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Well ID: 34-073-23076 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Monday Creek Township | |
Operator Name: MH OILFIELD SERVICE LLC | |
Well Pad ID: | |
Farm/Lease Name: DARRELL LUCAS | |
License Status: Plugged and Abandoned | |
License Date: 2020-02-19 | |
Spud Date: 1985-03-14 | |
Spud Drilling Contractor: ECHELBERRY DRLG | |
Final Drill Date: 1985-07-03 | |
Well Total Depth: 2780.00 ft | |
Configuration: Vertical | |
Latitude: 39.650000 | |
Longitude: -82.370000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1985-01-22 | Issued Date 1/22/85 Expired Date 7/21/85 Acres 0068700 Tool Type CT Proposed Formation CLINTON Proposed Depth 02780 Proposed Drill Depth 02780 |
Original Spud | 1985-03-14 | |
Completed | 1985-07-03 | |
Reached Total Depth | 1985-07-03 | |
CO | 1985-07-19 | 75 BARCLAY PETROLEUM INC GeoDate 1/22/85 |
Construction Permit Expires | 1985-07-21 | |
Completion Report Received | 1985-07-30 | |
Change of Owner | 2017-11-27 | Operator changed from 75, BARCLAY PETROLEUM INC to 8277, MH OILFIELD SERVICE LLC |
Record Last Modified | 2017-11-27 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 2746 | 2780 | 0 |
2746 | 2780 | 0 | |
2746 | 2780 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1900 Bbl | 1000 | FRAC;H2O,SAND | ||
GEL | 0 | 1300 Lbs | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | MARJAC ENERGY CO | 0.00 | 831.00 | 0 |
1986 | MARJAC ENERGY CO | 4026.00 | 1594.00 | 365 |
1988 | BARCLAY PETROLEUM INC | 1405.00 | 559.00 | 365 |
1989 | BARCLAY PETROLEUM INC | 5780.00 | 469.00 | 365 |
1990 | BARCLAY PETROLEUM INC | 1325.00 | 369.00 | 365 |
1991 | BARCLAY PETROLEUM INC | 2126.00 | 324.00 | 365 |
1992 | BARCLAY PETROLEUM INC | 1289.00 | 246.00 | 365 |
1993 | BARCLAY PETROLEUM INC | 1084.00 | 77.00 | 365 |
1994 | BARCLAY PETROLEUM INC | 400.00 | 153.00 | 300 |
1995 | BARCLAY PETROLEUM INC | 263.00 | 0.00 | 300 |
1996 | BARCLAY PETROLEUM INC | 380.00 | 306.00 | 366 |
1997 | BARCLAY PETROLEUM INC | 296.00 | 310.00 | 365 |
1998 | BARCLAY PETROLEUM INC | 194.00 | 80.00 | 270 |
1999 | BARCLAY PETROLEUM INC | 238.00 | 236.00 | 365 |
2000 | BARCLAY PETROLEUM INC | 237.00 | 158.00 | 365 |
2001 | BARCLAY PETROLEUM INC | 0.00 | 154.00 | 365 |
2002 | BARCLAY PETROLEUM INC | 0.00 | 151.00 | 365 |
2003 | BARCLAY PETROLEUM INC | 0.00 | 49.00 | 90 |
2004 | BARCLAY PETROLEUM INC | 0.00 | 69.00 | 365 |
2005 | BARCLAY PETROLEUM INC | 0.00 | 114.00 | 365 |
2006 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 365 |
2007 | BARCLAY PETROLEUM INC | 0.00 | 22.00 | 365 |
2008 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 180 |
2009 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 18 |
2010 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 10 |
2011 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 180 |
2012 | BARCLAY PETROLEUM INC | 0.00 | 0.00 | 60 |
2013 | BARCLAY PETROLEUM INC | 0.00 | 48.00 | 365 |
2014 | BARCLAY PETROLEUM INC | 0.00 | 77.00 | 365 |
2015 | BARCLAY PETROLEUM INC | 0.00 | 26.00 | 365 |
2016 | BARCLAY PETROLEUM INC | 0.00 | 53.00 | 365 |
2017 | MH OILFIELD SERVICE LLC | 0.00 | 0.00 | 182 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | MARJAC ENERGY CO | Brine | 1915 | 0 |
1986 | MARJAC ENERGY CO | Brine | 1540 | 365 |
1988 | BARCLAY PETROLEUM INC | Brine | 90 | 365 |
1989 | BARCLAY PETROLEUM INC | Brine | 110 | 365 |
1990 | BARCLAY PETROLEUM INC | Brine | 70 | 365 |
1991 | BARCLAY PETROLEUM INC | Brine | 20 | 365 |
1992 | BARCLAY PETROLEUM INC | Brine | 0 | 365 |
1993 | BARCLAY PETROLEUM INC | Brine | 60 | 365 |
1994 | BARCLAY PETROLEUM INC | Brine | 0 | 300 |
1995 | BARCLAY PETROLEUM INC | Brine | 0 | 300 |
1996 | BARCLAY PETROLEUM INC | Brine | 0 | 366 |
1997 | BARCLAY PETROLEUM INC | Brine | 0 | 365 |
1998 | BARCLAY PETROLEUM INC | Brine | 0 | 270 |
1999 | BARCLAY PETROLEUM INC | Brine | 140 | 365 |
2000 | BARCLAY PETROLEUM INC | Brine | 70 | 365 |
2001 | BARCLAY PETROLEUM INC | Brine | 210 | 365 |
2002 | BARCLAY PETROLEUM INC | Brine | 0 | 365 |
2003 | BARCLAY PETROLEUM INC | Brine | 140 | 90 |
2004 | BARCLAY PETROLEUM INC | Brine | 70 | 365 |
2005 | BARCLAY PETROLEUM INC | Brine | 0 | 365 |
2006 | BARCLAY PETROLEUM INC | Brine | 0 | 365 |
2007 | BARCLAY PETROLEUM INC | Brine | 140 | 365 |
2008 | BARCLAY PETROLEUM INC | Brine | 0 | 180 |
2009 | BARCLAY PETROLEUM INC | Brine | 0 | 18 |
2010 | BARCLAY PETROLEUM INC | Brine | 0 | 10 |
2011 | BARCLAY PETROLEUM INC | Brine | 0 | 180 |
2012 | BARCLAY PETROLEUM INC | Brine | 0 | 60 |
2013 | BARCLAY PETROLEUM INC | Brine | 105 | 365 |
2014 | BARCLAY PETROLEUM INC | Brine | 238 | 365 |
2015 | BARCLAY PETROLEUM INC | Brine | 129 | 365 |
2016 | BARCLAY PETROLEUM INC | Brine | 107 | 365 |
2017 | BARCLAY PETROLEUM INC | Brine | 53 | 180 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1088663096 | 2020-8-26 0:00: | PB | No Violations | 5.00 |
-1253044824 | 2017-10-25 0:00 | PW | No Violations | 0.50 |
-1318713982 | 2010-2-17 0:00: | AM | No Violations | |
-1756780772 | 2000-10-27 0:00 | PW | No Violations | |
-1836483773 | 2010-11-30 0:00 | AM | No Violations | |
-1899722304 | 2010-2-3 0:00:0 | AD | No Violations | |
-1928488124 | 2009-6-1 0:00:0 | PW | No Violations | |
-198056941 | 2020-9-1 0:00:0 | PB | No Violations | 2.50 |
-2034966943 | 2008-4-3 0:00:0 | PW | No Violations | |
-319467156 | 2010-1-5 0:00:0 | AD | No Violations | |
-323356525 | 2009-6-1 0:00:0 | PW | No Violations | |
-459217853 | 2020-8-25 0:00: | PB | No Violations | 8.00 |
-487276757 | 2008-4-21 0:00: | PW | No Violations | |
-541202719 | 2009-6-1 0:00:0 | PW | No Violations | |
-57598875 | 2009-6-1 0:00:0 | PW | No Violations | |
-786838366 | 2020-8-27 0:00: | PB | No Violations | 2.00 |
000PL16122 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
001269i153 | 2000-12-04 | Production Wells | No Violations | FOLLOW - UP on NOV , IN - COMPLIANCE . |
0057598875 | 2009-06-01 | Production Wells | No Violations | FOLLOW UP TO NOV # 582821827 A complaint was received alleging non-production, pipeline and electric line burial. An inspection revealed that the well contains a pumping unit with a motor and belts. The valve on the pumping tee was observed closed. The valve at well-head on 4.5 |
0108038748 | 2010-07-20 | Annular Disposal | No Violations | A follow-up inspection revealed non-compliance. The casing valve was observed open with steel line connected underground. The tank battery (shared) remains disconnected with no attached lines from wells on lease. No observed identification at the well. |
0319467156 | 2010-01-05 | Annular Disposal | No Violations | Received a copy of run ticket from 10/14/2009 for oil sales showing the Lucas #2 & #3 wells. A follow-up inspection revealed non-compliance. Production lines have not been connected to the common tank battery or separator. ID is now present at the tank battery. |
0323356525 | 2009-06-01 | Production Wells | No Violations | FOLLOW UP TO NOV # -541202719 FOLLOW UP TO NOV # 582821827 A complaint was received alleging non-production, pipeline and electric line burial. An inspection revealed that the well contains a pumping unit with a motor and belts. The valve on the pumping tee was observed closed. The valve at well-head on 4.5 casing was observed open with attached 2 steel line. At the tank battery location, two lines were found disconnected (Permit No. 3245 also included). No identification observed at the well (common tank battery) and has faded/not legible at tank. Approximately 30 of electric line was found above ground. At this time, the electric appears to have been turned off. Additional production equipment include two 100 bbl tanks with separator and knock-out. The separator was found approximately 10 away from tank and has been disconnected. Earthen dike at tank battery location does not contain a front wall. The landowner further states that lease requires burial below plow depth. Records indicate oil and/or gas production up to 2000. No brine reported since 1996. 0 reported production from 2001 to 2006. 22 bbl of oil reported for 2007 (common tank battery). 0 reported production of oil, gas and brine for 2008. Note: Paramount Gas has commercial sales line routed along property, but no connections were observed. Tap location near tank battery consisted of 2 black plastic routed from drip not connected and valve closed. No meter observed. Approximately 150 of the lease road has also eroded and will need to be graded. |
0396782731 | 2008-03-13 | Production Wells | Violations Noted | An inspection revealed that two of the four 100 bbl tanks (saltwater & oil) are corroded and leaking at the bottom. Oil and brine was observed around the tank battery location. This well does not contain a dike. As a result, contamination and pollution has washed over the hill onto the lease road. An SPCC dike will be required for the tank battery, in order to prevent future occurence. No contamination or pollution was observed off-site. Also noted was that the lease road will need to be graded and identification provided at the well and tank battery (common tank battery). The company was working at the time of the inspection. The owner, Mr. Bruce Kelly, was contacted by telephone on 3/13/2008 and informed of the inspection results and requirements. Mr. Kelly was questioned about production records for this well. He states that this well provides house gas. |
0487276757 | 2008-04-21 | Production Wells | No Violations | A follow-up inspection revealed compliance. |
0541202719 | 2009-06-01 | Production Wells | No Violations | FOLLOW UP TO NOV # 582821827 A complaint was received alleging non-production, pipeline and electric line burial. An inspection revealed that the well contains a pumping unit with a motor and belts. The valve on the pumping tee was observed closed. The valve at well-head on 4.5 casing was observed open with attached 2 steel line. At the tank battery location, two lines were found disconnected (Permit No. 3245 also included). No identification observed at the well (common tank battery) and has faded/not legible at tank. Approximately 30 of electric line was found above ground. At this time, the electric appears to have been turned off. Additional production equipment include two 100 bbl tanks with separator and knock-out. The separator was found approximately 10 away from tank and has been disconnected. Earthen dike at tank battery location does not contain a front wall. The landowner further states that lease requires burial below plow depth. Records indicate oil and/or gas production up to 2000. No brine reported since 1996. 0 reported production from 2001 to 2006. 22 bbl of oil reported for 2007 (common tank battery). 0 reported production of oil, gas and brine for 2008. Note: Paramount Gas has commercial sales line routed along property, but no connections were observed. Tap location near tank battery consisted of 2 black plastic routed from drip not connected and valve closed. No meter observed. Approximately 150 of the lease road has also eroded and will need to be graded. |
0562717226 | 2004-05-20 | Annular Disposal | No Violations | No violations. |
0582821827 | 2009-06-01 | Production Wells | Violations Noted | A complaint was received alleging non-production, pipeline and electric line burial. An inspection revealed that the well contains a pumping unit with a motor and belts. The valve on the pumping tee was observed closed. The valve at well-head on 4.5 casing was observed open with attached 2 steel line. At the tank battery location, two lines were found disconnected (Permit No. 3245 also included). No identification observed at the well (common tank battery) and has faded/not legible at tank. Approximately 30 of electric line was found above ground. At this time, the electric appears to have been turned off. Additional production equipment include two 100 bbl tanks with separator and knock-out. The separator was found approximately 10 away from tank and has been disconnected. Earthen dike at tank battery location does not contain a front wall. The landowner further states that lease requires burial below plow depth. Records indicate oil and/or gas production up to 2000. No brine reported since 1996. 0 reported production from 2001 to 2006. 22 bbl of oil reported for 2007 (common tank battery). 0 reported production of oil, gas and brine for 2008. Note: Paramount Gas has commercial sales line routed along property, but no connections were observed. Tap location near tank battery consisted of 2 black plastic routed from drip not connected and valve closed. No meter observed. Approximately 150 of the lease road has also eroded and will need to be graded. |
0687788210 | 2012-12-28 | Production Wells | No Violations | Attempts to gain compliance have been made. Flow line has been laid to the tank battery, but has not been connected. Well is equipped for production complete with pumping unit. Well supplies house gas. Spoke with Bruce Kelley in person about this well, and he stated that within the next couple of months, he will have the wells back in compliance. He had also serviced this well. |
0767431459 | 2016-10-05 | Production Wells | No Violations | Compliance notice follow-up. The well head has been cleaned of oil. This satisfies the compliance notice. |
0890785264 | 2016-09-28 | Production Wells | No Violations | Production well inspection. The well consists of a pumping unit and shares a common tank battery with 3407323245 and 3407323246. This well was serviced on 9-26-16. The is a small amount of paraffin left on the well head. The well is capable of production. The polish rod is shiny and the is no rust on the pulley. The well is being used for domestic gas use. I have contacted well owner Bruce Kelly regarding the paraffin that needs cleaned up. I instructed Mr. Kelly he had 5 working days to have the paraffin removed. I will re-inspect on 10-5-16 to determine if the well is in compliance. |
0999377450 | 2009-09-29 | Production Wells | No Violations | A follow-up inspection revealed non-compliance. |
1010413237 | 2017-05-04 | Production Wells | No Violations | Compliance notice follow-up. The well is in compliance, this satisfies the compliance notice. |
108038748 | 2010-7-20 0:00: | AD | No Violations | |
1121635906 | 2010-11-16 | Production Wells | No Violations | A follow-up inspection with Dan Goins, Mineral Resource Inspector III, revealed non-compliance. |
1253044824 | 2017-10-25 | Production Wells | No Violations | This inspection was conducted in regards to a phone call placed to the Incident Notification One-Call System. The caller reported that the company was not taking care of the wells on her property. The well owner Mr. Justin Kelly was at the tank battery when I arrived. The well was equipped with a pumping unit and motor. This well produces into a shared tank battery with API#3245 and API#3246. The tank battery consists of (2) 100 barrel tanks, (1) knockout tank, and separator inside an earthen dike. Identification was observed at the well and tank battery. There were no pollution or contamination issues. No violations were observed. Time of inspection: 3:00 PM. |
1269i11350 | 2000-10-27 | Production Wells | No Violations | An inspection of well site revealed No I.D. at the well and well produces into a common tank battery. |
1269i11350545 | 2000-10-27 0:00 | PW | No Violations | |
1269i153 | 2000-12-4 0:00: | PW | No Violations | |
1318713982 | 2010-02-17 | Administrative Inspection | No Violations | Called Mr. Bruce Kelly today at 9:11am in regards to NOVs that had been issued on the Lucas well(s). Mr. Kelly was instructed to continue working on placing the two wells back into production and provide identification. Mr. Kelly agreed and also stated that they plan to move the tanks back further and re-dike. Mr. Kelly states that the new line, in the field, would be buried when the weather breaks. |
1401584889 | 2009-06-01 | Production Wells | No Violations | FOLLOW UP TO NOV # -57598875 FOLLOW UP TO NOV # 582821827 A complaint was received alleging non-production, pipeline and electric line burial. An inspection revealed that the well contains a pumping unit with a motor and belts. The valve on the pumping tee was observed closed. The valve at well-head on 4.5 |
1496799950 | 2013-04-23 | Production Wells | No Violations | Production well inspection, this well consists of a pumping unit and 2-100 barrel tanks. This well provides house gas, no violations noted. |
1579812635 | 2020-1-23 0:00: | PW | No Violations | 1.00 |
1598280135 | 2020-8-24 0:00: | PB | No Violations | 8.00 |
1598964122 | 2020-8-31 0:00: | PB | No Violations | 8.00 |
1599050805 | 2020-9-2 0:00:0 | PB | No Violations | |
1599743633 | 2020-9-10 0:00: | PB | No Violations | |
1602165899 | 2020-10-7 0:00: | FR | No Violations | 0.60 |
1756780772 | 2000-10-27 | Production Wells | No Violations | FOLLOW UP TO NOV # 1269i113 An inspection of well site revealed No I.D. at the well and well produces into a common tank battery. |
1836483773 | 2010-11-30 | Administrative Inspection | No Violations | The well owner, Mr. Bruce Kelly, was contacted today by telephone at 5:06 pm regarding non-compliance with Notice of Violations issued on Lucas wells. Mr. Kelly was instructed to provide identification at the common tank battery and at all three (3) Lucas wells; advised that no dike wall exists for the front of tank battery; two out of three wells are idle, and credit for production (house gas) would be granted for well closest to landowner house (P#3245). Mr. Kelly requests additional time for compliance. Asked how much time he would need, Mr. Kelly replied by stating Spring 2011. Mr. Kelly was advised that request would be discussed with Mr. Robert Stonerock, South Region Oil and Gas Supervisor. |
1855422490 | 2009-07-22 | Production Wells | No Violations | A follow-up inspection revealed that a new earthen dike has been constructed for the tank battery. Called Mr. Bruce Kelly at 9:15am. He states that they will probably paint the tanks and before installing new identification. Asked if service rig would be needed, he states that they would just have to hook up wells. Currently, all three wells are not connected to tanks. One of which produces house gas. This work will be done within next week along with seed and straw for the dike. |
1899722304 | 2010-02-03 | Annular Disposal | No Violations | A follow-up inspection revealed non-compliance. A new black plastic line with a valve has been placed at the well, but not connected. |
1928488124 | 2009-06-01 | Production Wells | No Violations | FOLLOW UP TO NOV # 582821827 A complaint was received alleging non-production, pipeline and electric line burial. An inspection revealed that the well contains a pumping unit with a motor and belts. The valve on the pumping tee was observed closed. The valve at well-head on 4.5 casing was observed open with attached 2 steel line. At the tank battery location, two lines were found disconnected (Permit No. 3245 also included). No identification observed at the well (common tank battery) and has faded/not legible at tank. Approximately 30 of electric line was found above ground. At this time, the electric appears to have been turned off. Additional production equipment include two 100 bbl tanks with separator and knock-out. The separator was found approximately 10 away from tank and has been disconnected. Earthen dike at tank battery location does not contain a front wall. The landowner further states that lease requires burial below plow depth. Records indicate oil and/or gas production up to 2000. No brine reported since 1996. 0 reported production from 2001 to 2006. 22 bbl of oil reported for 2007 (common tank battery). 0 reported production of oil, gas and brine for 2008. Note: Paramount Gas has commercial sales line routed along property, but no connections were observed. Tap location near tank battery consisted of 2 black plastic routed from drip not connected and valve closed. No meter observed. Approximately 150 of the lease road has also eroded and will need to be graded. |
2034966943 | 2008-04-03 | Production Wells | No Violations | A follow-up inspection revealed that all C&P has been removed and taken to the landfill. Both 100bbl tanks have been removed. Run tickets received. 50.44 tons of soil was removed. |
396782731 | 2008-3-13 0:00: | PW | No Violations | |
562717226 | 2004-5-20 0:00: | AD | No Violations | |
582821827 | 2009-6-1 0:00:0 | PW | No Violations | |
687788210 | 2012-12-28 0:00 | PW | No Violations | 1.00 |
767431459 | 2016-10-5 0:00: | PW | No Violations | 0.50 |
890785264 | 2016-9-28 0:00: | PW | No Violations | 1.50 |
999377450 | 2009-9-29 0:00: | PW | No Violations | |
PL16122 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0396782731 | US-OH-124218 | 2008-03-31 | Failure to restore land surface within 6 months (CHANGE) | |
0396782731 | US-OH-124219 | 2008-03-31 | Well operation causing pollution and contamination | |
0396782731 | US-OH-124220 | 2008-03-31 | Failure to legibly identify well | |
0396782731 | US-OH-124221 | 2008-03-31 | Equipment pressure rated below operating pressure | |
0396782731 | US-OH-124222 | 2008-03-31 | No SPCC dike/or failure to keep dike free of water or oil | |
0582821827 | US-OH-126539 | 2009-06-17 | Well operation causing pollution and contamination | |
0582821827 | US-OH-126540 | 2009-06-22 | General Safety | |
0582821827 | US-OH-126541 | 2009-06-17 | Failure to legibly identify well | |
0582821827 | US-OH-126542 | 2009-06-22 | No SPCC dike/or failure to keep dike free of water or oil | |
0582821827 | US-OH-126543 | 2009-06-22 | Well shall be plugged |
For data sources see[9]