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Well ID: 34-075-24560 | Loading map...
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Country: United States | |
State: Ohio | |
County: Holmes | |
Municipality: Prairie Township | |
Operator Name: PONDEROSA CONSULTING SERVICES | |
Well Pad ID: | |
Farm/Lease Name: KNOTT JOSEPH L UNIT | |
License Status: Producing | |
License Date: 1985-06-19 | |
Spud Date: 1985-08-27 | |
Spud Drilling Contractor: H A D INC | |
Final Drill Date: 1985-08-31 | |
Well Total Depth: 3627.00 ft | |
Configuration: Vertical | |
Latitude: 40.650000 | |
Longitude: -81.880000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1985-06-19 | Issued Date 6/19/85 Expired Date 6/19/86 Acres 0020000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 03627 Proposed Drill Depth 03627 |
Original Spud | 1985-08-27 | |
Completed | 1985-08-31 | |
Reached Total Depth | 1985-08-31 | |
CO | 1985-09-24 | 2180 PONDEROSA CONSULT SER INC GeoDate 6/19/85 |
Completion Report Received | 1985-09-30 | |
Construction Permit Expires | 1986-06-19 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3468 | 3554 | 0 |
3468 | 3554 | 0 | |
2006-09-11 | 3478 | 3540 | 18 |
3478 | 3540 | 18 | |
3468 | 3554 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 150 Mscf | 0 | |||
H2O | 0 | 72500 Gal | 25000 | FRAC;H2O,SAND,N2 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1629334549 | 2020-2-3 0:00:0 | PW | No Violations | 0.50 |
-452773753 | 2020-9-29 0:00: | PW | No Violations | 0.50 |
-457689375 | 2016-10-24 0:00 | PW | No Violations | |
000PL15225 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0392469817 | 2017-06-08 | Production Wells | No Violations | This swab well is not producing commercially. The land owner is getting enough gas off the well to use for cooking only. There is no ID on the well and there is no legible ID on the tank. The production records have been brought up to date thru 2015. there is a compliance action in the works for this well. |
0457689375 | 2016-10-24 | Production Wells | No Violations | This swab well is producing only house gas to the landowner who is using it for hot water and cooking only. There has been no commercial production since the mid 1980s. There were no other problems noted at the time of the inspection. |
0967363657 | 2014-12-12 | Production Wells | Violations Noted | This well is not producing. There is no ID. Statement of Annual Production reports for 2013 have not been filed as required. This well shall be plugged within 180 days. A valid legible ID hall be posted immediately. The production report for 2013 |
1528119820 | 2018-06-04 | Production Wells | No Violations | This is a follow up inspection to compliance notice 967363657 issued on 12/15/2014 I found an 8 5/8 inch diameter casing, 4 1/2 inch diameter casing, a 4 1/2 inch diameter by 2 3/8 inch diameter swage, and a 2 3/8 inch diameter valve on top. The production equipment is made up of two 100 bbl. steel tanks, two vertical separators, and two 25 bbl. plastic tanks. The tanks are not properly identified. The heater tubes on both tanks are leaking. The production equipment is shared with another well. A sample was collected and tested by using Quantab test strips. The high range showed above 6939 ppm chlorides. A phone call has been placed to Bob Breneman with Ponderosa Consult Service and a message was left. |
1542813124 | 2018-11-21 | Production Wells | No Violations | This is a follow up inspection to compliance notice 967363657 issued on 12/15/2014 I found an 8 5/8-inch diameter casing, 4 1/2-inch diameter casing, a 4 1/2-inch diameter by 2 3/8-inch diameter swage, and a 2 3/8-inch diameter valve on top. The well is a swab well. The production equipment is made up of two 100 bbl. steel tanks, two vertical separators, and two 25 bbl. plastic tanks. The tanks are not properly identified. The tank assigned to this well, the heater tube has been plumbed back into the tank, no cleanup has been done. The production equipment is shared with another well. The landowner has expressed that they want the well plugged and abandon. |
1548336036 | 2019-01-24 | Production Wells | No Violations
-395 issued on 12/06/2018 I found an 8 5/8-inch diameter casing, 4 1/2-inch diameter casing, a 4 1/2-inch diameter by 2 3/8-inch diameter swage, and a 2 3/8-inch diameter valve on top. The well is a swab well. The production equipment is made up of two 100 bbl. steel tanks, two vertical separators, and two 25 bbl. plastic tanks. The tanks are not properly identified. The tank assigned to this well, the heater tube has been plumbed back into the tank, no cleanup has been done. The production equipment is shared with another well. The landowner has expressed that they want the well plugged and abandon. | |
1559563844 | 2019-06-03 | Production Wells | No Violations
-395 issued on 12/06/2018 I found an 8 5/8-inch diameter casing, 4 1/2-inch diameter casing, a 4 1/2-inch diameter by 2 3/8-inch diameter swage, and a 2 3/8-inch diameter valve on top. The well is a swab well. The production equipment is made up of two 100 bbl. steel tanks, two vertical separators, and two 25 bbl. plastic tanks. The tanks are not properly identified. No cleanup has been done. The production equipment is shared with another well. The landowner has expressed that they want the well plugged and abandon. The production for the year of 2018 has not been reported. | |
1570708313 | 2019-10-10 0:00 | PW | No Violations | 1.00 |
2027750734 | 2018-08-07 | Exempt Well Pre Transfer | No Violations | This is a follow up inspection to compliance notice 967363657 issued on 12/15/2014 I found an 8 5/8 inch diameter casing, 4 1/2 inch diameter casing, a 4 1/2 inch diameter by 2 3/8 inch diameter swage, and a 2 3/8 inch diameter valve on top. The well is a swab well. The production equipment is made up of two 100 bbl. steel tanks, two vertical separators, and two 25 bbl. plastic tanks. The tanks are not properly identified. The heater tubes on both tanks are leaking, and no cleanup has been done. The production equipment is shared with another well. The landowner has expressed that they want the well plugged and abandon. |
392469817 | 2017-6-8 0:00:0 | PW | No Violations | |
967363657 | 2014-12-12 0:00 | PW | No Violations | |
PL15225 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0967363657 | US-OH-131096 | 2015-01-08 | Failure to legibly identify well | |
0967363657 | US-OH-131097 | 2015-01-08 | Well shall be plugged | |
0967363657 | US-OH-131098 | 2015-01-08 | Statement of annual production not filed |
For data sources see[9]