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Well ID: 34-083-22949 | Loading map...
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Country: United States | |
State: Ohio | |
County: Knox | |
Municipality: Jefferson Township | |
Operator Name: LAKE REGION OIL INC | |
Well Pad ID: | |
Farm/Lease Name: CHASE JOSEPH | |
License Status: Final Restoration | |
License Date: 2005-07-05 | |
Spud Date: 1981-07-15 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-08-14 | |
Well Total Depth: 2953.00 ft | |
Configuration: Vertical | |
Latitude: 40.510000 | |
Longitude: -82.200000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-07-13 | 162 LAKE REGION OIL INC GeoDate 7/13/81 |
Original Spud | 1981-07-15 | |
Completed | 1981-08-14 | |
Reached Total Depth | 1981-08-14 | |
APP | 2005-07-05 | Proposed Formations:CLINTON, Issued Date:7/5/2005, Expired Date:7/5/2006 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2005-09-26 | |
Construction Permit Expires | 2006-07-05 | |
Record Last Modified | 2014-09-17 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 2874 | 2916 | 13 |
2874 | 2916 | 13 | |
2874 | 2916 | 13 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 74000 Gal | 30000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | LAKE REGION OIL INC | 763.00 | 214.00 | 365 |
1985 | LAKE REGION OIL INC | 730.00 | 274.00 | 365 |
1986 | LAKE REGION OIL INC | 577.00 | 262.00 | 365 |
1987 | LAKE REGION OIL INC | 498.00 | 164.00 | 365 |
1988 | LAKE REGION OIL INC | 367.00 | 88.00 | 365 |
1989 | LAKE REGION OIL INC | 252.00 | 89.00 | 365 |
1990 | LAKE REGION OIL INC | 136.00 | 108.00 | 365 |
1991 | LAKE REGION OIL INC | 158.00 | 86.00 | 365 |
1992 | LAKE REGION OIL INC | 225.00 | 89.00 | 365 |
1993 | LAKE REGION OIL INC | 90.00 | 86.00 | 365 |
1994 | LAKE REGION OIL INC | 0.00 | 0.00 | 365 |
1995 | LAKE REGION OIL INC | 127.00 | 76.00 | 365 |
1996 | LAKE REGION OIL INC | 0.00 | 0.00 | 365 |
1997 | LAKE REGION OIL INC | 96.00 | 186.00 | 365 |
1998 | LAKE REGION OIL INC | 0.00 | 0.00 | 365 |
1999 | LAKE REGION OIL INC | 0.00 | 0.00 | 365 |
2000 | LAKE REGION OIL INC | 0.00 | 0.00 | 365 |
2001 | LAKE REGION OIL INC | 0.00 | 0.00 | 365 |
2002 | LAKE REGION OIL INC | 0.00 | 0.00 | 365 |
2003 | LAKE REGION OIL INC | 0.00 | 0.00 | 365 |
2004 | LAKE REGION OIL INC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | LAKE REGION OIL INC | Brine | 0 | 365 |
1985 | LAKE REGION OIL INC | Brine | 115 | 365 |
1986 | LAKE REGION OIL INC | Brine | 137 | 365 |
1987 | LAKE REGION OIL INC | Brine | 158 | 365 |
1988 | LAKE REGION OIL INC | Brine | 148 | 365 |
1989 | LAKE REGION OIL INC | Brine | 114 | 365 |
1990 | LAKE REGION OIL INC | Brine | 145 | 365 |
1991 | LAKE REGION OIL INC | Brine | 45 | 365 |
1992 | LAKE REGION OIL INC | Brine | 152 | 365 |
1993 | LAKE REGION OIL INC | Brine | 50 | 365 |
1994 | LAKE REGION OIL INC | Brine | 0 | 365 |
1995 | LAKE REGION OIL INC | Brine | 0 | 365 |
1996 | LAKE REGION OIL INC | Brine | 0 | 365 |
1997 | LAKE REGION OIL INC | Brine | 0 | 365 |
1998 | LAKE REGION OIL INC | Brine | 70 | 365 |
1999 | LAKE REGION OIL INC | Brine | 0 | 365 |
2000 | LAKE REGION OIL INC | Brine | 0 | 365 |
2001 | LAKE REGION OIL INC | Brine | 0 | 365 |
2002 | LAKE REGION OIL INC | Brine | 0 | 365 |
2003 | LAKE REGION OIL INC | Brine | 0 | 365 |
2004 | LAKE REGION OIL INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1826641421 | 2005-8-22 0:00: | AM | No Violations | |
-469932998 | 2014-7-3 0:00:0 | FR | No Violations | |
-682145850 | 2005-9-15 0:00: | PB | No Violations | |
0321143491 | 2005-09-06 | Plug / Plug Back | No Violations | Bottom plug started. Lined pit constructed. 4 inch ripped at 2550. |
0469932998 | 2014-07-03 | Final Restoration | No Violations | All drilling and plugging equiptment have been removed from site. Vegetation and lease road have been restored. Previous well site is now in a woodland area. I was accompanied by inspector Brandon Mitchell during this inspection. Final restoration passes. |
0682145850 | 2005-09-15 | Plug / Plug Back | No Violations | 293 feet of cable line that broke was retrieved from hole. 8 inch cutting tools are still down the well. 8 inch pipe still needs to be removed and plugging finished. |
1074805641 | 2005-09-22 | Plug / Plug Back | No Violations | 8 inch being pulled, clay being washed in as joints being pulled. |
1117572870 | 2005-05-26 | Production Wells | Violations Noted | WELL PLUGGED BY FLAME ENERGY.Well is not being produced and appears to be incapable of production. Investigation taking place of nearby water well complaint on the Chase property. Inspection conducted with Jeff Fry and neighbor Mr. David Greer. |
1125585705 | 2005-09-01 | Plug / Plug Back | No Violations | Leonard Wanger has moved onto location to plug this well. GPS reading of tanks taken. |
1126179789 | 2005-09-07 | Plug / Plug Back | No Violations | All of 4 inch out. Bottom and Lime plug done. Preparing for brush and stone plug. |
1127142108 | 2005-09-19 | Plug / Plug Back | No Violations | 8 inch ripping tools have been retrieved out of hole. Broken cable is being replaced- may try to rip again by tomorrow. |
1127337251 | 2005-09-21 | Plug / Plug Back | No Violations | Still ripping 8 inch. Tanks being removed today by Mac Oil. |
1826641421 | 2005-08-22 | Administrative Inspection | No Violations | Received call from Bob Durbin of Lake Region Oil to inform me that plugging to start the week of 8/29/05. |
321143491 | 2005-9-6 0:00:0 | PB | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1117572870 | US-OH-102965 | 2005-05-31 | Failure to legibly identify well | |
1117572870 | US-OH-102966 | 2005-05-31 | Well shall be plugged |
For data sources see[9]