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Well ID: 34-067-20117 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Franklin Township | |
Operator Name: ATLAS NOBLE LLC | |
Well Pad ID: | |
Farm/Lease Name: SHEEHAN | |
License Status: Final Restoration | |
License Date: 2016-04-27 | |
Spud Date: 1972-05-03 | |
Spud Drilling Contractor: | |
Final Drill Date: 1972-06-16 | |
Well Total Depth: 5780.00 ft | |
Configuration: Vertical | |
Latitude: 40.330000 | |
Longitude: -81.250000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1971-12-27 | 43 RESOURCE AMERICA INC GeoDate 12/27/71 |
Original Spud | 1972-05-03 | |
Completed | 1972-06-16 | |
Reached Total Depth | 1972-06-16 | |
Change of Owner | 2004-03-12 | Operator changed from 43, RESOURCE AMERICA INC to 6867, ATLAS AMERICA INC |
Change of Owner | 2011-01-27 | Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC |
Change of Owner | 2011-02-08 | Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC |
APP | 2016-04-27 | Proposed Formations:CLINTON, Issued Date:4/27/2016, Expired Date:4/27/2018 12:00:00 PM, Drilling unit acres:104.75, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2016-05-12 | |
Record Last Modified | 2017-02-10 | |
Construction Permit Expires | 2018-04-27 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5503 | 5575 | 0 |
5503 | 5575 | 0 | |
5503 | 5575 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2200 Bbl | 0 | AVG, PUMP RATE: 49.3 BPM. AVG. PRESS W/SD. 3166#; HHP 3867 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | RESOURCE AMERICA INC | 2083.00 | 0.00 | 365 |
1985 | RESOURCE AMERICA INC | 3540.00 | 0.00 | 365 |
1987 | RESOURCE AMERICA INC | 3392.00 | 0.00 | 365 |
1988 | RESOURCE AMERICA INC | 4245.00 | 0.00 | 365 |
1989 | RESOURCE AMERICA INC | 3676.00 | 0.00 | 365 |
1990 | RESOURCE AMERICA INC | 3120.00 | 0.00 | 365 |
1991 | RESOURCE AMERICA INC | 2963.00 | 50.00 | 365 |
1993 | RESOURCE AMERICA INC | 2242.00 | 0.00 | 365 |
1994 | RESOURCE AMERICA INC | 2561.00 | 0.00 | 365 |
1995 | RESOURCE AMERICA INC | 2659.00 | 0.00 | 365 |
1996 | RESOURCE AMERICA INC | 2000.00 | 0.00 | 365 |
1997 | RESOURCE AMERICA INC | 1940.00 | 0.00 | 365 |
1998 | RESOURCE AMERICA INC | 1785.00 | 49.00 | 365 |
1999 | RESOURCE AMERICA INC | 1828.00 | 0.00 | 365 |
2000 | RESOURCE AMERICA INC | 917.00 | 0.00 | 365 |
2001 | RESOURCE AMERICA INC | 2290.00 | 0.00 | 365 |
2002 | RESOURCE AMERICA INC | 1030.00 | 0.00 | 365 |
2003 | RESOURCE AMERICA INC | 1460.00 | 0.00 | 365 |
2004 | CHEVRON APPALACHIA LLC | 577.00 | 0.00 | 365 |
2005 | CHEVRON APPALACHIA LLC | 0.00 | 0.00 | 365 |
2006 | CHEVRON APPALACHIA LLC | 0.00 | 0.00 | 365 |
2007 | CHEVRON APPALACHIA LLC | 0.00 | 13.00 | 365 |
2008 | CHEVRON APPALACHIA LLC | 5.00 | 0.00 | 366 |
2009 | CHEVRON APPALACHIA LLC | 0.00 | 0.00 | 365 |
2010 | ATLAS NOBLE LLC | 0.00 | 0.00 | 365 |
2011 | CHEVRON APPALACHIA LLC | 0.00 | 0.00 | 365 |
2012 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2013 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2014 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2015 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2016 | ATLAS NOBLE LLC | 0.00 | 0.00 | 366 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1985 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1987 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1988 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1989 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1990 | RESOURCE AMERICA INC | Brine | 83 | 365 |
1991 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1993 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1994 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1995 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1996 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1997 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1998 | RESOURCE AMERICA INC | Brine | 12 | 365 |
1999 | RESOURCE AMERICA INC | Brine | 49 | 365 |
2000 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2001 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2002 | RESOURCE AMERICA INC | Brine | 27 | 365 |
2003 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2004 | CHEVRON APPALACHIA LLC | Brine | 0 | 365 |
2005 | CHEVRON APPALACHIA LLC | Brine | 0 | 365 |
2006 | CHEVRON APPALACHIA LLC | Brine | 0 | 365 |
2007 | CHEVRON APPALACHIA LLC | Brine | 9 | 365 |
2008 | CHEVRON APPALACHIA LLC | Brine | 0 | 366 |
2009 | CHEVRON APPALACHIA LLC | Brine | 0 | 365 |
2010 | ATLAS NOBLE LLC | Brine | 0 | 365 |
2011 | CHEVRON APPALACHIA LLC | Brine | 0 | 365 |
2012 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2013 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2014 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2015 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2016 | ATLAS NOBLE LLC | Brine | 0 | 366 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-188837696 | 2016-7-26 0:00: | FR | No Violations | 1.00 |
-287273690 | 2016-7-6 0:00:0 | FR | No Violations | 1.00 |
-879344796 | 2016-5-9 0:00:0 | PB | No Violations | 6.00 |
0188837696 | 2016-07-26 | Final Restoration | No Violations | On the day of my inspection, I found that the final restoration has been complete. The site passed final restoration according to ORC 1509.072(B). Resolving all compliance issues. |
0287273690 | 2016-07-06 | Final Restoration | No Violations | This meets the requirements for the final restoration to be approved. The area has been graded and seeded with good vegetation established. There is some junk not associated with the well on site, an old boat and several tires which will not be part of the final restoration. |
0490465812 | 2016-06-09 | Plug / Plug Back | No Violations | On the day of my inspection accompanied by inspector Mark Moreland, I discovered the location has been reclaimed. However, no vegetation was established. I will be back at a later date to check on the final restoration. |
0879344796 | 2016-05-09 | Plug / Plug Back | No Violations | Began today with a Safety Meeting that included Atlas Noble, Nicks Well Plugging, Specialized Safety Service and ODNR Supervisors Bear and Moreland along with 3 Inspectors. Went over safety standards and plugging operations. Next went to the well to begin plugging. The first action was to set up a safety perimeter and a first and second muster area. Specialized Safety set up monitors and alarms and then allowed the plugging crew to add Sulfide blocker to the annular space between the 8 5/8 inch casing and the 4 1/2 casing. After the blocker was applied the readings dropped to 1 or 2 PPM. Nicks Well then inserted a spear into the 1 1/2 inch diameter tubing and was able to pull out one joint. The rabbit came up and they think the tubing is clear. Appalachian Well should be able to run in and shoot off the seating nipple at the bottom. They are scheduled for Tuesday morning at 7 AM |
0989911503 | 2016-05-05 | Administrative Inspection | No Violations | Meeting today with Inspector Zollars to calculate top of cement and figure plugs for the upcoming plug job. Prepare plug schedule before the meeting with Atlas Noble and Nicks Well Plugging. Calculate displacement and perforations needed to plug the H2S well and make copies. |
1460645743 | 2016-04-14 | Production Wells | Violations Noted | I am on site accompanied by Inspector Mark Moreland, I witnessed the production tanks have been removed and production equipment consist of a horizontal separator. The well is utilizing a plunger lift system equipped with 8.625 inch diameter surface casing, 4.5 inch diameter production casing, and 1.5 inch diameter production tubing. All valves are in the closed position. Utilizing an ODNR Honeywell PhD6 meter I recorded readings of 100 ppm H2S at the well head. The well head has lost integrity and is venting H2S (Hydrogen Sulfide) gas to atmosphere through a quarter sized hole placed on the side of the well head. It appears all strings of casing/tubing have also been impacted by the poisonous gas, causing the loss of integrity and promoting higher safety/environmental risk. The well has not produced commercially since 2005. After we conducted our inspection, I then placed a call to Pat Ervin (Atlas Nobles Supervisor) at (330) 319-3155 to inform him that this well is presenting an eminent threat to the environment and health/safety. I also stated that the well needs to be plugged as soon as possible. Pat informed me that he would provide me with a written plan and he understood the well was a hazard and needed to be plugged. Pat also stated that he plans to get the well plugged as soon as possible. The well owner/ operator shall apply for a permit to plug the well. The well owner/operator shall submit a written plugging schedule to Joe Zollars at 2207 Reiser Ave S.E New Philadelphia, Ohio 44663 within 30 days, per OAC 1501:9-11-05(B), and plug the well within 60 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
1462881548 | 2016-05-04 | Administrative Inspection | No Violations | I had a call today from Pat Ervin to go over information on the up coming plugging operation for the Sheehan well. Pat said that he wanted at least two Specialized Safety personnel on site for this plug. This is due to the known hazardous H2S conditions at the well. He also advised that he wanted them to have air packs available should any problem arise. I ask Pat if he had plans for how the well was to be plugged and he advised that a meeting was scheduled for Monday. The details will be worked out during that meeting. Atlas, Nicks Well Plugging and Specialized Safety along with ODNR staff are scheduled for 8:30 AM I contacted District Supervisor Mike Moreland and he is to contact the remaining ODNR staff that will attend the meeting. |
1901435660 | 2016-05-19 | Final Restoration | No Violations | I am on site today to check the well for leaks after it has been plugged. I did not find any leaks or gas bubbles. Well has been cut off and area needs graded and seeded. Final could not be passed today. |
1913847673 | 2016-04-21 | Production Wells | No Violations | I am on site today accompanied by my supervisor Mike Moreland following up on Compliance Number 1460645743, were I witness no changes has occurred since my last inspection. The well head is still leaking H2S gas at approximately 125 ppm and should be considered a definite health/environmental issue. With the last conversion I had with Pat Ervin, he stated that Atlas should meet the 60 day requirement to plug the well bore. |
2098667333 | 2016-05-09 | Production Wells | No Violations | On the day of my inspection accompanied by ODNR Southeast Regional Supervisor Brent Bear, Southeast District Supervisor Mike Moreland, Inspectors Mark Moreland and Joe Zollars, we met with Atlas Field Superintendent Chuck Wood and Nicks Well Plugging representatives and discussed upcoming plugging of well. |
490465812 | 2016-6-9 0:00:0 | PB | No Violations | 1.00 |
989911503 | 2016-5-5 0:00:0 | AM | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1460645743 | US-OH-113338 | 2016-08-12 | Well operation causing pollution and contamination | |
1460645743 | US-OH-113339 | 2016-08-12 | General Safety | |
1460645743 | US-OH-113340 | 2016-08-12 | Well shall be plugged | |
1460645743 | US-OH-113341 | 2016-08-12 | Defective casing, leaking well |
For data sources see[9]