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34-067-20165

Well Details

Well ID: 34-067-20165
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Country: United States
State: Ohio
County: Harrison
Municipality: Washington Township
Operator Name: ATLAS NOBLE LLC
Well Pad ID:
Farm/Lease Name: IRELAND
License Status: Plugged and Abandoned
License Date: 2016-09-13
Spud Date: 1974-01-31
Spud Drilling Contractor:
Final Drill Date: 1974-10-01
Well Total Depth: 5549.00 ft
Configuration: Vertical
Latitude: 40.300000
Longitude: -81.300000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1972-12-08 43 RESOURCE AMERICA INC GeoDate 12/8/72
Original Spud 1974-01-31 RE-ISSUE & REV. LOC. 11-14-73
Completed 1974-10-01 RE-ISSUE & REV. LOC. 11-14-73
Reached Total Depth 1974-10-01 RE-ISSUE & REV. LOC. 11-14-73
Change of Owner 2004-03-12 Operator changed from 43, RESOURCE AMERICA INC to 6867, ATLAS AMERICA INC
Change of Owner 2011-01-27 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
Change of Owner 2011-02-08 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
APP 2014-02-03 Proposed Formations:CLINTON, Issued Date:2/3/2014, Expired Date:2/3/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
APP 2016-09-13 Proposed Formations:CLINTON, Issued Date:9/13/2016, Expired Date:9/13/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-10-19 RE-ISSUE & REV. LOC. 11-14-73
Record Last Modified 2017-02-15 RE-ISSUE & REV. LOC. 11-14-73
Construction Permit Expires 2018-09-13 RE-ISSUE & REV. LOC. 11-14-73

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5475 5479 26
5475 5479 26
5475 5479 26

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2159 Bbl 0 68.3 BPM, PRESS 2950#, HHP 4582.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RESOURCE AMERICA INC 4204.00 0.00 365
1985 RESOURCE AMERICA INC 3450.00 63.00 365
1987 RESOURCE AMERICA INC 6008.00 61.00 365
1988 RESOURCE AMERICA INC 4524.00 109.00 365
1989 RESOURCE AMERICA INC 4344.00 58.00 365
1990 RESOURCE AMERICA INC 4497.00 62.00 365
1993 RESOURCE AMERICA INC 3406.00 0.00 365
1994 RESOURCE AMERICA INC 3429.00 51.00 365
1995 RESOURCE AMERICA INC 3274.00 66.00 365
1996 RESOURCE AMERICA INC 3013.00 0.00 365
1997 RESOURCE AMERICA INC 2454.00 67.00 365
1998 RESOURCE AMERICA INC 1758.00 0.00 365
1999 RESOURCE AMERICA INC 1657.00 0.00 365
2000 RESOURCE AMERICA INC 1252.00 74.00 365
2001 RESOURCE AMERICA INC 1113.00 0.00 365
2002 RESOURCE AMERICA INC 1097.00 0.00 365
2003 RESOURCE AMERICA INC 1286.00 0.00 365
2004 CHEVRON APPALACHIA LLC 1335.00 65.00 365
2005 CHEVRON APPALACHIA LLC 1289.00 0.00 365
2006 CHEVRON APPALACHIA LLC 604.00 0.00 365
2007 CHEVRON APPALACHIA LLC 0.00 37.00 365
2008 CHEVRON APPALACHIA LLC 0.00 0.00 366
2009 CHEVRON APPALACHIA LLC 0.00 0.00 365
2010 ATLAS NOBLE LLC 0.00 0.00 365
2011 CHEVRON APPALACHIA LLC 0.00 0.00 365
2012 ATLAS NOBLE LLC 0.00 0.00 0
2013 ATLAS NOBLE LLC 0.00 0.00 0
2014 ATLAS NOBLE LLC 0.00 0.00 0
2015 ATLAS NOBLE LLC 0.00 0.00 0
2016 ATLAS NOBLE LLC 0.00 0.00 366

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RESOURCE AMERICA INC Brine 0 365
1985 RESOURCE AMERICA INC Brine 0 365
1987 RESOURCE AMERICA INC Brine 0 365
1988 RESOURCE AMERICA INC Brine 0 365
1989 RESOURCE AMERICA INC Brine 0 365
1990 RESOURCE AMERICA INC Brine 130 365
1993 RESOURCE AMERICA INC Brine 0 365
1994 RESOURCE AMERICA INC Brine 0 365
1995 RESOURCE AMERICA INC Brine 0 365
1996 RESOURCE AMERICA INC Brine 0 365
1997 RESOURCE AMERICA INC Brine 0 365
1998 RESOURCE AMERICA INC Brine 0 365
1999 RESOURCE AMERICA INC Brine 32 365
2000 RESOURCE AMERICA INC Brine 0 365
2001 RESOURCE AMERICA INC Brine 0 365
2002 RESOURCE AMERICA INC Brine 64 365
2003 RESOURCE AMERICA INC Brine 0 365
2004 CHEVRON APPALACHIA LLC Brine 9 365
2005 CHEVRON APPALACHIA LLC Brine 0 365
2006 CHEVRON APPALACHIA LLC Brine 43 365
2007 CHEVRON APPALACHIA LLC Brine 3 365
2008 CHEVRON APPALACHIA LLC Brine 0 366
2009 CHEVRON APPALACHIA LLC Brine 0 365
2010 ATLAS NOBLE LLC Brine 0 365
2011 CHEVRON APPALACHIA LLC Brine 0 365
2012 ATLAS NOBLE LLC Brine 0 0
2013 ATLAS NOBLE LLC Brine 0 0
2014 ATLAS NOBLE LLC Brine 0 0
2015 ATLAS NOBLE LLC Brine 0 0
2016 ATLAS NOBLE LLC Brine 66 366

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2002615813 2016-9-29 0:00: PW No Violations 4.00
-52421377 2016-10-19 0:00 PB No Violations 12.00
-854289650 2017-4-10 0:00: FR No Violations 1.00
-913224120 2016-10-14 0:00 PB No Violations 6.00
0052421377 2016-10-19 Plug / Plug Back No Violations

-978 feet using 51 sacks of Class A cement and . After setting the plug NWP then pulled the casing to a depth of 828 feet, established circulation and set another plug from a depth of 828 feet to 628 feet using 60 sacks of Class A cement. The casing was then pulled to 200 feet, where cement was circulated to surface.

0080914575 2016-09-08 Production Wells No Violations I arrived on site today to perform a follow-up inspection on a well control issue that my previous inspection revealed. With the conduction of my inspection today, I discovered the casing patch Atlas had installed on the production casing has slowed down the leak of the production fluid around the well head. The containment dike around the well head appears to be containing on fluids. After my inspection I called Chuck Woods (an Atlas Noble Supervisor) who informed me that Nicks Well Plugging Service will be on site to plug the well within 3 weeks.
0492069265 2013-09-09 Production Wells Violations Noted Arrived on location and found well idle, checked production reports which show that the well has not produced since 2007. Make well capable of commercial production within 30 days; or plugging is required within 60 days. Failure to comply may result in forfeture of bond.
0618623657 2016-10-17 Plug / Plug Back No Violations
0789402028 2013-09-09 Production Wells No Violations FOLLOW UP TO NOV # 492069265 Arrived on location and found well idle, checked production reports which show that the well has not produced since 2007. Make well capable of commercial production within 30 days; or plugging is required within 60 days. Failure to comply may result in forfeiture of bond.
0854289650 2017-04-10 Final Restoration No Violations Well has been plugged. Onsite to check for vegetation for final restoration. Site has not established vegetation and needs reseeded. I will contact Atlas Noble representative to inform them of necessary reclamation.
0912394276 2016-11-03 Final Restoration No Violations On the day of my inspection I witnessed that the lease road and well location had been restored. However vegetation was not established due to the season. With the inspection of the well bore I did not notice any signs of plug malfunction.
0913224120 2016-10-14 Plug / Plug Back No Violations
1281276057 2017-11-13 Final Restoration No Violations On the day of my inspection I walked out to the area of the plugged well. There remains a barren area that is likely due water saturation. This area is a low spot in a flat floodplain area. Cattails are growing on a portion of it. Cannot pass final restoration until vegetation is adequate.
1379021524 2016-10-20 Plug / Plug Back No Violations On the day of my inspection I witnessed that the surface plug had not dropped, after witnessing the plug had not drop I then witnessed Atlas noble digging up the well 3 feet below ground level, cutting the surface casing and installing ID plate on casing prior to filling hole back in. Atlas noble graded the location to the best of their ability. I will arrive on site at a later date to check on the status of the final restoration.
1458307317 2016-03-17 Production Wells No Violations On the day of my inspection accompanied by Inspector Mark Moreland following up on in NOV 492069265, I witnessed the well is still idle. All valves on the well head are in the closed position and all the production equipment has been removed.
1502281142 2016-10-18 Plug / Plug Back No Violations
1941428490 2016-10-13 Plug / Plug Back No Violations I am on site today to perform a site overview and review the process that will be taken to plug the well bore. While on site I met with Chuck Woods and Jeff Shepard. We created a schedule on where to put the plugs and how the well would be plugged.
2002615813 2016-09-29 Production Wells No Violations On the day of my inspection, I witnessed the temporary earthen dike around the well head is holding all pollution and contamination. During my inspection I was unable to capture how high the chloride readings were inside the dike, due to the fact my chloride testing strips could not read levels that high. While on site I walked a 300 foot perimeter around the well where I saw no signs of environmental impact since my last inspection. After my inspection I placed a call to Chuck Woods (an Atlas Noble supervisor) who informed that Nicks Well Plugging Service should be rigged up over the well within the next two weeks to plug the well. A permit has been received to plug and abounded this well bore.
2055221497 2016-08-19 Production Wells No Violations On the day of my inspection I witnessed the well consist of 4.5 inch diameter production casing and 1.5 inch diameter production tubing. All valves were placed in the closed position and the well was disconnected from the flow line. With the conduction of my inspection I discovered the 4.5 inch diameter production casing has lost integrity above the well head and is leaking fluids to surface level. There was a kill area around the well head that measured approximately 25 foot by 30 foot in diameter and penetrated approximately 3 inches of the soil. After my inspection I placed a call to Chris Belch (an Atlas Noble production supervisor and informed him of the issues) he stated that he was un-aware the well was leaking and he would access the contaminated area as soon as possible. We agreed to meet on site 8/22/2016 to gather a plan on resolving the issues with the well. I also informed Chris that the well would need to be plugged as soon as possible.
492069265 2013-9-9 0:00:0 PW No Violations
618623657 2016-10-17 0:00 PB No Violations 11.00
789402028 2013-9-9 0:00:0 PW No Violations
80914575 2016-9-8 0:00:0 PW No Violations 2.00
912394276 2016-11-3 0:00: FR No Violations 1.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0492069265 US-OH-125387 2013-09-09 Well shall be plugged

For data sources see[9]

References