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34-067-21117

Well Details

Well ID: 34-067-21117
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Country: United States
State: Ohio
County: Harrison
Municipality: Washington Township
Operator Name: GULFPORT APPALACHIA LLC
Well Pad ID: US-OH-000512
Farm/Lease Name: LYON
License Status: Producing
License Date: 2012-12-14
Spud Date: 2012-11-29
Spud Drilling Contractor: UNION DRLG
Final Drill Date: 2013-01-09
Well Total Depth: 14441.00 ft
Configuration: Horizontal
Latitude: 40.240000
Longitude: -81.300000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2012-11-23 Proposed Formations:POINT PLEASANT, Issued Date:11/23/2012, Expired Date:11/23/2014 12:00:00 PM, Drilling unit acres:415.749, Proposed Well Type:OG, Proposed Well Class:EDPW
APP 2012-12-14 Proposed Formations:POINT PLEASANT, Issued Date:12/14/2012, Expired Date:12/14/2014 12:00:00 PM, Drilling unit acres:415.749, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2013-01-09
Correction to Well 2013-03-22 CORRECTION TO TARGET INFORMATION: FOOTAGE & X,Y COORDINATES FROM AS DRILLED SURVEY PLAT. UNIT SIZE CHANGED TO 422.877 ACRES.
Completion Report Received 2013-11-06
Correction to Well 2013-11-29 CHANGE IN TAKE-POINT COORDINATES FROM AS DRILLED SURVEY PLAT.
Construction Permit Expires 2014-12-14
Record Last Modified 2017-10-24

For data sources see[2]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 01/25/2013 02/22/2013 7481 6,906,270.0 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 Clean Gel Stingray Guar Gel heavy aliphatic NA 35 0.0692 0
Solvent naphtha, (petroleum) 64742-96-7 65 0.12851 0
RAPID BIOCONTROL 265 Rapid Energy Microbiocide Ethanol 64-17-5 4 0.00133 0
Alkyl dimethyl benzyl ammonium chloride 68424-85-1 5.5 0.00183 0
Didecyl dimethyl ammonium chloride 7173-51-5 8 0.00266 0
Glutaraldehyde 111-30-8 27 0.00898 0
Water 7732-18-5 60 0.01995 0
IC 116 Chem Rock Organic Acid Liquid Citric Acid 77-92-9 60 0.33646 0
Water 7732-18-5 50 0.28039 0
Per Break Stingray Breaker Ammonium Persulfate 7727-54-0 99 0.0162 0
30/50 White Minerva/Cadiz Proppant Sand 14808-60-7 100 0.37151 0
CI-360 Chem Rock Corossion Inhibitor 2-Butoxyethanol 111-76-2 10 0.00008000 0
Nonylphenol 15 mole ethoxylate 9016-45-9 5 0.00004000 0
Cinnamaldehyde 104-55-2 10 0.00008000 0
Triethyl Phosphate 78-40-0 2.5 0.00002000 0
Quinoline 91-22-5 2 0.00002000 0
Ethylene glycol 107-21-1 40 0.00031 0
C8-C10 Alcohol 85566-12-7 10 0.00008000 0
Isoquinoline 119-65-3 10 0.00008000 0
Tar Bases, quinoline derivs 72480-70-7 10 0.00008000 0
N, N-Dimethyl Formamide 68-12-2 20 0.00015 0
Water 7732-18-5 25 0.00019 0
2-Methyl Quinoline 91-63-4 5 0.00004000 0
Proprietary polycarboxylic acid mixture NA 60 0.00046 0
IC-250 Stingray Corrosion Inhibitor Water 7732-18-5 80 0.00312 0
Proprietary polycarboxylic acid mixture NA 20 0.00078 0
40/70 White Minerva/Cadiz Proppant Sand 14808-60-7 100 0 0
OB-2 Stingray Breaker Silica, Crystalline-Quartz 14808-60-7 10 0.00168 0
Ammonium persulfate 7727-54-0 75 0.0126 0
Cured acrylic resin NA 16 0.00269 0
Fresh water Stingray Carrier Water 7732-18-5 100 97.4648 0
SC 460 CHEM ROCK Scale Inhibitor Phosphonate, Amine Salt NA 28 0.00275 0
Water 7732-18-5 75 0.00735 0
FR 1214 Chem Rock Friction Reducer Water 7732-18-5 75 0.05371 0
Distillates(petroleum), hydrotreated light 64742-47-8 25 0.0179 0
SURF 601 Chem Rock Non-Emulsifier Water 7732-18-5 62 0.03314 0
Alcohols C9-C11 (ethoxylated) 68439-48-3 43 0.02299 0
X-Linker Stingray Guar Gel Ethylene Glycol NA 30 0.01888 0
Water 7732-18-5 70 0.04406 0
100 mesh Minerva/Cadiz Proppant Sand 14808-60-7 100 1.07489 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2013-02-06 H2O 28 323778 Gal 517461 STINGRAY PRESSURE PUMPING LLC STAGE 5, 36 SHOTS
2013-02-07 H2O 28 318864 Gal 517700 STINGRAY PRESSURE PUMPING LLC STAGE 7, 36 SHOTS
2013-02-10 H2O 28 179088 Gal 267740 STINGRAY PRESSURE PUMPING LLC STAGE 15, 36 SHOTS
2013-02-19 H2O 28 232302 Gal 47100 STINGRAY PRESSURE PUMPING LLC STAGE 20, 36 SHOTS
2013-02-09 H2O 28 317226 Gal 517690 STINGRAY PRESSURE PUMPING LLC STAGE 12, 36 SHOTS
2013-02-10 H2O 28 474264 Gal 499823 STINGRAY PRESSURE PUMPING LLC STAGE 14, 36 SHOTS
2013-02-08 H2O 28 221256 Gal 99000 STINGRAY PRESSURE PUMPING LLC STAGE 10, 36 SHOTS
2013-02-09 H2O 28 275142 Gal 269930 STINGRAY PRESSURE PUMPING LLC STAGE 11, 36 SHOTS
2013-02-06 H2O 28 295512 Gal 537250 STINGRAY PRESSURE PUMPING LLC STAGE 6, 36 SHOTS
2013-02-22 H2O 28 276822 Gal 523780 STINGRAY PRESSURE PUMPING LLC STAGE 25, 36 SHOTS
2013-02-20 H2O 28 269850 Gal 447870 STINGRAY PRESSURE PUMPING LLC STAGE 22, 36 SHOTS
2013-02-11 H2O 28 452802 Gal 69130 STINGRAY PRESSURE PUMPING LLC STAGE 16, 36 SHOTS
2013-02-03 H2O 28 21756 Gal 650 STINGRAY PRESSURE PUMPING LLC STAGE 3, 36 SHOTS
2013-02-19 H2O 28 284844 Gal 553500 STINGRAY PRESSURE PUMPING LLC STAGE 19, 36 SHOTS
2013-02-02 H2O 28 299376 Gal 2900 STINGRAY PRESSURE PUMPING LLC STAGE 1, 36 SHOTS
H2O 28 255108 Gal 531250 STINGRAY PRESSURE PUMPING LLC STAGE 23, 36 SHOTS
2013-02-08 H2O 28 325542 Gal 529980 STINGRAY PRESSURE PUMPING LLC STAGE 9, 36 SHOTS
2013-02-20 H2O 28 287952 Gal 551000 STINGRAY PRESSURE PUMPING LLC STAGE 21, 36 SHOTS
2013-02-07 H2O 28 312228 Gal 522129 STINGRAY PRESSURE PUMPING LLC STAGE 8, 36 SHOTS
2013-02-12 H2O 28 243390 Gal 512840 STINGRAY PRESSURE PUMPING LLC STAGE 17, 36 SHOTS
2013-02-18 H2O 28 285222 Gal 361490 STINGRAY PRESSURE PUMPING LLC STAGE 18, 36 SHOTS
2013-01-27 H2O 28 290682 Gal 394600 STINGRAY PRESSURE PUMPING LLC STAGE 1, 36 SHOTS
2013-02-09 H2O 28 251538 Gal 545400 STINGRAY PRESSURE PUMPING LLC STAGE 13, 36 SHOTS
2013-02-21 H2O 28 228942 Gal 609960 STINGRAY PRESSURE PUMPING LLC STAGE 24, 36 SHOTS
2013-02-04 H2O 28 172284 Gal 650 STINGRAY PRESSURE PUMPING LLC STAGE 4, 36 SHOTS

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2013 GULFPORT ENERGY CORPORATION 103882 16190 139
2014 GULFPORT ENERGY CORPORATION 40277 8160 249
2015 GULFPORT ENERGY CORPORATION 34305 3400 92
2016 GULFPORT ENERGY CORPORATION 45512 6422 302
2017 GULFPORT ENERGY CORPORATION 43170 5344 343
2018 GULFPORT ENERGY CORPORATION 48031 5291 358
2019 GULFPORT ENERGY CORPORATION 9663 1017 87

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2013 GULFPORT ENERGY CORPORATION Brine 24364 139
2014 GULFPORT ENERGY CORPORATION Brine 2406 249
2015 GULFPORT ENERGY CORPORATION Brine 1013 92
2016 GULFPORT ENERGY CORPORATION Brine 1945 302
2017 GULFPORT ENERGY CORPORATION Brine 1256 343
2018 GULFPORT ENERGY CORPORATION Brine 1260 358
2019 GULFPORT ENERGY CORPORATION Brine 225 87

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-130396781 2013-10-22 0:00 PW No Violations 1.00
-1623425349 2014-6-11 0:00: PW No Violations 2.50
-693251413 2018-3-19 0:00: PW No Violations 1.00
0130396781 2013-10-22 Production Wells No Violations I am on site today to check on the operation status of the well. I found that it was in production and did not find any violations on this site at this time.
0693251413 2018-03-19 Production Wells No Violations On the day of my inpection I found the Lyon pad to have 3 properly labeled and producing plunger lift wells. This well has 200 psi on the surface casing and no pressure on the intermediate casing. Production equipment includes four 400 barrel steel tanks and one 50 barrel steel tank, all are contained in a steel dike. Three sand seperators, a heater treater, and a combustor are also onsite.
1002288525 2017-09-05 Production Wells No Violations On the day of my inpection I found the Lyon pad to have 3 properly labeled producing wells. This well has 300 psi on the surface casing and no pressure on the intermediate casing. Production equipment includes four 400 barrel steel tanks, two are produced water and two arecondensate and one 50 barrel steel tank, all are contained in a steel dike. Three vertical seperators, a heater treater, and a combustor are also onsite.
1355240011 2012-12-05 Drill / Deepen / Reopen No Violations Arrived on location for intermediate string #1 cement job. Got cement returns to surface.
1355242334 2012-11-29 Drill / Deepen / Reopen No Violations Arrived on location for cementing of conductor pipe, cement did not circulate so well was grouted with 18 yards from a ready mix truck which we got cement to surface.
1355244938 2012-12-02 Drill / Deepen / Reopen No Violations Arrived on location for surface job, got cement returns to surface.
1397523054 2014-04-14 Production Wells No Violations I am on site today with David Lee of Gulfport Energy along with Randy Akins from ODNR. We are responding to a complaint from Stephanie Rohal. She said that this production facility is generating tremors and that they increase during the night as more equipment is operated. My inspection did not reveal any tremors or loud sounds. I was able to talk on my cell phone from any point near the equipment. I called Stephanie to clarify her complaint and she did not return my call. I contacted Bob Worstall and ask for seismic records for that time period during the night. I was advised that records for seismic events did not reveal any activity for that time period.
1402340659 2014-06-09 Production Wells Violations Noted I received a call today from Chris Anderson to inform me that a spill had occurred on the Lyons Pad. He said that there had been a line which broke on the compressor station and blew condensate and light crude over an area 150ft x 150ft. When I arrived on site I did find that crude and condensate had been spilled on the site. I reviewed the site with Chris and ask what type of equipment was called to cleanup the spill. Then a berm was established to act as a barrier to any fluid exiting the site. There was a ditch cut and filled with peatsorb and in front was to be an absorbent boom along the entire length. That same thing was repeated near the back side of the production tanks and compressors to make a two sided containment. The area is to be vacuumed free of fluid and then pressure washed into a sump at the low point of the pad in front of the line heaters. Containment is also being set up to hold the rock and soil removed before a roll off container can be dropped off. All of the excavated rock and soil is to be removed to a landfill.
1402492898 2014-06-10 Production Wells No Violations I arrived on site today to find the cleanup of the contaminated soil and rock from a spill 06/09/2014 continuing. 50 % of the contaminated soil and rock has been removed. I collected photos to show the progress. All of the free fluid has been removed and containment is in place to capture any fluid before it can exit the production pad. Chris Anderson is on site and advised me that they worked through the night to make sure containment is in place and to remove as much contamination as possible before a rain event. He has vacuum trucks on site to deal with any rain and has duck pond containment set up to store excavated material until it can be loaded into a dump truck and removed to a landfill. Clean up is to continue through the night again until all of the contamination has been removed. The wells on the site are not in operation at this time and will remain shut in until the cleanup is complete.
1402606085 2014-06-12 Production Wells No Violations I arrived today to check on the status of the cleanup of the spill from 6/09/2014. The entire area that had contamination from the spill has been cleaned up and hauled to Kimbles Landfill .Clean material is being compacted and put back in place of the excavated material. There has been no run off of contamination from the site. During the clean up there has been no rain events to cause material to exit the site. Containment is to be left in place until after a few rain events have occurred just to make sure nothing has been missed during the cleanup. I checked the two sumps near the entrance for chlorides with a titration test strip and had no readings for the second day in a row.
1403016881 2014-06-16 Production Wells No Violations I am on site today to check on the cleanup status of the spill which occurred 06/09/2014. I found that all of the contaminated soil and rock has been removed replaced and graded. The well is back in operation and the equipment used to produce the wells on this pad are operating. I have had calls about noise and vibrations coming from this equipment but can not find any problem at this time. I was able to make a phone call 5 feet from the compressor. I did not have any trouble hearing the conversation during that call. I did check for loud noise and vibrations but did not find the levels to be in excess of normal operations. When I was 100 ft from the compressor I could not be sure that it was running.
1623425349 2014-06-11 Production Wells No Violations Check on cleanup from spill 6/09/2014 . I found that the entire area of the spill has been excavated and removed to a landfill. The area now has clean limestone rock put back in place and the area has been graded. There are two roll off containers on site which need removed and the equipment needs put back in place. The well are not in operation at this time but should be sometime today. I have collected photos today to show the progress of the cleanup.
1902217994 2013-09-25 Preliminary Restoration No Violations On the day of my inspection the site passed preliminary restoration according to 1509.072A.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1402340659 US-OH-111908 2014-06-18 Inadequate pipeline strength
1402340659 US-OH-111909 2014-06-18 Well operation causing pollution and contamination
1402340659 US-OH-111910 2014-06-18 Well insufficiently equipped to prevent escape of oil and gas

For data sources see[9]

References