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Well ID: 34-067-62285 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Short Creek Township | |
Operator Name: ORPHAN WELL PROGRAM | |
Well Pad ID: | |
Farm/Lease Name: HILLIGAS | |
License Status: Final Restoration | |
License Date: 2013-09-24 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 40.230000 | |
Longitude: -80.950000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Well Added to System | 2013-07-19 | WELL WAS ADDED TO SYSTEM ON 7/19/2013 1:33:34 PM |
APP | 2013-09-24 | Proposed Formations:BEREA, Issued Date:9/24/2013, Expired Date:9/24/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2013-09-24 | Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM |
Plugged by Orphan Well Program | 2013-10-01 | Plugged by Orphan Well Program |
Plugged/Abandoned | 2013-10-01 | Orphan Well 2013 09 011 |
Construction Permit Expires | 2015-09-24 | Orphan Well 2013 09 011 |
Record Last Modified | 2017-02-10 | Orphan Well 2013 09 011 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0707830435 | 2013-09-25 | Orphan | No Violations | Drillers total depth was 913. Tagged with the tools at 880. Loggers total depth is 821. There is only about 40 of fluid in the hole. There is only 62 of 8-5/8 casing in the hole. The 6-1/4 casing is absent. |
0932530298 | 2013-09-30 | Orphan | No Violations | On 9/28/13 the Contractor checked well pressure - 3 PSI on gauge. On 9/30/13, while I was on-site, Contractor tagged the top of cement in the well bore at 495 and water at 100 . Contractor gravity fed 2 bags of oats (for lost corculation) and 84 sacks of concrete mix into the well bore. Tagged top of cement at 395. Ordered 9 yards of 9 Sack Grout and used 8 yards of this to fill the well bore to surface. Shut in well, gas tight, overnite and will check in morning. |
1223220332 | 2013-09-25 | Orphan | No Violations
-937-2225 extension 111). This information was based on data from a core hole (C# SC4-40), which was drilled 2100 feet north of this well. Mineral Resource Inspector Todd Miller will be covering the plugging on Friday 09/27/13 | |
1353401603 | 2013-10-08 | Final Restoration | No Violations | This well was plugged on 9/30/13 and checked for gas leakage on 10/1/13 (no leakage detected).
On todays inspection I checked the site for restoration and found the area leveled and vegetation established. Final Restoration Passed and Orphan well case closed. |
1380538481 | 2013-09-27 | Plug / Plug Back | No Violations | Washed 2-3/8 tubing to old total depth of 904. Continued washing an finally broke thru and washed down to 945. Hooked up Petroset Cementing and pumped 8 bbls of gel with hulls LCM ahead and 160 sacks of Class A cement and displaced to 400. Shut down for 1.5 hours. (a total of 3 hrs. before the 2nd plug was pumped) Tagged cement at 703 (wireline). The fluid level was ~ 100. Pumped 220 sacks of Class A cement with hulls LCM in the front end and displaced to 130. Pulled the tubing. The fluid level was ~ 60. The well started making gas immediately. The well was shut in. |
1382108092 | 2013-10-01 | Orphan | No Violations | On my inspection today I checked the well for gas leakage with my Sperian Gas Meter. No gas was detected. There was water on top of the cement, inside the well casing. No gas bubbles were visually detected. I will check site in 7 - 10 days for restoration progress. |
1737924655 | 2015-12-29 | Final Restoration | No Violations | Collecting photographic evidence of final restoration. Final restoration is approved. |
707830435 | 2013-9-25 0:00: | OR | No Violations | |
932530298 | 2013-9-30 0:00: | OR | No Violations |
For data sources see[3]