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Well ID: 34-075-22891 | Loading map...
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Country: United States | |
State: Ohio | |
County: Holmes | |
Municipality: Killbuck Township | |
Operator Name: MAC OIL FIELD SERVICE INC | |
Well Pad ID: | |
Farm/Lease Name: LEE A YOUNG | |
License Status: Final Restoration | |
License Date: 2016-09-30 | |
Spud Date: 1981-03-26 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-03-29 | |
Well Total Depth: 3704.00 ft | |
Configuration: Vertical | |
Latitude: 40.490000 | |
Longitude: -81.950000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-12-16 | 162 LAKE REGION OIL INC GeoDate 12/16/80 |
Oil and Gas | 1980-12-16 | Issued Date 12/16/80 Expired Date Acres 0020000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1981-03-26 | |
Completed | 1981-03-29 | |
Reached Total Depth | 1981-03-29 | |
Completion Report Received | 1981-06-24 | |
CO | 1996-06-11 | 5312 MAC OIL FIELD SERVICE INC GeoDate 12/16/80 |
Plugged/Abandoned | 2016-09-14 | |
APP | 2016-09-30 | Proposed Formations:CLINTON, Issued Date:9/30/2016, Expired Date:9/30/2018 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:HAD, Proposed Well Class: |
Record Last Modified | 2017-10-19 | |
Construction Permit Expires | 2018-09-30 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3516 | 3575 | 12 |
3516 | 3575 | 12 | |
3516 | 3575 | 12 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 67000 Gal | 35000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1149243549 | 2016-9-15 0:00: | PB | No Violations | |
-1379900401 | 2017-10-5 0:00: | FR | No Violations | |
-1535414691 | 2016-9-29 0:00: | FR | No Violations | |
-2127326464 | 2016-9-8 0:00:0 | WR | No Violations | |
-414441299 | 2015-11-18 0:00 | PW | No Violations | |
000PL15882 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
001239i374 | 2002-08-14 | Production Wells | No Violations | |
0047376287 | 2002-10-28 | Production Wells | No Violations | Check to see if id has been posted beause the id had faded and could not be read on last inspection . It was posted but just faded . The new id has been posted . |
0245383316 | 2012-12-06 | Production Wells | No Violations | This is a producing pump jack well. There were no problems noted at the time of the inspection. |
0414441299 | 2015-11-18 | Production Wells | No Violations | This well is not producing. The operator says it needs swabbed. Will try to get in there before bad weather. |
0423029957 | 2016-09-12 | Plug / Plug Back | No Violations | No activity this date. |
0917321990 | 2014-05-28 | Production Wells | No Violations | This is a producing pump jack well. There were no problems noted at the time of the inspection. |
1145251940 | 2017-04-19 | Final Restoration | No Violations | There is some erosion of the lease road at the steepest part. Not too much growth of grasses on the location. There are some wet weather springs coming out of the hill above the location that inhibits growth. Contacted the operator to seed the location and put in road bars on the steep part of the lease road. He has to get with the landowner anyway for a pipeline R-O-W and will determine how the landowner is going to use the property going forward and adjust the reclamtion to that plan. |
1149243549 | 2016-09-15 | Plug / Plug Back | No Violations | The top plug dropped 15 from ground level. The operator cut off the casing below plow depth and filled with 6 bags of Sacrete and put a plate with the Permit number on the top. The pit has been emptied and closed and the location has been roughed in to original grade. |
1239i374 | 2002-8-14 0:00: | PW | No Violations | 0.70 |
1379900401 | 2017-10-05 | Final Restoration | No Violations | Final restoration is passed. |
1449662445 | 2015-12-08 | Administrative Inspection | No Violations | I received a call from Brandon McVickers about their plans for this well. They have cut a road in to the well. They are waiting for a service rig to run rods in the well and will test the well to see if they can catch up with the fluid by the spring. If not the well will be plugged and abandoned. |
1473677934 | 2016-09-09 | Plug / Plug Back | No Violations | Appalachian Well Service shot the tubing off at 2969. The rig pulled the tubing out of the hole and rigged up the ripping tools to rip the 4-1/2 casing on Monday morning. |
1473938778 | 2016-09-13 | Plug / Plug Back | No Violations | Ran in the hole with the ripper and ripped the 4-1/2 casing at 2600. Pulled the casing and ran the 1-1/2 tubing to 2460 thru which to spot the cement plugs. |
1474976810 | 2016-09-14 | Plug / Plug Back | No Violations | Petroset ciculated ~100 bbls of oil out of the well then set cement plugs to plug out the well. See the plugging report for the details. |
1535414691 | 2016-09-29 | Final Restoration | No Violations | The location has been roughed in but needs seeded and mulched. |
1838796564 | 2016-09-07 | Production Wells | No Violations | There is no rig on location at this time. |
1915756027 | 2012-12-05 | Production Wells | No Violations | This is a producing pump jack well. There were no problems noted at the time of the inspection. |
2127326464 | 2016-09-08 | Work Over Reconditioning | No Violations | This workover encountered a very high fluid level. The packer may be leaking but the rig was unable to get it loose and it is on the bottom of 1-1/2 tubing. The decision was made to plug the well. A 30 sack bottom cement plug was bullheaded thru the tubing and the well was shut in. |
245383316 | 2012-12-6 0:00: | PW | No Violations | |
423029957 | 2016-9-12 0:00: | PB | No Violations | |
47376287 | 2002-10-28 0:00 | PW | No Violations | 0.70 |
917321990 | 2014-5-28 0:00: | PW | No Violations | |
PL15882 | PL | No Violations |
For data sources see[9]