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Well ID: 34-073-60110 | Loading map...
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Country: United States | |
State: Ohio | |
County: Hocking | |
Municipality: Benton Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: SAMUEL EVELAND ETAL | |
License Status: Final Restoration | |
License Date: 2010-10-13 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: 1921-04-24 | |
Well Total Depth: 2353.00 ft | |
Configuration: Vertical | |
Latitude: 39.420000 | |
Longitude: -82.600000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Completed | 1921-04-24 | WELL IS ON COLUMBIA'S 2005 REHAB LIST PF=PAY |
Reached Total Depth | 1921-04-24 | WELL IS ON COLUMBIA'S 2005 REHAB LIST PF=PAY |
APP | 2010-10-13 | Proposed Formations:CLINTON, Issued Date:10/13/2010, Expired Date:10/12/2012 12:00:00 PM, Drilling unit acres:205, Proposed Well Type:SO, Proposed Well Class: |
Plugged/Abandoned | 2010-12-20 | WELL IS ON COLUMBIA'S 2005 REHAB LIST PF=PAY |
Construction Permit Expires | 2012-10-12 | WELL IS ON COLUMBIA'S 2005 REHAB LIST PF=PAY |
Record Last Modified | 2013-03-14 | WELL IS ON COLUMBIA'S 2005 REHAB LIST PF=PAY |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-218173724 | 2010-12-15 0:00 | PB | No Violations | 7.00 |
-308350216 | 2011-9-15 0:00: | FR | No Violations | |
0105668171 | 2010-12-20 | Plug / Plug Back | No Violations | Witnessed plugging and abandonment. Pumped cement inside 3.5 csg from 1790 to 1000 for Lime plug. Perforated at 770 (6 shots) and set 3.5 cement retainer at 753 then perforated again at 300 (6 shots). Stabbed into retainer with stinger. Pump pressure reached 1250lb w/no estbl circulation and unable to squeeze w/ stinger. Therefore, we would now rely on hydrostatic pressure and stabbed-out of retainer to pump 4bbl of cement to 315. Pulled 15 joints. Closed return line on BOP w/initial circulation and pumped 0.75 bbl cement w/pressure of over 800 lbs. Opened line and observed cement returns. TOH. Cement dropped and unable to visually see. Topped off to surface. The above procedures were done with the idea that at least hydrostatic would assist with squeezing of cement on backside of casing to seal Berea formation. Background: Set a 600 bottom hole plug on 12/15/2010, through 2.063 tubing (inside 3.5 casing cemented to surface). Note: Columbia records had showed 3.5 csg to surface inside un-cemented 5.5 csg; and 7 csg left from 534-782 w/lead BH packer also not cemented and placed across the Berea. In the 1960s, the 5.5csg was perforated and cemented from 210 to surface. Recent new drill for Columbia, Permit No. 3596 showed freshwater at 405. No casing would be retrieved from this plug job. |
0218173724 | 2010-12-15 | Plug / Plug Back | No Violations | Witnessed kill procedure with 20.5 bbl saltwater (morning) and bottom hole plug (afternoon). |
0308350216 | 2011-09-15 | Final Restoration | No Violations | Restoration meets 1509.072 requirements. Lease road is still used for access to existing storage well. |
105668171 | 2010-12-20 0:00 | PB | No Violations | 8.00 |
For data sources see[4]