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Well ID: 34-067-20525 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Washington Township | |
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL | |
Well Pad ID: | |
Farm/Lease Name: DUNLAP PHILLIP & NEAL | |
License Status: Producing | |
License Date: 1982-03-12 | |
Spud Date: 1982-03-16 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1982-03-19 | |
Well Total Depth: 6276.00 ft | |
Configuration: Vertical | |
Latitude: 40.230000 | |
Longitude: -81.230000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1982-03-12 | Issued Date 3/15/82 Expired Date 9/11/82 Acres 0279830 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06276 Proposed Drill Depth 06276 |
Original Spud | 1982-03-15 | |
Completed | 1982-03-19 | |
Reached Total Depth | 1982-03-19 | |
CO | 1982-04-19 | 168 RED HILL DEVELOPMENT GeoDate 3/12/82 |
Construction Permit Expires | 1982-09-11 | |
Completion Report Received | 1984-01-30 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 6065 | 6180 | 0 |
6065 | 6180 | 0 | |
2006-09-11 | 6086 | 6142 | 6 |
6086 | 6142 | 6 | |
6065 | 6180 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 67880 Gal | 0 | FRAC: WATER |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1747379136 | 2006-3-22 0:00: | PW | No Violations | 1.00 |
0093377304 | 2006-02-24 | Production Wells | Violations Noted | Inspection revealed that there are several small leaks in the oil storage tank app. 2/3 of the way up the tank . The biggest hole has a stick stuck in it to try to prevent it from leaking . The other spots look like rust bubbles and they are leaking (weeping) oil . There is pollution and contamination inside the tank battery SPCC dike ; less than 5 gallons of free oil . The rest of the pollution and contamination is black stained stone and dirt inside the dike . The tank battery consists of one 210 bbl oil storage tank . |
1347757565 | 2020-3-17 0:00: | PW | No Violations | 1.00 |
1501165314 | 2017-07-27 | Production Wells | No Violations | On the day of my inspection I found this plunger lift well equipped with a motor valve, 4.5 inch diameter casing, and 2.375 inch diameter tubing. Domestic meter off of the 4.5 inch diameter casing. Production equipment includes a 100 barrel steel production tank, a horziontal seperator with meter box and a 1 inch diameter sales line orfice, all contained in an earthened dike. Tank is identified and production is current in RBDMS. Well is shut in on tubing and partially open on casing. |
1747379136 | 2006-03-22 | Production Wells | No Violations | Follow-up inspection revealed that the leaking oil storage tank has been removed and replaced with a new 100 bbl oil storage tank . The pollution and contamination inside the tank battery SPCC dike has been cleaned up and new stone placed inside the dike . The SPCC dike has been reconstructed to meet the SPCC requirements . All violations have been corrected at this time . Case RESOLVED at this time . |
93377304 | 2006-2-24 0:00: | PW | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0093377304 | US-OH-130678 | 2006-03-06 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[9]