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34-067-20681

Well Details

Well ID: 34-067-20681
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Country: United States
State: Ohio
County: Harrison
Municipality: Franklin Township
Operator Name: ATLAS NOBLE LLC
Well Pad ID:
Farm/Lease Name: A HARSHEY
License Status: Final Restoration
License Date: 2012-10-22
Spud Date: 1984-09-10
Spud Drilling Contractor: CHM DRLG
Final Drill Date: 1984-09-13
Well Total Depth: 5716.00 ft
Configuration: Vertical
Latitude: 40.360000
Longitude: -81.240000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-09-04 43 RESOURCE AMERICA INC GeoDate 9/4/84
Oil and Gas 1984-09-04 Issued Date 9/4/84 Expired Date 3/3/85 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05716 Proposed Drill Depth 05716
Original Spud 1984-09-10
Completed 1984-09-13
Reached Total Depth 1984-09-13
Completion Report Received 1984-12-13
Change of Owner 2004-03-12 Operator changed from 43, RESOURCE AMERICA INC to 6867, ATLAS AMERICA INC
Change of Owner 2011-01-27 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
Change of Owner 2011-02-08 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
APP 2012-10-22 Proposed Formations:CLINTON, Issued Date:10/22/2012, Expired Date:10/22/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-03-12
Construction Permit Expires 2014-10-22
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5457 5527 0
5457 5527 0
2006-09-11 5486 5524 48
5486 5524 48
5457 5527 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 0 0 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RESOURCE AMERICA INC 0.00 0.00 365
1985 RESOURCE AMERICA INC 9984.00 384.00 365
1987 RESOURCE AMERICA INC 3572.00 387.00 365
1988 RESOURCE AMERICA INC 2082.00 305.00 365
1989 RESOURCE AMERICA INC 1206.00 292.00 365
1990 RESOURCE AMERICA INC 939.00 195.00 365
1991 RESOURCE AMERICA INC 1276.00 239.00 365
1993 RESOURCE AMERICA INC 730.00 89.00 306
1994 RESOURCE AMERICA INC 0.00 0.00 50
1995 RESOURCE AMERICA INC 460.00 0.00 40
1996 RESOURCE AMERICA INC 290.00 1040.00 71
1997 RESOURCE AMERICA INC 880.00 148.00 195
1998 RESOURCE AMERICA INC 1150.00 208.00 365
1999 RESOURCE AMERICA INC 1045.00 92.00 365
2000 RESOURCE AMERICA INC 1091.00 95.00 365
2001 RESOURCE AMERICA INC 963.00 0.00 324
2002 RESOURCE AMERICA INC 156.00 97.00 365
2003 RESOURCE AMERICA INC 0.00 0.00 365
2004 CHEVRON APPALACHIA LLC 0.00 0.00 365
2005 CHEVRON APPALACHIA LLC 0.00 0.00 365
2006 CHEVRON APPALACHIA LLC 0.00 0.00 365
2007 CHEVRON APPALACHIA LLC 0.00 0.00 365
2008 CHEVRON APPALACHIA LLC 0.00 0.00 366
2009 CHEVRON APPALACHIA LLC 0.00 0.00 365
2010 ATLAS NOBLE LLC 0.00 0.00 365
2011 CHEVRON APPALACHIA LLC 0.00 0.00 365
2012 ATLAS NOBLE LLC 0.00 0.00 0
2013 ATLAS NOBLE LLC 0.00 0.00 0
2014 ATLAS NOBLE LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RESOURCE AMERICA INC Brine 0 365
1985 RESOURCE AMERICA INC Brine 459 365
1987 RESOURCE AMERICA INC Brine 0 365
1988 RESOURCE AMERICA INC Brine 0 365
1989 RESOURCE AMERICA INC Brine 0 365
1990 RESOURCE AMERICA INC Brine 56 365
1991 RESOURCE AMERICA INC Brine 0 365
1993 RESOURCE AMERICA INC Brine 0 306
1994 RESOURCE AMERICA INC Brine 0 50
1995 RESOURCE AMERICA INC Brine 0 40
1996 RESOURCE AMERICA INC Brine 0 71
1997 RESOURCE AMERICA INC Brine 0 195
1998 RESOURCE AMERICA INC Brine 302 365
1999 RESOURCE AMERICA INC Brine 0 365
2000 RESOURCE AMERICA INC Brine 0 365
2001 RESOURCE AMERICA INC Brine 0 324
2002 RESOURCE AMERICA INC Brine 182 365
2003 RESOURCE AMERICA INC Brine 0 365
2004 CHEVRON APPALACHIA LLC Brine 70 365
2005 CHEVRON APPALACHIA LLC Brine 0 365
2006 CHEVRON APPALACHIA LLC Brine 0 365
2007 CHEVRON APPALACHIA LLC Brine 0 365
2008 CHEVRON APPALACHIA LLC Brine 0 366
2009 CHEVRON APPALACHIA LLC Brine 0 365
2010 ATLAS NOBLE LLC Brine 0 365
2011 CHEVRON APPALACHIA LLC Brine 0 365
2012 ATLAS NOBLE LLC Brine 0 0
2013 ATLAS NOBLE LLC Brine 0 0
2014 ATLAS NOBLE LLC Brine 75 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1765152116 2015-7-9 0:00:0 FR No Violations 2.00
-1904175785 2014-3-11 0:00: PB No Violations 7.00
1394550382 2014-03-10 Plug / Plug Back No Violations Arrive totday to begin plugging well to surface. NicksWell Plugging is on site with all of the equipment needed to plug the well. I found that they are at the break over point with time to begin plugging. Before they begin they want to be able to pull tubing out after setting the bottom plug. The job was later schduled for Tuesday at 8:00 am
1394632016 2014-03-12 Plug / Plug Back No Violations Arrive to plug the well and did not find any vehicles parked as they have been before. Both dozers are parked out front at the entrance and nobody has answered the phone. Wait to make sure they are plugging today because it is almost 1 mile off the road and it has been raining all night. Set # 2 plug and # 3 plug thru tubing and now they need to pull all of the tubing out so they can go in to rip casing. Inspector Grimm is to cover the remaining 2 plugs to surface.
1765152116 2015-07-09 Final Restoration No Violations Location has met 1509.072B requirements.
1904175785 2014-03-11 Plug / Plug Back No Violations Nicks Well Plugging has 2-3/8 inch diameter tubing set at 5450 ft and will set the bottom plug with 25 sks of class A cement. After the bottom plug is set they will pull up to 4717 ft and shoot off the tubing. Next they will shoot 15 holes in the 4-1/2 inch diameter casing and pull up to 3900 ft and shoot the 4-1/2 inch casing again. Then run tubing bask to 4717 ft and set # 2 plug and up to set # 3 plug before pulling all of the tubing out. Then go in and rip 4-1/2 casing and lay it all down run back to plug thru 2-3/8 tubing to surface. After shooting the tubing off Appalachian Well Service could not get back down the tubing to shoot the 4-1/2 inch casing. Nicks Well Service had to pull all of the tubing out and clear it, then run back in to shoot. They did get all of the shots in place and now the job is scheduled for Weds. @ 7:30 to start plugging.

For data sources see[9]

References