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Well ID: 34-067-20531 | ![]() Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. ![]() |
Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Moorefield Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: DUNLAP HARVEY L & SHIRLEY | |
License Status: Final Restoration | |
License Date: 2013-05-02 | |
Spud Date: 1982-04-12 | |
Spud Drilling Contractor: | |
Final Drill Date: 1982-04-19 | |
Well Total Depth: 6345.00 ft | |
Configuration: Vertical | |
Latitude: 40.200000 | |
Longitude: -81.220000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1982-03-16 | 2143 CARLESS RESOURCES INC GeoDate 3/16/82 |
Oil and Gas | 1982-03-16 | Issued Date 3/17/82 Expired Date 9/13/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06345 Proposed Drill Depth 06345 |
Original Spud | 1982-04-12 | IP. A.F. |
Completed | 1982-04-19 | IP. A.F. |
Reached Total Depth | 1982-04-19 | IP. A.F. |
Completion Report Received | 1982-10-01 | IP. A.F. |
Change of Owner | 1998-06-15 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2013-05-02 | Proposed Formations:CLINOTN, Issued Date:5/2/2013, Expired Date:5/2/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-11-20 | IP. A.F. |
Construction Permit Expires | 2015-05-02 | IP. A.F. |
Record Last Modified | 2017-02-15 | IP. A.F. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 6160 | 6225 | 2 |
6160 | 6225 | 2 | |
6160 | 6225 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 0 | 50000 | FRAC: FLUID, 50M SAND, 500G ACID |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1636108571 | 2013-12-19 0:00 | PB | No Violations | 1.50 |
-2046594771 | 2013-9-17 0:00: | PW | No Violations | 2.50 |
-490251213 | 2013-11-19 0:00 | PB | No Violations | 4.00 |
-950551418 | 2013-11-20 0:00 | PB | No Violations | |
0286629085 | 2016-06-17 | Final Restoration | No Violations | On the day of my inspection, I found that the final restoration has been complete. The site passed final restoration according to ORC 1509.072(B). |
0490251213 | 2013-11-19 | Plug / Plug Back | No Violations | I am on site today to plug this well and Chipco could not get 4 -1/2 inch casing to rip. On site while they went thru 3 blades and went after more. Did not witness any plugs today. |
0697371033 | 2013-11-21 | Plug / Plug Back | No Violations | Today I am on site to check the well for leaks. I did not find any leaks. The well has been cut off and can be covered over. I am also waiting to meet Little Bit for the cement ticket but he did not arrive. |
0950551418 | 2013-11-20 | Plug / Plug Back | No Violations | Chipco Well Service has Appalachian Wire line service on site to shoot the 4-1/2 inch diameter casing off. Was able to shoot off at 1660 ft. Chipco pulled one joint of casing out and then, wait on cement trucks. They were scheduled for 8:30 am. |
1384955577 | 2013-11-19 | Plug / Plug Back | No Violations | I am on site today to finish plugging this well to surface. The bottom plug and the Big Lime plug have been set. They tried to rip the 4-1/2 inch diameter casing and were not able to get a rip. Chipco Well service went thru 5 new blades and did not get the casing to rip. Next I advised that casing would have to be shot off . |
1546112570 | 2013-11-12 | Plug / Plug Back | No Violations | I am on site today to plug this well to surface. Chipco well service was to start plugging today but had to cancel the job today because they are not ready to plug. |
1636108571 | 2013-12-19 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed that the well has been plugged and all equipment has been removed. Compliance issue has been resolved. |
2046594771 | 2013-09-17 | Production Wells | Violations Noted
- 210bbl tanks. There was no domestic gas, pumping unit, flow line, separator, sales line, valves were closed on wellhead and no well identification. The well has not had any production the last 5 calendar years. The owner shall produce this well within 30 days or the well shall be plugged within 90 days. If the well is placed in production proper identification shall be posted. Spoke with Tim McConaha Enervest Energy at 330-877-6747 and he stated that the well is on their plugging list and a permit has been issued. | |
286629085 | 2016-6-17 0:00: | FR | No Violations | 1.00 |
697371033 | 2013-11-21 0:00 | PB | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
2046594771 | US-OH-120836 | 2014-04-23 | Well shall be plugged |
For data sources see[9]