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34-063-20253

Well Details

Well ID: 34-063-20253
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Country: United States
State: Ohio
County: Hancock
Municipality: Portage Township
Operator Name: DUNBAR & SON OIL ENT INC
Well Pad ID:
Farm/Lease Name: KUHLMAN JAMES
License Status: Producing
License Date: 1982-05-06
Spud Date: 1982-10-30
Spud Drilling Contractor: SHELDON DRLG
Final Drill Date: 1982-11-08
Well Total Depth: 2030.00 ft
Configuration: Vertical
Latitude: 41.130000
Longitude: -83.690000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-05-06 Issued Date 5/6/82 Expired Date 11/1/82 Acres 0108535 Tool Type RTAF Proposed Formation TREMPEALEAU Proposed Depth 02030 Proposed Drill Depth 02030
Construction Permit Expires 1982-11-01 PERMIT EXPIRED.
Original Spud 1982-11-04 PERMIT EXPIRED.
Completed 1982-11-08 PERMIT EXPIRED.
Reached Total Depth 1982-11-08 PERMIT EXPIRED.
CO 1983-12-01 806 DUNBAR & SON OIL ENT INC GeoDate 5/6/82
Completion Report Received 1984-08-13 PERMIT EXPIRED.
Record Last Modified 2017-02-15 PERMIT EXPIRED.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1263 1917 0
1263 1917 0
1263 1917 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 1000 Gal 0 ACID;ACID & FRAC;OIL FOAM
ACID 0 1000 Gal 0 300 GAL. 15% MOD. 202., FOAM OIL FRAC.

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1401736513 2014-04-01 Production Wells Violations Noted At the time of the inspection the well is not in production and there are no production records on file. There was 4.5 casing with a Type S/SS casing head. There was 2 tubing, rods, stuffing box, polish rod, pulling rod, and bridal but there was no pumping unit on the well. The stuffing box has been bent over and broken off the production T making the well incapable of production at this time. The production lines were in disrepair and open to the atmosphere. There were no flow lines, tanks, lease road, or identification. The phone number listed in the Database was disconnected so no contact could be made with the operator. The landowner, James B. Kuhlman, was unavailable for information regarding the well and needs to be contacted regarding the status of the well.
1525973186 2018-05-10 Production Wells No Violations FOLLOWUP FOR NOV # 1401736513 FOR FAILURE TO IDENTIFY WELL AND REPORT PRODUCTION. The well is not in production and there are no production records on file. The well consist of 4.5 casing with a Type S/SS casing head. There is 2 tubing, rods, stuffing box, polish rod, pulling rod, and bridal but no pumping or storage units at the well site. The stuffing box has been bent over and broken off and the production T making the well incapable of production at this time. The production line is open to the atmosphere and no identification is posted. . The phone number listed in the RBDMS Database is disconnected and it appears the owner of the well is no longer in business. The landowner, James B. Kuhlman, was unavailable for information regarding the well.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1401736513 US-OH-111892 2014-06-12 Failure to legibly identify well
1401736513 US-OH-111893 2014-06-12 Well shall be plugged
1401736513 US-OH-111894 2014-06-12 Statement of annual production not filed

For data sources see[5]

References