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34-083-20163

Well Details

Well ID: 34-083-20163
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Country: United States
State: Ohio
County: Knox
Municipality: Howard Township
Operator Name: MARAM ENERGY INC
Well Pad ID:
Farm/Lease Name: SIMPSON CHARLES & ZELLA
License Status: Producing
License Date: 2013-03-18
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1937-10-09
Well Total Depth: 2688.00 ft
Configuration: Vertical
Latitude: 40.420000
Longitude: -82.330000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1937-10-09 QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002
Reached Total Depth 1937-10-09 QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002
APP 1999-12-15 Proposed Formations:CLINTON, Issued Date:12/15/99, Expired Date:12/14/00 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2000-12-14 Proposed Formations:CLINTON, Issued Date:12/14/2000, Expired Date:12/14/2001 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2002-02-15 Proposed Formations:CLINTON, Issued Date:2/15/2002, Expired Date:2/15/2003 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2002-02-15 QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002
APP 2010-07-09 Proposed Formations:CLINTON, Issued Date:7/9/2010, Expired Date:7/9/2011 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2013-03-18 Proposed Formations:, Issued Date:3/18/2013, Expired Date:3/18/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2014-08-13 QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002
Construction Permit Expires 2015-03-18 QUAD=GAMBIER, RI, PLUG & ABAN 2/15/2002

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 PERKINS SIDNEY 0.00 0.00 0
2005 MARAM ENERGY INC 0.00 0.00 150
2006 MARAM ENERGY INC 0.00 0.00 0
2007 MARAM ENERGY INC 0.00 0.00 0
2008 MARAM ENERGY INC 0.00 0.00 0
2009 MARAM ENERGY INC 0.00 0.00 0
2010 MARAM ENERGY INC 0.00 0.00 0
2011 MARAM ENERGY INC 0.00 0.00 0
2012 MARAM ENERGY INC 0.00 0.00 0
2013 MARAM ENERGY INC 0.00 0.00 0
2014 MARAM ENERGY INC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 PERKINS SIDNEY Brine 0 0
2005 MARAM ENERGY INC Brine 0 150
2006 MARAM ENERGY INC Brine 0 0
2007 MARAM ENERGY INC Brine 0 0
2008 MARAM ENERGY INC Brine 0 0
2009 MARAM ENERGY INC Brine 0 0
2010 MARAM ENERGY INC Brine 0 0
2011 MARAM ENERGY INC Brine 0 0
2012 MARAM ENERGY INC Brine 0 0
2013 MARAM ENERGY INC Brine 0 0
2014 MARAM ENERGY INC Brine 90 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1022735037 2015-3-9 0:00:0 PB No Violations
-1395882410 2014-12-15 0:00 PB No Violations
-1839822235 2014-12-18 0:00 PW No Violations
-1911254236 2015-3-4 0:00:0 PB No Violations
-2020174091 2015-1-5 0:00:0 PB No Violations
-2065072911 2015-2-9 0:00:0 PB No Violations
-526820111 2015-3-16 0:00: PB No Violations
-965730803 2015-5-21 0:00: PB No Violations
0288328235 2015-01-06 Plug / Plug Back No Violations There was no one on site during this inspection. The service rig is setting idle on location.
0526820111 2015-03-16 Plug / Plug Back No Violations The service rig has moved off the well still needs more clay to finish the top of the plug, 8 inch cut off and well id plate.
0693655615 2015-03-12 Plug / Plug Back No Violations In the process of cutting off the drive pipe and welding on a 8 inch nipple to pull the surface casing went to get more clay to finish plugging the surface hole again the clay company has no clay they will try again tomorrow.
0958557686 2015-03-11 Plug / Plug Back No Violations Washing in clay from brush and stone plug to surface casing, preparing to pull 8 inch surface casing.
0965730803 2015-05-21 Plug / Plug Back No Violations Maram Energy moved their service rig back on location to finish plugging this well today.
0967225577 2015-06-02 Plug / Plug Back No Violations This well has finished being plugged, and the area has been reclaimed of all the production equipment has been removed, and all the debris have been cleaned up. The landowner is in the process of planting the area in crops as well.
1022735037 2015-03-09 Plug / Plug Back No Violations They are in the process of driving out a bridge that occurred when dropping in the stone for the brush and stone plug.
1029132993 2014-12-24 Plug / Plug Back No Violations Plugging with Maram Energy today pulling 3 inch after shooting it off.
1395882410 2014-12-15 Plug / Plug Back No Violations This well is in the process of being plugged and abandoned, the service rig is on site the pump jack has been removed the rods pulled, the pipe is scheduled to be shot off and pulled. This will also satisfy a prior compliance notice to plug this well once completed.
1398375250 2014-04-24 Final Restoration No Violations This inspection was for a final restoration. The well is still equipped with a pumping unit and a single tank. The well has not been produced for some time according to the production records on this well. The records also state this well was plugged in 2002. The well has no identification posted. The well needs to be plugged to be compliant with the law.
1426519591 2015-03-13 Plug / Plug Back No Violations Today they attempted to pull the 8 inch surface casing after several trys it is decided to leave the surface casing and plug to surface.
1491937034 2015-02-24 Plug / Plug Back No Violations Plugging operations are ongoing with this well the 3 inch has been recovered, the bottom hole clay plug has been set, the 5 inch production casing has been shot off at 1495 feet and the casing has been recovered.
1839822235 2014-12-18 Production Wells Violations Noted This well is in the process of being plugged and satisfies the Compliance Notice.
1909045638 2015-03-03 Plug / Plug Back No Violations Plugging operations were going on during this inspection clay was being washed in to finish the bottom plug after ripping and pulling the production casing.
1911254236 2015-03-04 Plug / Plug Back No Violations Plugging operations were on going. They were setting a brush and stone plug to finish washing the top plug after pulling the surface casing.
2020174091 2015-01-05 Plug / Plug Back No Violations Plugging operations are underway on this well the clay was delivered today. No one was on site during this inspection.
2065072911 2015-02-09 Plug / Plug Back No Violations I witnessed plugging operations on this well. Maram Energy plugging with clay. Approximately 230 shovels of clay were washed in. The 5.5 casing will be shot later this week. Refer to plug report for details. Time of inspection: 1:15 PM. Weather: 25 degrees F, Cloudy
288328235 2015-1-6 0:00:0 PB No Violations
693655615 2015-3-12 0:00: PB No Violations
958557686 2015-3-11 0:00: PB No Violations
967225577 2015-6-2 0:00:0 PB No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1839822235 US-OH-118372 2014-12-29 Failure to legibly identify well
1839822235 US-OH-118373 2014-12-29 Well shall be plugged

For data sources see[8]

References