive pipe into bedrock and remove any excess water and then utilizing 9-grout fill the backside to surface. Precision cleaned the wellbore up with a 42 inch diameter bit to 16 feet and ran 21 feet of 36 inch 195.175 pound per foot drive pipe and drove it leaving it set at 5 feet below surface. Water was removed from the annulus and Caldwell Redi-Mix pumped 10 yards of 9-sack grout bringing grout to surface. Tomorrow Precision Rathole will commence drilling a 30 inch diameter hole to the total depth of 120 feet and then running 24 inch diameter conductor pipe with cement to follow. |
0709172815 | 2019-03-12 | Production Wells | No Violations | I was accompanied by ODNR Southeast Regional Manager Brent Bear and the purpose of our inspection was a status check. During my inspection the well was equipped with a plunger lift system with valves in the open position. The 13.375-inch diameter surface casing had 0 pounds per square inch, the 9.625-inch diameter intermediate casing had 1290 pounds per square inch, the 5.5-inch diameter production casing had 461 pounds per square inch, and the 2.875-inch diameter tubing had 900 pounds per square inch. The production equipment consisted of four sand traps, four gas production units, and two 400-barrel tanks. The produced water was being separated on pad and being stored in the 400-barrel tanks. Produced oil and gas was being gathered at the Eclipse outlaw pad via pipeline. Identification was located at the wellhead. |
1006008437 | 2018-01-30 | Casing String Witnessed | No Violations | On the day of my inspection I witnessed Precision Rathole drill through the grout and cleaned the wellbore up with a 42 inch diameter bit to 16 feet and ran 21 feet of 36 inch 195.175 pound per foot drive pipe and drove it to 26 feet leaving it set at 5 feet below surface. Water was removed from the annulus and Caldwell Redi-Mix pumped 10 yards of 9-sack grout bringing grout to surface. |
1063736660 | 2020-1-15 0:00: | PW | No Violations | 0.60 |
136345607 | 2020-1-15 0:00: | PW | No Violations | 0.50 |
1525104112 | 2018-04-30 | Drill / Deepen / Reopen | No Violations | During my inspection H&P Drilling Rig 531 was on location drilling the 12.25 inch diameter intermediate borehole at 4166 feet in depth. 9.625 inch diameter casing was laid out on the pipe racks. The Eclipse company man estimates that the cement job will be Wednesday 5/2/18. |
1548946965 | 2019-01-31 | Production Wells | No Violations | The purpose of my inspection was a status check. The pad is named Jupiter and on this date the pad consist of two production wells 3405924520 and 3405924521. During my inspection the well was equipped with a plunger lift system with valves in the open position. The 13.375-inch diameter surface casing had 0 pounds per square inch, the 9.625-inch diameter intermediate casing had 1100 pounds per square inch, the 5.5-inch diameter production casing had 530 pounds per square inch, and the 2.875-inch diameter tubing had 1100 pounds per square inch. The production equipment consisted of four sand traps, four gas production units, four frac tanks, and two 400-barrel tanks. The produced water was being separated on pad and distributed in the frac and 400-barrel tanks. The oil and gas were being gathered at the Eclipse outlaw pad via pipeline. Identification was located at the wellhead. |
1571229107 | 2019-10-9 0:00: | PW | No Violations | 0.20 |
1682330919 | 2019-12-4 0:00: | PW | No Violations | 0.50 |
1754808326 | 2018-09-10 | Completion Testing | No Violations | The purpose of my inspection was a status check on a preliminary restoration. During my inspection Deep Well Services stand alone snubbing unit 10 was on location drilling out frac plugs on 3405924521 and production equipment was being assembled. The area affected by pad construction has all been remediated with vegetation growth. The lease road was paved with asphalt and concrete and the pad was gravel. The location meets the preliminary restoration requirements for 1509.072 (A). |
2046745238 | 2018-02-01 | Casing String Witnessed | No Violations | On the day inspection I witnessed that Precision Rathole had drilled a 30 inch diameter hole to the depth of 100 feet and ran 102 feet of 24 inch diameter 94.62 pounds per foot conductor pipe with a 2 foot stick up. Stingray Pressure Pumping was onsite and pumped 2 barrels of fresh water, performed a 300 pounds per square inch pressure test and cemented pipe with 290 sacks Class A cement with 2% CaCl and .25 pound per sack of Celluseal weighing 15.6 pounds per gallon and a yield of 1.2 cubic foot per sack. Cement was weight was verified with pressurized mud scales and displaced to 92 feet with 48.3 barrels of fresh water with good cement returns of 12 barrels to surface. Mix water was tested revealing chlorides of 32 parts per million, pH 7 and 57 degrees. |
212186130 | 2018-10-9 0:00: | PL | No Violations | 0.20 |
500703194 | 2018-1-29 0:00: | CS | No Violations | 1.50 |
870332104 | 2020-7-29 0:00: | PW | No Violations | 1.00 |
For data sources see[10]