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Well ID: 34-081-20647 | Loading map...
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Country: United States | |
State: Ohio | |
County: Jefferson | |
Municipality: Salem Township | |
Operator Name: EAP OHIO LLC | |
Well Pad ID: US-OH-001551 | |
Farm/Lease Name: OLD OAK FARM 6-10-3 | |
License Status: Producing | |
License Date: 2018-05-10 | |
Spud Date: 2018-05-14 | |
Spud Drilling Contractor: PATTERSON DRILLING | |
Final Drill Date: 2018-07-12 | |
Well Total Depth: 21635.00 ft | |
Configuration: Horizontal | |
Latitude: 40.460000 | |
Longitude: -80.750000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2016-06-20 | Proposed Formations:TRENTON THRU BLACK RIVER, Issued Date:6/20/2016, Expired Date:6/20/2018 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
Correction to Well | 2017-09-15 | CHANGE TO WELL NUMBER FROM 1 TO 5 |
APP | 2018-05-10 | Proposed Formations:POINT PLEASANT, Issued Date:5/10/2018, Expired Date:5/9/2020 12:00:00 PM, Drilling unit acres:301.433, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2018-07-12 | |
Correction to Well | 2018-08-31 | TAKE TARGET AS-DRILLED |
Change of Owner | 2018-12-18 | Operator changed from 8756, CHESAPEAKE EXPLORATION LLC to 10240, EAP OHIO LLC |
Completion Report Received | 2019-01-11 | |
Record Last Modified | 2019-01-16 | |
Construction Permit Expires | 2020-05-09 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2019-01-15 | 9304 | 9464 | 0 |
2019-01-15 | 21408 | 21504 | 0 |
21408 | 21504 | 0 | |
9304 | 9464 | 0 | |
9304 | 9464 | 0 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 08/11/2018 | 09/08/2018 | 8976.5 | 15,478,200.0 | 1,118,310.0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Northern White Sand | HALLIBURTON | Proppant - Natural | Crystalline Silica (Quartz Sand, Silicon Dioxide) | 014808-60-7 | 1 | 0.13154 | 0 |
Fresh Water | CHESAPEAKE ENERGY | Carrier/Base Fluid | Water | 007732-18-5 | 1 | 0.73343 | 0 | |
SC-30 | FOUNTAIN QUAIL | Scale Inhibitor | Sodium Hydroxide | 1310-73-2 | 0.02 | 0 | 0 | |
Recycled Produced Water | CHESAPEAKE ENERGY | Carrier/Base Fluid | Water | 007732-18-5 | 1 | 0.12211 | 0 | |
LD-2900 | MULTI-CHEM | Friction Reducer | Distillates (petroleum), Hydrotreated Light | 64742-47-8 | 0.3 | 0 | 0 | |
Poly(oxy-1.2-ethanediyl), a-tridecyl-w-hydroxy-, branched | 69011-36-5 | 0.05 | 0 | 0 | ||||
OptiKleen-WF | HALLIBURTON | Breaker | Sodium perborate tetrahydrate | 010486-00-7 | 1 | 0.00002000 | 0 | |
HAI-OS | HALLIBURTON | Corrosion Inhibitor | Methanol (Methyl Alcohol) | 000067-56-1 | 0.6 | 0.00001000 | 0 | |
Propargyl Alcohol (2-Propynol) | 000107-19-7 | 0.1 | 0 | 0 | ||||
FE-2A | HALLIBURTON | Iron Control Agent | Citric Acid | 000077-92-9 | 0.6 | 0.00004000 | 0 | |
FDP-S1320-18, FE-2A, FightR EC-1,
HAI-OS, OptiKleen-WF, SP BREAKER |
HALLIBURTON | Breaker, Corrosion Inhibitor, Friction Reducer, Iron Control Agent | Not Provided | Not Assigned | 1 | 0.00039 | 0 | |
Enter Chemical Name... | Not Assigned | 0 | 0 | 0 | ||||
Non-MSDS Components Not Provided by Supplier | Not Assigned | 0 | 0 | 0 | ||||
SP BREAKER | HALLIBURTON | Breaker | Sodium Persulfate | 007775-27-1 | 1 | 0.00002000 | 0 | |
Chlorine Dioxide | FOUNTAIN QUAIL | Anti-Bacterial Agent | Chlorine Dioxide | 10049-04-4 | 0.01 | 0 | 0 | |
15% HCl Acid | HALLIBURTON | Acid | Hydrochloric Acid | 7647-01-0 | 0.3 | 0.00365 | 0 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2018-08-11 | H2O | 15 | 194233 Gal | 200860 | Halliburton | STAGE 1/62
STAGES 2-60 SEE IMAGES |
2018-09-08 | H2O | 15 | 218062 Gal | 325660 | Halliburton | STAGE 62/62
STAGES 2-61 SEE IMAGES |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | CHESAPEAKE EXPLORATION LLC | 628034 | 0 | 29 |
2019 | EAP OHIO LLC | 920619 | 0 | 75 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | CHESAPEAKE EXPLORATION LLC | Brine | 0 | 0 |
2019 | EAP OHIO LLC | Brine | 18730 | 75 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1325927511 | 2020-9-21 0:00: | PW | No Violations | 0.50 |
-1397885549 | 2019-4-23 0:00: | PL | No Violations | 1.00 |
-1697077239 | 2018-8-9 0:00:0 | CT | No Violations | 1.00 |
-694469487 | 2018-7-13 0:00: | DD | No Violations | 1.00 |
-977684844 | 2018-8-14 0:00: | CT | No Violations | 2.00 |
0066727537 | 2018-06-26 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I witnessed Patterson 580 was drilling an 8.75 inch diameter hole at 6335 feet. Walk around inspection revealed no issues with containment. No flare during inspection. |
0217725251 | 2018-05-15 | Casing String Witnessed | No Violations | Pad address is 1136 township road 259, Richmond Ohio. On the day of my inspection I witnessed Express had augured a 26 inch diameter hole to 120 feet. 120 feet of 20 inch diameter conductor casing was run. Express was onsite with 230 sacks of class A cement. Additives include 2% CaCl and .5 lb./sack cello-flake. Cement weighed with mudscale at 15.6 ppg and yield of 1.18. 50 percent excess ran. Cement was displaced with 39 barrels of fresh water. No returns to surface. Cement fell back from ~30 to 60 feet after puming. Company man David Newman will tag cement after it solidifies and call me with results. Top out will be 5/15 or 5/16. |
0361714087 | 2018-07-27 | Completion Testing | No Violations | On the day of my inspection I witnessed 9 Energy running a CBL on the 1H. No frack crew onsite yet. Company man said they would be opening the toe valves on Monday. Surface and annular gauges read 0. |
0694469487 | 2018-07-13 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I witnessed wyonming casing running 5.5 inch diameter production casing. 23#/ft grade p-110. Well was drilled to a total depth of 21635. Kick off point was 8338 and landing point was 9329. this is the last well on this pad and rig will leave for Pennsylvania starting Monday. Cement job will be late tonight. |
0977684844 | 2018-08-14 | Completion Testing | No Violations | On the day of my inspection I witnessed a Halliburton frac crew rigged up on well. ID to company men Fletcher Brand and Rudy. Surface annular pressure is zero. Intermediate annular pressure is 289 psi. A composite plug is at 10560 and operator has a tractor with a mill on it coming out to try and mill the plug out. They fracked stage 1 and were setting plug for casing test. Plug failed and needs milled out. |
1044405085 | 2018-08-20 | Completion Testing | No Violations | On the day of my inspection I witnessed a Halliburton frac crew on site. ID to company men Rudy and Fletcher. Surface annular pressure is 0 and intermediate annular pressure is 216 psi, prior to frac. Last week they had brought a tractor on location that had a mill. They went down hole and milled out the center of the plug but did not get the slips. They anticipate bringing in Stone rig 15 or coiled tubing unit later in week to drill out the plug so they can continue fracking. |
1397885549 | 2019-04-23 | Preliminary Restoration | No Violations | On the day of my inspection I witnessed this pad to contain 3 producing wells. Production equipment includes three sand seperators, three GPUs, and six line heaters that are not plumbed in. Three 400 barrel steel produced water tanks are in their own containment. The 13.375x9.625 annular pressure is 0 psi and the 9.625x5.5 annular pressure is 1400 psi. The 9.625x5.5 annular is plumbed into a flowline. Pad slopes are stable and vegetated. Site meets requirements of 1509.072 (A) for preliminary restoration. |
1526474304 | 2018-05-16 | Casing String Witnessed | No Violations | On the day of my inspection I witnessed Superintenant David Newman tag cement at 68 feet from ground surface. Backside was grouted back to surface with approximately 8 yards of grout. |
1530542055 | 2018-07-02 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I witnessed Schlumberger pump an 800 foot plug with 25% excess (~1000 feet total). Bottom of plug is 6795 feet and top is estimated around 5800 feet. 28 barrels of 13.0 ppg mud push was pumped prior to 74.4 barrels of 17.5 ppg class H cement with .94 yield. Cement was followed with 12 barrels of 13 ppg mud push. Plug displaced with 102 barrels of oil based mud. This kick off plug was set because the rig lost a fish in the wellbore. Total depth drilled was 8340. Top of fish is at 6847 feet, fish is 1445 feet long and consists of 3 joints of drill pipe, 5 crossover subs, 2 antenna subs, 2 indexing tools, drill collars, MWD tool, shock sub, mud motor, and bit. |
1599754002 | 2020-8-31 0:00: | PW | No Violations | 0.50 |
1697077239 | 2018-08-09 | Completion Testing | No Violations | On the day of my inspection I found a Halliburton frac crew on location. ID to compnay man Dave. He said they should be starting to frac in the next day or two. Surface and intermediate annular pressures are zero. |
217725251 | 2018-5-15 0:00: | CS | No Violations | 1.00 |
361714087 | 2018-7-27 0:00: | CT | No Violations | 1.00 |
66727537 | 2018-6-26 0:00: | DD | No Violations | 1.00 |
For data sources see[10]