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34-073-21250

Well Details

Well ID: 34-073-21250
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Country: United States
State: Ohio
County: Hocking
Municipality: Green Township
Operator Name: HOCKING HILLS ENERGY AND WELL
Well Pad ID:
Farm/Lease Name: RHEINSCHELD RALPH A& BLANCHE
License Status: Producing
License Date: 1966-08-11
Spud Date: 1966-08-09
Spud Drilling Contractor:
Final Drill Date: 1966-09-14
Well Total Depth: 2743.00 ft
Configuration: Vertical
Latitude: 39.510000
Longitude: -82.370000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 566 GRIM PAUL A
Original Spud 1966-08-09 GL=719.7, DF=721.7
Completed 1966-09-14 GL=719.7, DF=721.7
Reached Total Depth 1966-09-14 GL=719.7, DF=721.7
Change of Owner 2001-10-29 Operator changed from 566, GRIM PAUL A to 5755, CHIEFTAIN ENERGY CORP.
Record Last Modified 2013-10-03 GL=719.7, DF=721.7

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2875 Bbl 450 300# BEADS

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 GRIM PAUL A 1025.00 392.00 365
1985 GRIM PAUL A 651.00 384.00 365
1986 GRIM PAUL A 375.00 317.00 365
1987 GRIM PAUL A 595.00 303.00 365
1988 GRIM PAUL A 653.00 384.00 365
1989 GRIM PAUL A 960.00 212.00 365
1990 GRIM PAUL A 756.00 304.00 365
1991 GRIM PAUL A 601.00 361.00 365
1992 GRIM PAUL A 727.00 276.00 365
1993 GRIM PAUL A 204.00 169.00 365
1994 GRIM PAUL A 0.00 146.00 365
1995 GRIM PAUL A 0.00 18.00 365
1996 GRIM PAUL A 0.00 282.00 365
1997 GRIM PAUL A 0.00 170.00 365
1998 GRIM PAUL A 0.00 45.00 365
1999 GRIM PAUL A 0.00 37.00 365
2000 GRIM PAUL A 0.00 109.00 365
2001 GRIM PAUL A 0.00 0.00 365
2002 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0
2003 HOCKING HILLS ENERGY AND WELL 517.00 151.00 365
2004 HOCKING HILLS ENERGY AND WELL 744.00 66.00 365
2005 HOCKING HILLS ENERGY AND WELL 533.00 154.00 365
2006 HOCKING HILLS ENERGY AND WELL 746.00 157.00 365
2008 HOCKING HILLS ENERGY AND WELL 156.00 292.00 365
2009 HOCKING HILLS ENERGY AND WELL 156.00 292.00 365
2010 HOCKING HILLS ENERGY AND WELL 703.00 312.00 0
2011 HOCKING HILLS ENERGY AND WELL 758.00 410.00 0
2012 HOCKING HILLS ENERGY AND WELL 619.00 338.00 366
2013 HOCKING HILLS ENERGY AND WELL 574.00 296.00 365
2014 HOCKING HILLS ENERGY AND WELL 508.00 398.00 365
2015 HOCKING HILLS ENERGY AND WELL 390.00 148.00 365
2016 HOCKING HILLS ENERGY AND WELL 799.00 344.00 365
2017 HOCKING HILLS ENERGY AND WELL 1011.00 361.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 GRIM PAUL A Brine 0 365
1985 GRIM PAUL A Brine 620 365
1986 GRIM PAUL A Brine 420 365
1987 GRIM PAUL A Brine 420 365
1988 GRIM PAUL A Brine 210 365
1989 GRIM PAUL A Brine 0 365
1990 GRIM PAUL A Brine 280 365
1991 GRIM PAUL A Brine 380 365
1992 GRIM PAUL A Brine 450 365
1993 GRIM PAUL A Brine 165 365
1994 GRIM PAUL A Brine 80 365
1995 GRIM PAUL A Brine 30 365
1996 GRIM PAUL A Brine 520 365
1997 GRIM PAUL A Brine 440 365
1998 GRIM PAUL A Brine 140 365
1999 GRIM PAUL A Brine 110 365
2000 GRIM PAUL A Brine 200 365
2001 GRIM PAUL A Brine 0 365
2002 HOCKING HILLS ENERGY AND WELL Brine 0 0
2003 HOCKING HILLS ENERGY AND WELL Brine 180 365
2004 HOCKING HILLS ENERGY AND WELL Brine 306 365
2005 HOCKING HILLS ENERGY AND WELL Brine 420 365
2006 HOCKING HILLS ENERGY AND WELL Brine 385 365
2008 HOCKING HILLS ENERGY AND WELL Brine 390 365
2009 HOCKING HILLS ENERGY AND WELL Brine 390 365
2010 HOCKING HILLS ENERGY AND WELL Brine 400 0
2011 HOCKING HILLS ENERGY AND WELL Brine 320
2012 HOCKING HILLS ENERGY AND WELL Brine 360 366
2013 HOCKING HILLS ENERGY AND WELL Brine 980 365
2014 HOCKING HILLS ENERGY AND WELL Brine 700 365
2015 HOCKING HILLS ENERGY AND WELL Brine 110 365
2016 HOCKING HILLS ENERGY AND WELL Brine 310 365
2017 HOCKING HILLS ENERGY AND WELL Brine 210 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1166953966 2004-6-22 0:00: PW No Violations
-1402863559 2004-6-8 0:00:0 PW No Violations
-1425736256 2004-7-7 0:00:0 PW No Violations
-1458468785 2014-11-19 0:00 PW No Violations 1.00
-1594781399 2004-6-10 0:00: PW No Violations
-2127126931 2004-6-23 0:00: PW No Violations
-580284449 2006-11-7 0:00: PW No Violations
0042799395 2010-09-08 Production Wells No Violations A follow-up inspection revealed that oil is now pooled on ground surface a round backside of 100 bbl tank. The tank contains a leak at bottom and will need to be addressed. Chieftain Energy notified by telephone and confirmed leak and also stating they will be replacing this tank.
0202430507 2004-05-20 Production Wells Violations Noted An inspection of the well revealed oil and oily soil around well site and along flow line, flow line leaking in dike of tank battery, dike full of brine, and kill area starting out side of dike.
0580284449 2006-11-07 Production Wells No Violations A follow-up inpsection conducted on 11/7/2006, revealed that the previously noted violations have been resolved.
0944889068 2018-08-16 Production Wells No Violations My inspection revealed the well consists of a pumping unit. The tank battery consists of 2-100 barrel tanks and a knock out tank. There is also a drip and gas sales meter with a new chart. The valves on the well were open. The well lacks a legible identification. The owner of the well shall place a legible identification per 1501:9-9-05(A)10 within 10 days.
1088691916 2004-06-30 Production Wells No Violations Follow-up on NOV, company has haul out several tons of contaminated soils and are now hauling in fresh soils.
1154311908 2006-07-21 Production Wells Violations Noted An inspection was conducted at the facility owned by Chieftain Energy Corp on 7/21/2006. During the inspection, it was noted that a fitting was leaking oil onto the ground surface.
1160765839 2006-09-01 Production Wells No Violations A follow-up inspection was conducted on 9/1/2/006. During the inspection, it was noted that the previously noted violation has not been resolved.
1166953966 2004-06-22 Production Wells No Violations Follow-up on NOV, Non-Compliance, company is working on violations.
1186750280 2007-08-06 Production Wells No Violations No violations were noted.
1197552835 2007-12-11 Production Wells No Violations No violations were noted.
1290685459 2004-07-01 Production Wells No Violations Follow-up on NOV, company still needs to haul in more dirt, grade, seed and mulch area, dike around tanks should be large enough.
1402863559 2004-06-08 Production Wells No Violations Non-compliance.
1425736256 2004-07-07 Production Wells No Violations Non-Compliance, grade work not finished , then area will need seed and mulch.
1430353216 2004-07-13 Production Wells No Violations Follow-up on NOV, In-Compliance.
1458468785 2014-11-19 Production Wells No Violations Production well inspection. The well consists of 2-100 barrel tanks and a pumping unit. The identification is faded, there is a oil and paraffin on the wellhead. I have contacted Hocking Hills Energy to have the identification redone and the wellhead cleaned.
1471838641 2010-09-22 Administrative Inspection No Violations Mr. Ron McBride called today at 8:28 a.m. regarding status of non-related well in Vinton Co. Mr. McBride was informed that 100 bbl tank is leaking and oil now exists around the outside of tank. Mr. McBride confirmed leak and that they will be replacing this tank. Further stating they found a good tank at Mr. Paul Grims shop.
1541398306 2004-06-29 Production Wells No Violations Follow-up on NOV, company cleaning up area and trying to comply with NOV.
1543587146 2018-11-30 Production Wells No Violations My inspection revealed that identification has been posted at the tank battery and well. The violation has been resolved. Time of inspection: 8:00 AM. Weather: 37 degrees F, Overcast
1557031074 2017-01-17 Production Wells No Violations Production well inspection. The well consists of a pumping unit and 2-100 barrel tanks. Legible identification was posted. No violations were noted.
1594781399 2004-06-10 Production Wells No Violations Non-compliance, met with JoeHoerst, Dave Hodges, and Doug Kitchen and his attorney to review violations at well site.
1968562205 2010-08-03 Production Wells No Violations An inspection revealed identification at the 100 bbl tank was not legible and will need to be replaced. A bare area inside the earthen dike contained an approx 3 x 5 bare area (U shaped) with salt crystals on ground surface. The source could potentially be from top of tank containing a 1.25 production line or bottom of 100 bbl tank contains a small leak. Although records indicate that the last year of reported production was 2006, the well was equipped and appears capable of production. A verbal notification was provided to Mr. Ron McBride, Chieftain Energy Contractor, in the field, on 8/18/2010, to perform cleanup and check/repair leaks, and submit production statements. A follow-up inspection will be conducted.
202430507 2004-5-20 0:00: PW No Violations
2127126931 2004-06-23 Production Wells No Violations Follow-up on NOV, Non-Compliance, company is working on violations.
2145730839 2010-10-01 Production Wells No Violations A follow-up inspection revealed that a replacement 100 bbl tank (used) has been placed at the location.
42799395 2010-9-8 0:00:0 PW No Violations
944889068 2018-8-16 0:00: PW No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0202430507 US-OH-120571 2004-05-21 Unlawful method of storage or disposal of brine or other wastes
0202430507 US-OH-120572 2004-05-21 Failure to keep SPCC dike/pit free of brine and other wastes
0202430507 US-OH-120573 2004-05-21 Unlawful use of pit for temporary storage of brine or other wastes
0202430507 US-OH-120574 2004-05-21 Well operation causing pollution and contamination
1154311908 US-OH-104028 2006-08-02 Well operation causing pollution and contamination

For data sources see[8]

References