X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-075-60086

Well Details

Well ID: 34-075-60086
Loading map...
Country: United States
State: Ohio
County: Holmes
Municipality: Hardy Township
Operator Name: W H PATTEN DRILLING CO
Well Pad ID:
Farm/Lease Name: GALLEY GEO
License Status: Final Restoration
License Date: 2011-09-30
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1926-02-24
Well Total Depth: 3546.00 ft
Configuration: Vertical
Latitude: 40.580000
Longitude: -81.940000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1926-02-24 R.R.
Reached Total Depth 1926-02-24 R.R.
APP 2011-09-30 Proposed Formations:CLINTON, Issued Date:9/30/2011, Expired Date:9/29/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2012-04-30 R.R.
Record Last Modified 2013-03-14 R.R.
Construction Permit Expires 2013-09-29 R.R.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2011 W H PATTEN DRILLING CO 0.00 0.00 365
2012 W H PATTEN DRILLING CO 0.00 0.00 366

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2011 W H PATTEN DRILLING CO Brine 0 365
2012 W H PATTEN DRILLING CO Brine 0 366

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1105487957 2012-4-16 0:00: PB No Violations
-1317229094 2012-4-26 0:00: PB No Violations
-1590081945 2012-4-24 0:00: PB No Violations
-1712635545 2012-4-11 0:00: PB No Violations
-1886196707 2012-4-18 0:00: PB No Violations
-2015532631 2012-5-2 0:00:0 FR No Violations
-2103192549 2012-4-9 0:00:0 PB No Violations
-608316427 2012-4-17 0:00: PB No Violations
0608316427 2012-04-17 Plug / Plug Back No Violations Tagged Berea plug at 698. Shot off 5-1/2 casing at 500.
0887160668 2012-04-20 Plug / Plug Back No Violations Washed in 3 tons of clay on the top plug and the well filled back up. Will let it settle over the weekend and top it off on Monday morning.
0924892866 2012-04-06 Plug / Plug Back No Violations Running 1-1/2 tubing.
1105487957 2012-04-16 Plug / Plug Back No Violations Omega Cementing spotted cement plugs over the top of the Big Lime and the Berea. See plugging report for details.
1231107681 2012-04-04 Plug / Plug Back No Violations Pulling tubing.
1317229094 2012-04-26 Plug / Plug Back No Violations Still topping off the top clay plug.
1334605566 2012-04-12 Plug / Plug Back No Violations Tagged bottom plug at 2920. Pulled tubing.
1334659189 2012-04-13 Plug / Plug Back No Violations Perforated 5-1/2 casing at Big lime and Berea. Ran 1-1/2 tubing to Big Lime perforations.
1334918249 2012-04-19 Plug / Plug Back No Violations Ripped 7 at 425 but could not pull it. Ripped it again at 320 and were able to pull it. Bailing oil out of hole.
1590081945 2012-04-24 Plug / Plug Back No Violations The top plug continues to drop slightly. The operator keeps filling it up.
1712635545 2012-04-11 Plug / Plug Back No Violations Washed out the clay inside of the 5.5 casing. Stopped at top of the liner, at 3320, and spotted a cement plug from 3320 to 2920 with 45 sacks of Class A cement.
1739832968 2012-04-23 Plug / Plug Back No Violations
1886196707 2012-04-18 Plug / Plug Back No Violations Pulled 500 of 5-1/2 casing. Trying to rip 7 but cant get past 423. Will try to rip there.
1986737709 2011-10-13 Production Wells No Violations This well is not in production and production has not been reported for years. Owner has plugging permit in hand.
2015532631 2012-05-02 Final Restoration No Violations The well casing has been cut off and buried and the location leveled. The farmer will till the soil shortly. Final Restoration passed.
2103192549 2012-04-09 Plug / Plug Back No Violations The 1-1/2 tubing set down at 2412. We were able to circulate. Pulled 1-1/2 out to run 2-3/8 tubing in to wash out clay.
887160668 2012-4-20 0:00: PB No Violations
924892866 2012-4-6 0:00:0 PB No Violations

For data sources see[7]

References