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Well ID: 34-079-20259 | Loading map...
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Country: United States | |
State: Ohio | |
County: Jackson | |
Municipality: Milton Township | |
Operator Name: TOMSTAN DRILLING COMPANY | |
Well Pad ID: | |
Farm/Lease Name: MORROW J | |
License Status: Final Restoration | |
License Date: 2007-12-13 | |
Spud Date: 2008-01-11 | |
Spud Drilling Contractor: G & H DRLG | |
Final Drill Date: 2008-01-14 | |
Well Total Depth: 2019.00 ft | |
Configuration: Vertical | |
Latitude: 39.070000 | |
Longitude: -82.520000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2007-12-13 | Proposed Formations:BIG LIME, Issued Date:12/13/2007, Expired Date:12/12/2008 6:00:00 AM, Drilling unit acres:61.47, Proposed Well Type:OG, Proposed Well Class:EW |
Correction to Well | 2007-12-21 | CHANGE IN WELL TYPE FROM OIL & GAS TO STRATAGRAPHIC. |
Reached Total Depth | 2008-01-14 | |
Completion Report Received | 2008-09-24 | |
Construction Permit Expires | 2008-12-12 | |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | NOT PERFED, TREATED, OR PRODUCED |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2013 | TOMSTAN DRILLING COMPANY | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2010 | TOMSTAN DRILLING COMPANY | Brine | 0 | 120 |
2011 | TOMSTAN DRILLING COMPANY | Brine | 0 | 120 |
2012 | TOMSTAN DRILLING COMPANY | Brine | 0 | 120 |
2013 | TOMSTAN DRILLING COMPANY | Brine | 0 | 0 |
2014 | TOMSTAN DRILLING COMPANY | Brine | 0 | 0 |
2015 | TOMSTAN DRILLING COMPANY | Brine | 0 | 0 |
2016 | TOMSTAN DRILLING COMPANY | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-125100270 | 2008-1-12 0:00: | DD | No Violations | |
-1702146215 | 2008-1-11 0:00: | DD | No Violations | |
-1730239957 | 2008-1-14 0:00: | DD | No Violations | |
-1800969489 | 2012-10-1 0:00: | FR | No Violations | 2.00 |
-1817043872 | 2009-12-14 0:00 | PL | No Violations | |
-1826864904 | 2009-10-8 0:00: | PL | No Violations | |
-1874207679 | 2010-8-24 0:00: | PL | No Violations | 1.50 |
-241863723 | 2012-9-24 0:00: | NF | No Violations | 3.00 |
-283144582 | 2015-5-11 0:00: | PB | No Violations | |
-293127877 | 2010-1-6 0:00:0 | PL | No Violations | |
0019554332 | 2016-02-01 | Production Wells | No Violations | Tank battery consists of two 100 bbl steel tanks, a separator, meter, and a dike. No noted violations. |
0125100270 | 2008-01-12 | Drill / Deepen / Reopen | No Violations | Surface cement job. Spud date 1-11-2008. Ran 65 of conductor in a 11 hole. TD 1144 set 1095 of 8 5/8 plus 11 landing joint. I got called out at 8:30pm on the 12th and cement trucks were late. Cement trucks arrived at 3am and got stuck at location for an hour. Had good circulation and good cement returns to the surface. I left the location at 6:30 am on the 13th. |
0201495372 | 2009-08-10 | Preliminary Restoration | No Violations | Site has been graded. No substantial erosion at this time. Two main areas void of vegetation measure 102 by 40 and 60 by 30. I called Stan Holler at 9:30am and we discussed the restoration problems and the measures needed to correct them. Re: establish vegetative cover. Prevent erosion. Identify well and equip wells for production. |
0241863723 | 2012-09-24 | Field Inspected, Well Not Found | No Violations | Using RBDMS coordinates I search for this well. The GPS coordinates listed for this well are actually the bottom hole location for the well API 34-079-20259-00-00. This well was drilled horizontally through the Ohio Shale. |
0283144582 | 2015-05-11 | Plug / Plug Back | No Violations | Updated record to reflect status of well according to IT section, from FR to PB. |
0293127877 | 2010-01-06 | Preliminary Restoration | No Violations | This is a Horizontal portion of well # 34-079-20259-00-00. All restoration reports and NOVs will be listed under #34-079-20259-00-00. |
1201614705 | 2008-01-28 | Drill / Deepen / Reopen | Violations Noted | Pit liner on the mud pit has fallen in on one side. Oil and other drilling fluids are in contact with the soil. Oil in puddles around the well head. Wellhead is leaking some gas. I tried to call the well owner but could only get an answering machine. I left a message but was cut off due to machine running out of memory space. |
1204731059 | 2008-02-07 | Drill / Deepen / Reopen | No Violations | Pits still full and over flowing. I called Stan Holler and he informed me that work has been arranged and that the weather is making it difficult to get a water truck in to the location. I suggested dragging a frac tank with a dozer to the location and pumping the pits into it until it dries up. |
1205182071 | 2008-03-10 | Drill / Deepen / Reopen | No Violations | Pits have been pumped out and taken to an injection well. Pits have been closed. Site is very muddy and will be reclaimed in the spring as weather allows. |
1231353774 | 2009-01-05 | Production Wells | Violations Noted | Well has no identification. Well site has not been graded there are piles of soil mixed with drill cuttings and pit liner pieces. Well has 2 tubing ran. Well is not connected to any production equipment or production lines. Vegetative cover has not been established. 95% bare ground. Site is very rough with ruts and mud over entire location. Pit liner pieces are strewn around location. Sediment is moving off location and into the wood line. A half joint of 8 5/8 casing is laying in mud along access road. Access road does not have any diversions or means to control erosion. Road is a low cut through the woods. This traps the surface water and allows it to form a channel with in the road. Place Identification at wellhead. Remove all debris from well site. Grade well site. Seed and apply mulch to establish vegetative growth on location. Follow Best Management Practices For Well Site Construction. Follow Permit Restoration Plan. |
1702146215 | 2008-01-11 | Drill / Deepen / Reopen | No Violations | No permit on location. I told them they need the permit on location. Rig has not spuded yet. Pit is positioned to allow for 60 of flow line. They are drilling with air. I talked to the driller about a min. of 60 of conductor. I advised them to take the conductor down until they hit something solid at least 60. I gave the rig crew a copy of Ohio Oil& Gas Laws & Rules. |
1730239957 | 2008-01-14 | Drill / Deepen / Reopen | No Violations | They have TD hole at 2019 and are preparing to cement the kick off plug. Mud logger said the formation looks good. |
1800969489 | 2012-10-01 | Final Restoration | No Violations | Well is shut-in. Restoration of site is slowly recovering. Owner claims he has tried reseeding several times. It appears from my visit that the pH of the soil may not be conducive to support plant growth. May need to add some amendments such as lime to facilitate plant growth. pH could be a problem since rainwater drains over some exposed coal material above this site. |
1817043872 | 2009-12-14 | Preliminary Restoration | No Violations | Seed and mulch have been reapplied to location. 85 % of location has grass growing. Erosion ditches have been filled in. Chucks of fertilizer have been applied to location. No identification at well. No production equipment or production lines are at well site. Well is equipped with tubing and a valve with a gauge. Gauge reads 120psi. A small gas leak at the 8 5/8 collar and the 8 5/8 by 4 1/2 swedge. No explosive levels were detected with the gas detector. I called Stan Holler (well owner) and left him a message regarding the leak and for him to call me with a time frame on getting the well in production. |
1826864904 | 2009-10-08 | Preliminary Restoration | No Violations | New Grass is growing. Site still has some bare areas with no vegetative cover. Need to reseed bare areas with a variety of seed types to allow better vegetative cover. Well head has slight audible leak. No explosive levels detected with gas meter. Still need to grade erosion site and seed and mulch. No identification, No production equipment or production lines. Called and talked to Stan Holler Well owner and we discussed the work that needs to be done. Stan asked if he could install the id when he runs the production lines. He is bidding out the line work now. I agreed as long as the work gets accomplished soon. |
1874207679 | 2010-08-24 | Preliminary Restoration | No Violations | Vegetation established. Trees starting to grow on location. No substantial erosion. Inspected site with Robert Stonerock South Region Supervisor. Well is connected to production line. No identification on wellhead. Stan Holler ( well owner) was on the lease during inspection. Robert and I talked to him in detail about corrective actions that need to be taken. We also discussed the tank battery and the dike drain which does not have a valve or other means to close the drain. No identification on the tank. |
19554332 | 2016-2-1 0:00:0 | PW | No Violations | 1.00 |
201495372 | 2009-8-10 0:00: | PL | No Violations | |
2120889198 | 2008-01-31 | Administrative Inspection | No Violations | Talked to Stan (Owner) He said that a contractor is meeting at the site on 2-1-08 to look at it and give him a price. Stan said that he will call me next week to give me an update. I explained what I wanted right now was the fluid in the pit with the bad liner to be pumped out and hauled to a disposal well. I told him the restoration time lines on his project 5 months to pump and reclaim the pits and 9 months to reclaim the location. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1201614705 | US-OH-105285 | 2008-01-29 | Drilling operation causing pollution and contamination | |
1201614705 | US-OH-105286 | 2008-01-29 | Dike or pit not able to prevent escape of brine or other wastes | |
1231353774 | US-OH-106222 | 2009-01-07 | Failure to restore land surface within 9 mos. (CHANGE) (REPLACE) | |
1231353774 | US-OH-106223 | 2009-01-07 | Failure to legibly identify well | |
1231353774 | US-OH-106224 | 2009-01-07 | Disposal of muds or cuttings in violation of a rule |
For data sources see[8]