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| Well ID: 34-073-23169 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Hocking | |
| Municipality: Starr Township | |
| Operator Name: KILBARGER INVESTMENTS INC | |
| Well Pad ID: | |
| Farm/Lease Name: LOGAN SAND & GRAVEL | |
| License Status: Producing | |
| License Date: 1986-03-20 | |
| Spud Date: 1986-06-02 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1986-06-05 | |
| Well Total Depth: 3288.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.410000 | |
| Longitude: -82.350000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1986-03-20 | Issued Date 3/20/86 Expired Date 3/20/87 Acres 0060000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 03288 Proposed Drill Depth 03288 |
| Original Spud | 1986-06-02 | |
| Completed | 1986-06-05 | |
| Reached Total Depth | 1986-06-05 | |
| CO | 1986-07-11 | 133 QUAKER STATE OIL REF CORP GeoDate 3/20/86 |
| Completion Report Received | 1986-07-25 | |
| Construction Permit Expires | 1987-03-20 | |
| CO | 1995-04-12 | 4243 NUTTCO OIL & GAS GeoDate 3/20/86 |
| Change of Owner | 2004-02-12 | Operator changed from 4243, NUTTCO OIL & GAS to 7589, HOUSTON OIL |
| Change of Owner | 2004-04-12 | Operator changed from 7589, HOUSTON OIL to 1675, KILBARGER INVESTMENTS INC |
| Last Compliance Report | 2015-12-11 | |
| Record Last Modified | 2017-02-15 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2006-09-11 | 3152 | 3170 | 19 |
| 3152 | 3170 | 19 | |
| 3152 | 3170 | 19 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| N2 | 0 | 252 Mscf | 0 | |||
| H2O | 0 | 2624 Bbl | 44000 |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1986 | QUAKER STATE OIL REF CORP | 0.00 | 793.00 | 365 |
| 1987 | QUAKER STATE OIL REF CORP | 1859.00 | 1054.00 | 365 |
| 1988 | QUAKER STATE OIL REF CORP | 2776.00 | 563.00 | 365 |
| 1989 | QUAKER STATE OIL REF CORP | 1559.00 | 349.00 | 365 |
| 1990 | QUAKER STATE OIL REF CORP | 959.00 | 249.00 | 365 |
| 1991 | QUAKER STATE OIL REF CORP | 1000.00 | 239.00 | 365 |
| 1992 | QUAKER STATE OIL REF CORP | 969.00 | 199.00 | 365 |
| 1993 | QUAKER STATE OIL REF CORP | 193.00 | 174.00 | 365 |
| 1994 | QUAKER STATE OIL REF CORP | 248.00 | 138.00 | 365 |
| 1995 | NUTTCO OIL & GAS | 1000.00 | 1.00 | 156 |
| 1996 | NUTTCO OIL & GAS | 0.00 | 1.00 | 180 |
| 2002 | NUTTCO OIL & GAS | 0.00 | 160.00 | 100 |
| 2004 | KILBARGER INVESTMENTS INC | 0.00 | 0.00 | 267 |
| 2005 | KILBARGER INVESTMENTS INC | 0.00 | 69.00 | 267 |
| 2006 | KILBARGER INVESTMENTS INC | 0.00 | 53.00 | 365 |
| 2007 | KILBARGER INVESTMENTS INC | 0.00 | 58.00 | 365 |
| 2008 | KILBARGER INVESTMENTS INC | 0.00 | 71.00 | 119 |
| 2009 | KILBARGER INVESTMENTS INC | 0.00 | 65.00 | 365 |
| 2010 | KILBARGER INVESTMENTS INC | 0.00 | 64.00 | 365 |
| 2011 | KILBARGER INVESTMENTS INC | 0.00 | 70.00 | 365 |
| 2012 | KILBARGER INVESTMENTS INC | 0.00 | 0.00 | 366 |
| 2013 | KILBARGER INVESTMENTS INC | 0.00 | 66.00 | 365 |
| 2014 | KILBARGER INVESTMENTS INC | 0.00 | 95.00 | 365 |
| 2015 | KILBARGER INVESTMENTS INC | 0.00 | 37.00 | 365 |
| 2016 | KILBARGER INVESTMENTS INC | 0.00 | 0.00 | 365 |
| 2017 | KILBARGER INVESTMENTS INC | 0.00 | 79.00 | 365 |
| 2018 | KILBARGER INVESTMENTS INC | 0.00 | 0.00 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -170348777 | 2005-2-1 0:00:0 | AD | No Violations | |
| -681572276 | 2009-5-19 0:00: | PW | No Violations | |
| -861367210 | 2009-6-24 0:00: | PW | No Violations | |
| 000PL16069 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 0170348777 | 2005-02-01 | Annular Disposal | No Violations | No violations, Checked AD for Columbus, AD not used. NEW LAT & LONG |
| 0642566593 | 2010-04-13 | Annular Disposal | No Violations | An inspection of this well was requested by Central Office to verify Annular Disposal (AD) connection. During the inspection, it was noted that the AD remains disconnected. Brine drains from standing knockout to 100 bbl tank. At time of inspection, the tank appeared to be full. Records indicate that the reported Brine production has been zero since 2002. GPS reading obtained for the tank battery. |
| 0681572276 | 2009-05-19 | Production Wells | Violations Noted | An inspection revealed old and new oil around the well head from stuffing box leak. A 1 plastic line from knock-out to 100 bbl saltwater tank contained a small cut allowing fluid to drip onto ground surface. Old oil observed inside dike which appeared to be breaking down. A bare area approximately 10 x 50 (length) was observed outside the dike from saltwater tank location. High Range Quantabs showed 4.0 units, which equals 986 ppm (mg/L) Cl-. Note: Side of saltwater tank with bottom valve not inside earthen dike. The valve on this tank was observed closed. The lease road is eroding and will need to be graded. GPS reading obtained for well and tank battery locations. Notified Mr. Mike McPeek with Kilbarger of the inspection results. |
| 0861367210 | 2009-06-24 | Production Wells | No Violations | A follow-up inspection revealed compliance. |
| 1892294826 | 2015-09-16 | Temporary Abandoned Annular Disposal | No Violations | An inspection of this well was requested by Central Office to verify Annular Disposal (AD) connection. During the inspection, it was noted that the AD remains disconnected |
| 642566593 | 2010-4-13 0:00: | AD | No Violations | |
| PL16069 | PL | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0681572276 | US-OH-127709 | 2009-06-04 | Well operation causing pollution and contamination | |
| 0681572276 | US-OH-127710 | 2009-06-04 | Well insufficiently equipped to prevent escape of oil and gas | |
| 0681572276 | US-OH-127711 | 2009-06-04 | Equipment pressure rated below operating pressure |
For data sources see[9]