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Well ID: 34-067-20837 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Washington Township | |
Operator Name: D & D ENERGY COMPANY | |
Well Pad ID: | |
Farm/Lease Name: OVERHOLT D | |
License Status: Producing | |
License Date: 1987-12-24 | |
Spud Date: 1988-01-05 | |
Spud Drilling Contractor: SHERMAN DRLG | |
Final Drill Date: 1988-01-11 | |
Well Total Depth: 5557.00 ft | |
Configuration: Vertical | |
Latitude: 40.280000 | |
Longitude: -81.320000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1987-12-24 | 182 BELDEN & BLAKE CO GeoDate 12/24/87 |
Oil and Gas | 1987-12-24 | Issued Date 12/24/87 Expired Date 12/23/88 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05557 Proposed Drill Depth 05557 |
Original Spud | 1988-01-05 | |
Completed | 1988-01-11 | |
Reached Total Depth | 1988-01-11 | |
Completion Report Received | 1988-04-05 | |
Construction Permit Expires | 1988-12-23 | |
Change of Owner | 2002-08-06 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC |
Change of Owner | 2005-07-08 | Operator changed from 1966, PETROX, INC to 5660, S & S ENERGY CORPORATION |
Change of Owner | 2015-06-02 | Operator changed from 5660, S & S ENERGY CORPORATION to 5569, D & D ENERGY COMPANY |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5376 | 5449 | 32 |
5376 | 5449 | 32 | |
5376 | 5449 | 32 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 93700 Gal | 80000 | FRAC: H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | BELDEN & BLAKE CORPORATION | 637.00 | 65.00 | 116 |
1991 | BELDEN & BLAKE CORPORATION | 2232.00 | 154.00 | 365 |
1992 | BELDEN & BLAKE CORPORATION | 1760.00 | 35.00 | 335 |
1993 | BELDEN & BLAKE CORPORATION | 1462.00 | 75.00 | 351 |
1994 | BELDEN & BLAKE CORPORATION | 1197.00 | 68.00 | 337 |
1995 | BELDEN & BLAKE CORPORATION | 743.00 | 0.00 | 358 |
1996 | BELDEN & BLAKE CORPORATION | 1293.00 | 83.00 | 360 |
1997 | BELDEN & BLAKE CORPORATION | 980.00 | 0.00 | 252 |
1998 | BELDEN & BLAKE CORPORATION | 729.00 | 69.00 | 246 |
1999 | BELDEN & BLAKE CORPORATION | 250.00 | 0.00 | 83 |
2000 | BELDEN & BLAKE CORPORATION | 676.00 | 53.00 | 180 |
2001 | BELDEN & BLAKE CORPORATION | 738.00 | 59.00 | 307 |
2002 | PETROX, INC | 736.00 | 66.00 | 56 |
2003 | PETROX, INC | 516.00 | 57.00 | 365 |
2004 | PETROX, INC | 380.00 | 60.00 | 365 |
2005 | PETROX, INC | 262.00 | 80.00 | 180 |
2006 | S & S ENERGY CORP | 406.00 | 0.00 | 365 |
2007 | S & S ENERGY CORP | 574.00 | 0.00 | 365 |
2008 | S & S ENERGY CORP | 509.00 | 69.00 | 365 |
2009 | S & S ENERGY CORP | 672.00 | 0.00 | 365 |
2010 | S & S ENERGY CORP | 0.00 | 45.00 | 365 |
2011 | S & S ENERGY CORP | 109.00 | 0.00 | 365 |
2012 | S & S ENERGY CORP | 1182.00 | 0.00 | 366 |
2013 | S & S ENERGY CORP | 245.00 | 0.00 | 365 |
2014 | S & S ENERGY CORP | 123.00 | 0.00 | 365 |
2015 | D & D ENERGY COMPANY | 4.00 | 0.00 | 365 |
2016 | D & D ENERGY COMPANY | 4.00 | 0.00 | 365 |
2017 | D & D ENERGY COMPANY | 0.00 | 27.00 | 365 |
2018 | D & D ENERGY COMPANY | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000004068 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 2/25/93 INSPECTOR MIKE KAVAGE DATE 02/2519/93 DATA FROM OLD VAX INFO | |
1465392306 | 2016-05-23 | Production Wells | No Violations | Diddy Well Service has removed the 110 bbl. Production tank from inside the dike and was suppose to have removed the oil and brine saturated soil weeks ago. I contacted Bob Diddy and he said he was aware that it needs done and that it should be done within the next few days. I also spoke with Inspector Zollars to inform him that the violation was not corrected. |
4068 | PL | No Violations |
For data sources see[9]