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Well ID: 34-075-22121 | Loading map...
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Country: United States | |
State: Ohio | |
County: Holmes | |
Municipality: Monroe Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: KINSEY | |
License Status: Final Restoration | |
License Date: 2017-08-23 | |
Spud Date: 1978-12-14 | |
Spud Drilling Contractor: | |
Final Drill Date: 1979-03-27 | |
Well Total Depth: 3405.00 ft | |
Configuration: Vertical | |
Latitude: 40.570000 | |
Longitude: -82.070000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1978-10-20 | 1453 GREEN ENERGY INC GeoDate 10/20/78 |
Original Spud | 1978-12-14 | |
Completed | 1979-03-27 | |
Reached Total Depth | 1979-03-27 | |
Change of Owner | 2000-07-06 | Operator changed from 1453, GREEN ENERGY INC to 2491, MILLER ROY/RA MILLER ENER |
Change of Owner | 2007-10-05 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
APP | 2017-08-23 | Proposed Formations:CLINTON, Issued Date:8/23/2017, Expired Date:8/23/2019 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2017-09-19 | |
Record Last Modified | 2017-11-08 | |
Construction Permit Expires | 2019-08-23 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 0 | 1 | |
0 | 1 | ||
0 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 850 Bbl | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | JADOIL INC D VERNAU | 106.00 | 31.00 | 0 |
1985 | JADOIL INC D VERNAU | 0.00 | 0.00 | 200 |
1986 | SIMPSON B T JR | 4470.00 | 0.00 | 365 |
1987 | MELANIE OIL DRIL USA INC | 3190.00 | 0.00 | 245 |
1988 | MELANIE OIL DRIL USA INC | 5941.00 | 88.00 | 365 |
1989 | MELANIE OIL DRIL USA INC | 3798.00 | 0.00 | 365 |
1990 | GREEN ENERGY INC | 0.00 | 0.00 | 153 |
1991 | GREEN ENERGY INC | 3401.00 | 0.00 | 365 |
1992 | GREEN ENERGY INC | 2957.00 | 0.00 | 365 |
1993 | GREEN ENERGY INC | 2266.00 | 0.00 | 365 |
1994 | GREEN ENERGY INC | 1997.00 | 0.00 | 365 |
1995 | GREEN ENERGY INC | 1600.00 | 0.00 | 365 |
1996 | GREEN ENERGY INC | 638.00 | 0.00 | 365 |
1997 | GREEN ENERGY INC | 547.00 | 0.00 | 365 |
1998 | GREEN ENERGY INC | 915.00 | 0.00 | 365 |
1999 | GREEN ENERGY INC | 1039.00 | 0.00 | 365 |
2000 | GREEN ENERGY INC | 713.00 | 0.00 | 180 |
2001 | MILLER ROY/R A MILLER ENERGY L | 99.00 | 0.00 | 365 |
2002 | MILLER ROY/R A MILLER ENERGY L | 338.00 | 0.00 | 365 |
2003 | MILLER ROY/R A MILLER ENERGY L | 216.00 | 20.00 | 365 |
2004 | MILLER ROY/R A MILLER ENERGY L | 58.00 | 0.00 | 365 |
2005 | MILLER ROY/R A MILLER ENERGY L | 872.00 | 43.00 | 365 |
2006 | MILLER ROY/R A MILLER ENERGY L | 1018.00 | 0.00 | 365 |
2011 | DEEP RESOURCES LLC | 16.00 | 13.00 | 90 |
2012 | DEEP RESOURCES LLC | 0.00 | 0.00 | 366 |
2014 | DEEP RESOURCES LLC | 0.00 | 0.00 | 0 |
2016 | DEEP RESOURCES LLC | 0.00 | 0.00 | 0 |
2017 | DEEP RESOURCES LLC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2102062282 | 2017-9-1 0:00:0 | PB | No Violations | |
-410133785 | 2011-9-21 0:00: | PW | No Violations | |
0410133785 | 2011-09-21 | Production Wells | No Violations | Producing rabbit well, cannot find tank battery. |
0925967094 | 2017-07-13 | Production Wells | Violations Noted | This well is not producing. Contacted the new owner of Deep Resources and he will check it out and get a plugging permit for it. |
1322523769 | 2017-09-20 | Final Restoration | No Violations | The top plug dropped 6. The operator will be cutting off the casing and reclaiming the location. |
1373883888 | 2013-07-12 | Production Wells | No Violations | This is a producing plunger lift well. There were no problems noted at the time of the inspection. |
1505480413 | 2017-09-14 | Plug / Plug Back | No Violations | Allie Oprzadek requested assistance to witness plugging the well. Arrived on location and the production casing had parted. The service rig was pulling long string. The rig crew is going to run tubing back in the well and cement is tentatively postponed until Friday. |
1505751146 | 2017-09-18 | Plug / Plug Back | No Violations | Arrived on location to assist Allie Oprzadek of the DOGRM with plugging. Cement was cancelled for today by the cement contractor. No work on location. |
1541489877 | 2017-10-05 | Final Restoration | No Violations | Cropland, final grade, seeded. Final restoration passed. |
2071194010 | 2017-09-19 | Plug / Plug Back | No Violations | This well was plugged this date. Petroset Services set cement plugs at: 2225-2175, 965-795, 600-400 and 162-0. The well circulated prior to each plug. |
2102062282 | 2017-09-01 | Plug / Plug Back | No Violations | Went to the well to check out the casing size. 3-1/2. No reference to 3-1/2: in the copletion report or anywhere else in the files. |
925967094 | 2017-7-13 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0925967094 | US-OH-130579 | 2017-08-31 | NONE | Well shall be plugged |
For data sources see[9]