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34-069-20047

Well Details

Well ID: 34-069-20047
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Country: United States
State: Ohio
County: Henry
Municipality: Richfield Township
Operator Name: OGE ENERGY LTD
Well Pad ID:
Farm/Lease Name: KIEFFER
License Status: Producing
License Date: 1975-04-21
Spud Date: 1975-05-28
Spud Drilling Contractor:
Final Drill Date: 1975-07-11
Well Total Depth: 1965.00 ft
Configuration: Vertical
Latitude: 41.320000
Longitude: -83.920000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1975-04-21 772 GRAHAM MICHAELIS CORP GeoDate 4/21/75
Oil and Gas 1975-04-21 Issued Date 4/21/75 Expired Date 4/20/76 Acres 0000000 Tool Type CT Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1975-05-28 GL=682.1
Completed 1975-07-11 GL=682.1
Reached Total Depth 1975-07-11 GL=682.1
Construction Permit Expires 1976-04-20 GL=682.1
CO 1994-03-07 4770 KIEFFER GLENN W & RUTH M GeoDate 4/21/75
Change of Owner 1999-04-15 Operator changed from 4770, KIEFFER GLENN W & RUTH M to 6136, AURORA ENERGY LTD
Change of Owner 2006-10-03 Operator changed from 6136, AURORA ENERGY LTD to 8096, OGE ENERGY LTD
Record Last Modified 2013-10-03 GL=682.1

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 180 Bbl 0 1/2# SD. PER GAL., GAUGED 114MCFG
ACID 15 750 Gal 0 MUD, WELL GAUGED 33MCFG/2 HRS, & 56MCF/72 HRS.

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 GRAHAM MICHAELIS CORP 0.00 0.00 365
1999 AURORA ENERGY LTD 2339.00 0.00 184
2000 AURORA ENERGY LTD 820.00 0.00 227
2001 AURORA ENERGY LTD 1644.00 108.00 237
2002 AURORA ENERGY LTD 103.00 10.00 12
2003 AURORA ENERGY LTD 0.00 0.00 0
2004 AURORA ENERGY LTD 0.00 0.00 0
2005 AURORA ENERGY LTD 1756.00 0.00 141
2006 AURORA ENERGY LTD 593.00 0.00 178

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 GRAHAM MICHAELIS CORP Brine 0 365
1999 AURORA ENERGY LTD Brine 160 184
2000 AURORA ENERGY LTD Brine 0 227
2001 AURORA ENERGY LTD Brine 1704 237
2002 AURORA ENERGY LTD Brine 197 12
2003 AURORA ENERGY LTD Brine 0 0
2004 AURORA ENERGY LTD Brine 0 0
2005 AURORA ENERGY LTD Brine 835 141
2006 AURORA ENERGY LTD Brine 137 178

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1309058915 2017-7-26 0:00: PW No Violations
-1452483425 2012-1-4 0:00:0 PW No Violations
-431784386 2011-8-5 0:00:0 PW No Violations
0051939172 2013-01-31 Production Wells No Violations At the time of the inspection the well was shut in and there was no gauges on the annulus or production lines. There were no signs of any leaks. The corrective action from the Compliance Notice issued in 2011 has not been completed. The inspection was done at the request of Eric Vendel from The Ohio Division of Oil and Gas.
0431784386 2011-08-05 Production Wells Violations Noted Pump jack on well with no motor. Well is shut in on annulus and tubing. No production records since 2006. I.D. on site still identifies previous owner Aurora Energy.
0473704747 2015-04-29 Production Wells No Violations At the time of the inspection. Well has pump jack installed and surface and production casing is in fair condition.
1309058915 2017-07-26 Production Wells Violations Noted This inspection is a followup inspection on NOVs issued in 2015 to plug this well. This well appears to have had no production since the previous inspection on 2015. Well is not able to produce at the present time. Pumpjack without a motor and 1000 gallon propane tank at site. No action appears to have taken place to remedy NOV from 2011. Notice of violation was for nonproduction, failure to maintain liability insurance/bond and no identification at site.
1426085156 2015-02-11 Production Wells Violations Noted At the time of the inspection the well was still shut in and has not produced since the previous inspection on 1-31-2013. The well is capable of production but no Production Records have been filed since 2006. No Hydrogen Sulfide was detected but this is a known Hydrogen Sulfide area so precaution should be taken during any service or plugging work. There has been no response from OGE Energy to previous Compliance Notice #431784386 issued on 9-8-2011. This well is hereby ordered to be plugged and the land restored by 9-11-2015.
1452483425 2012-01-04 Production Wells No Violations No change from last inspection. NOVs from last inspection on 8/5/2011 still need resolved.
1519997155 2018-01-25 Production Wells No Violations FOLLOWUP ON NOV # 43184386 DATED 8/05/2011 AND NOV # 1426085156 DATED 2/11/15 Well consist of 7 inch surface casing extending approximately 8 inches above wellhead. Annulus and tubing is shut in but gauges appears to reads 110 PSI on annulus and 140 PSI on the gauge of the 2 3/8 upset tubing. The field is under cultivation. One thousand gallon propane tank is at well site. Pumpjack is located on wellhead but does not currently have a motor or engine installed. No odor or leakage observed at well.
1584738102 2020-3-4 0:00:0 PW No Violations
473704747 2015-4-29 0:00: PW No Violations
51939172 2013-1-31 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0431784386 US-OH-124621 2011-08-15 Nonproduction; well shall be plugged or placed in temporary inactive status
0431784386 US-OH-124622 2011-08-15 Failure to register/obtain or maintain bond/insurance
0431784386 US-OH-124623 2011-08-15 Statement of annual production not filed
1309058915 US-OH-108747 2017-11-06 NONE Well shall be plugged
1426085156 US-OH-112412 2015-05-19 Well shall be plugged

For data sources see[8]

References