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| Well ID: 34-067-20221 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Harrison | |
| Municipality: Freeport Township | |
| Operator Name: CHEVRON APPALACHIA LLC | |
| Well Pad ID: | |
| Farm/Lease Name: RUPERT | |
| License Status: Final Restoration | |
| License Date: 2006-04-18 | |
| Spud Date: 1975-05-05 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1975-05-18 | |
| Well Total Depth: 5745.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.190000 | |
| Longitude: -81.290000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1973-11-27 | 43 RESOURCE AMERICA INC GeoDate 11/27/73 |
| Completed | 1975-05-18 | RE-ISSUE 8-21-74, 1/29/75 |
| Original Spud | 1975-05-18 | RE-ISSUE 8-21-74, 1/29/75 |
| Reached Total Depth | 1975-05-18 | RE-ISSUE 8-21-74, 1/29/75 |
| Change of Owner | 2004-03-12 | Operator changed from 43, RESOURCE AMERICA INC to 6867, ATLAS AMERICA INC |
| APP | 2006-04-18 | Proposed Formations:CLINTON, Issued Date:4/18/2006, Expired Date:4/18/2007 6:00:00 AM, Drilling unit acres:158.19, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2006-04-21 | RE-ISSUE 8-21-74, 1/29/75 |
| Construction Permit Expires | 2007-04-18 | RE-ISSUE 8-21-74, 1/29/75 |
| Record Last Modified | 2013-09-18 | RE-ISSUE 8-21-74, 1/29/75 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2006-09-11 | 5623 | 5694 | 19 |
| 5623 | 5694 | 19 | |
| 5623 | 5694 | 19 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 66170 Gal | 60000 |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
| 1985 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
| 1987 | RESOURCE AMERICA INC | 11558.00 | 0.00 | 365 |
| 1988 | RESOURCE AMERICA INC | 6501.00 | 0.00 | 365 |
| 1989 | RESOURCE AMERICA INC | 4585.00 | 89.00 | 365 |
| 1990 | RESOURCE AMERICA INC | 5324.00 | 0.00 | 365 |
| 1991 | RESOURCE AMERICA INC | 5288.00 | 82.00 | 365 |
| 1993 | RESOURCE AMERICA INC | 4445.00 | 0.00 | 365 |
| 1994 | RESOURCE AMERICA INC | 2887.00 | 0.00 | 258 |
| 1995 | RESOURCE AMERICA INC | 0.00 | 0.00 | 0 |
| 1996 | RESOURCE AMERICA INC | 0.00 | 0.00 | 0 |
| 1997 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
| 1998 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
| 1999 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
| 2000 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
| 2001 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
| 2002 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
| 2003 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
| 2004 | CHEVRON APPALACHIA LLC | 0.00 | 0.00 | 365 |
| 2005 | CHEVRON APPALACHIA LLC | 0.00 | 0.00 | 365 |
| 2006 | CHEVRON APPALACHIA LLC | 0.00 | 118.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 1985 | RESOURCE AMERICA INC | Brine | 1190 | 365 |
| 1987 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 1988 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 1989 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 1990 | RESOURCE AMERICA INC | Brine | 142 | 365 |
| 1991 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 1993 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 1994 | RESOURCE AMERICA INC | Brine | 0 | 258 |
| 1995 | RESOURCE AMERICA INC | Brine | 0 | 0 |
| 1996 | RESOURCE AMERICA INC | Brine | 0 | 0 |
| 1997 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 1998 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 1999 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 2000 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 2001 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 2002 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 2003 | RESOURCE AMERICA INC | Brine | 0 | 365 |
| 2004 | CHEVRON APPALACHIA LLC | Brine | 0 | 365 |
| 2005 | CHEVRON APPALACHIA LLC | Brine | 0 | 365 |
| 2006 | CHEVRON APPALACHIA LLC | Brine | 35 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1228800905 | 2006-4-18 0:00: | PB | No Violations | 1.00 |
| -1685794241 | 2013-9-16 0:00: | FR | No Violations | 1.50 |
| 0667582127 | 2006-04-13 | Production Wells | Violations Noted | Inspection revealed that the well is still idle . Talked with Terry Whitehair and he advised that they are applying for the plugging permit and that they need a couple of more weeks to get the well plugged . I advised that they can have an extension until 04/28/06 . |
| 1110382263 | 2005-03-07 | Production Wells | Violations Noted | Inspection revealed that the well is an idle well ; incapable of production . The separator has been unhooked and the the wellhead is shut in (valves are rusted ) . Production reports submitted by the operator to Columbus indicates that there hasnt been any production reported since 1995 . The operator needs to plug or produce the well . Remedial action must be completed by April 11th, 2005 . |
| 1141705939 | 2006-02-24 | Production Wells | Violations Noted | Jim Hershman complaint of idle well and occasional H2S gas odor . Inspection of the well revealed that the well is idle . The valves on the wellhead are all closed and rusted . Parts of the separator is missing and the gas sales line is unhooked . I am issuing a written NOV to Atlas America to plug or produce the well . Note: There is a faint H2S gas odor at the wellhead at this time . I didnt have my gas detector with me to check the H2S gas levels . |
| 1145988249 | 2006-04-19 | Plug / Plug Back | No Violations | On site to witness the bottom hole plug ( Clinton Plug ) . Formation cementing pumped a 25 sk plug thru tubing to plug from 5644 to 5344 . H2S gas odor while they were pumping the plug . Gary Haught advised that they were going to rip the 4 1/2 casing and pull the casing because there is a hole in the casing . They are going to run tubing back into the well to finish plugging the well . Should be ready on Monday morning to finish plugging the well . |
| 1228800905 | 2006-04-18 | Plug / Plug Back | No Violations | Inspection revealed that Cardinal Well Services has fished the 1 1/2 tubing out of the well and are running the 2 3/8 upset tubing back into the well to spot the bottom hole plug tomorrow morning . |
| 1500062950 | 2006-04-21 | Plug / Plug Back | No Violations | On site today to finish plugging the well . Pumped the Clinton plug on 04/19/2006 . Pumped the lime plug , bottom 8 5/8 plug , berea plug , and the surface plug . Well has plugged and abandoned . This well is associated with the Jim Hershman complaint . Case can be resolved at this time . |
| 1685794241 | 2013-09-16 | Final Restoration | No Violations | On the day of my inspection I witnessed that the pit had been filled, vegetation was in place. All production equipment had been removed. Site passed according to 1509.072B. |
| 1875421302 | 2006-04-18 | Plug / Plug Back | No Violations | Inspection revealed that Cardinal Well Services is running a fishing tool back into the well with tubing ; trying to fish out the 1 1/2 tubing that H2S gas rotted of at app. 2785. They got ahold of the tubing with the fishing tool and started coming out of the hole . I advised that I would return to the site later today to check on the progress of the fishing job. |
| 667582127 | 2006-4-13 0:00: | PW | No Violations | 1.00 |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0667582127 | US-OH-127559 | 2006-04-23 | Well shall be plugged | |
| 1110382263 | US-OH-102748 | 2005-03-09 | Well shall be plugged | |
| 1141705939 | US-OH-103589 | 2006-03-06 | Well shall be plugged |
For data sources see[9]