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Well ID: 34-083-23639 | Loading map...
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Country: United States | |
State: Ohio | |
County: Knox | |
Municipality: Union Township | |
Operator Name: CAMPHIRE GEORGE E. | |
Well Pad ID: | |
Farm/Lease Name: SAPP ROBERT & HELEN / BAER ALBERT | |
License Status: Producing | |
License Date: 1985-04-24 | |
Spud Date: 1985-04-29 | |
Spud Drilling Contractor: FERENBAUGH DRLG | |
Final Drill Date: 1985-05-28 | |
Well Total Depth: 2958.00 ft | |
Configuration: Vertical | |
Latitude: 40.460000 | |
Longitude: -82.250000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1985-04-24 | Issued Date 4/24/85 Expired Date 10/21/85 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 02958 Proposed Drill Depth 02958 |
Original Spud | 1985-04-29 | IP. OIL = 1/2 BBL |
Completed | 1985-05-28 | IP. OIL = 1/2 BBL |
Reached Total Depth | 1985-05-28 | IP. OIL = 1/2 BBL |
CO | 1985-07-16 | 2529 BCP ENERGY INC GeoDate 4/24/85 |
Completion Report Received | 1985-07-29 | IP. OIL = 1/2 BBL |
Construction Permit Expires | 1985-10-21 | IP. OIL = 1/2 BBL |
CO | 1994-01-07 | 230 UNION OIL CO GeoDate 4/24/85 |
Change of Owner | 2005-02-22 | Operator changed from 230, UNION OIL CO to 1499, CAMPHIRE DRILLING-GEORGE |
Record Last Modified | 2017-02-15 | IP. OIL = 1/2 BBL |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 2830 | 2900 | 0 |
2830 | 2900 | 0 | |
2006-09-11 | 2854 | 2897 | 15 |
2854 | 2897 | 15 | |
2830 | 2900 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 61800 Gal | 35000 | FRAC;H2O,SAND,N2 | ||
N2 | 0 | 200 Mscf | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | GEO ENERGY INC | 3997.00 | 336.00 | 217 |
1986 | BCP ENERGY INC | 1064.00 | 53.00 | 82 |
1987 | BCP ENERGY INC | 4567.00 | 225.00 | 363 |
1988 | BCP ENERGY INC | 3312.00 | 91.00 | 365 |
1989 | BCP ENERGY INC | 2264.00 | 93.00 | 365 |
1990 | BCP ENERGY INC | 1844.00 | 84.00 | 365 |
1991 | BCP ENERGY INC | 1703.00 | 88.00 | 365 |
1992 | BCP ENERGY INC | 1640.00 | 35.00 | 365 |
1993 | BCP ENERGY INC | 1322.00 | 47.00 | 365 |
1994 | UNION OIL CO | 0.00 | 27.00 | 365 |
1995 | UNION OIL CO | 1020.00 | 0.00 | 365 |
1996 | UNION OIL CO | 749.00 | 40.00 | 365 |
1997 | UNION OIL CO | 695.00 | 40.00 | 250 |
1998 | UNION OIL CO | 664.00 | 0.00 | 90 |
1999 | UNION OIL CO | 387.00 | 0.00 | 90 |
2000 | UNION OIL CO | 437.00 | 37.00 | 250 |
2001 | UNION OIL CO | 0.00 | 0.00 | 60 |
2002 | UNION OIL CO | 316.00 | 0.00 | 225 |
2003 | UNION OIL CO | 168.00 | 36.00 | 110 |
2004 | UNION OIL CO | 175.00 | 0.00 | 125 |
2005 | CAMPHIRE GEORGE E. | 4.00 | 0.00 | 0 |
2006 | CAMPHIRE GEORGE E. | 0.00 | 30.00 | 156 |
2007 | CAMPHIRE GEORGE E. | 0.00 | 26.00 | 156 |
2008 | CAMPHIRE GEORGE E. | 104.00 | 36.00 | 365 |
2009 | CAMPHIRE GEORGE E. | 0.00 | 0.00 | 0 |
2010 | CAMPHIRE GEORGE E. | 214.00 | 0.00 | 0 |
2011 | CAMPHIRE GEORGE E. | 248.00 | 0.00 | 0 |
2012 | CAMPHIRE GEORGE E. | 143.00 | 0.00 | 0 |
2013 | CAMPHIRE GEORGE E. | 116.00 | 0.00 | 365 |
2014 | CAMPHIRE GEORGE E. | 155.00 | 0.00 | 365 |
2015 | CAMPHIRE GEORGE E. | 0.00 | 0.00 | 365 |
2016 | CAMPHIRE GEORGE E. | 0.00 | 0.00 | 365 |
2017 | CAMPHIRE GEORGE E. | 0.00 | 0.00 | 365 |
2018 | CAMPHIRE GEORGE E. | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | GEO ENERGY INC | Brine | 170 | 217 |
1986 | BCP ENERGY INC | Brine | 0 | 82 |
1987 | BCP ENERGY INC | Brine | 58 | 363 |
1988 | BCP ENERGY INC | Brine | 0 | 365 |
1989 | BCP ENERGY INC | Brine | 0 | 365 |
1990 | BCP ENERGY INC | Brine | 0 | 365 |
1991 | BCP ENERGY INC | Brine | 0 | 365 |
1992 | BCP ENERGY INC | Brine | 0 | 365 |
1993 | BCP ENERGY INC | Brine | 0 | 365 |
1994 | UNION OIL CO | Brine | 5 | 365 |
1995 | UNION OIL CO | Brine | 5 | 365 |
1996 | UNION OIL CO | Brine | 8 | 365 |
1997 | UNION OIL CO | Brine | 15 | 250 |
1998 | UNION OIL CO | Brine | 5 | 90 |
1999 | UNION OIL CO | Brine | 5 | 90 |
2000 | UNION OIL CO | Brine | 5 | 250 |
2001 | UNION OIL CO | Brine | 0 | 60 |
2002 | UNION OIL CO | Brine | 50 | 225 |
2003 | UNION OIL CO | Brine | 20 | 110 |
2004 | UNION OIL CO | Brine | 10 | 125 |
2005 | UNION OIL CO | Brine | 0 | 30 |
2006 | CAMPHIRE GEORGE E. | Brine | 0 | 156 |
2007 | CAMPHIRE GEORGE E. | Brine | 17 | 156 |
2008 | CAMPHIRE GEORGE E. | Brine | 0 | 365 |
2009 | CAMPHIRE GEORGE E. | Brine | 0 | 0 |
2010 | CAMPHIRE GEORGE E. | Brine | 0 | 0 |
2011 | CAMPHIRE GEORGE E. | Brine | 0 | 0 |
2012 | CAMPHIRE GEORGE E. | Brine | 0 | 0 |
2013 | CAMPHIRE GEORGE E. | Brine | 0 | 365 |
2014 | CAMPHIRE GEORGE E. | Brine | 0 | 365 |
2015 | CAMPHIRE GEORGE E. | Brine | 0 | 365 |
2016 | CAMPHIRE GEORGE E. | Brine | 0 | 365 |
2017 | CAMPHIRE GEORGE E. | Brine | 0 | 365 |
2018 | CAMPHIRE GEORGE E. | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1900899768 | 2018-3-15 0:00: | PW | No Violations | |
-878760767 | 2018-3-13 0:00: | PW | No Violations | |
000PL14568 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0347258912 | 2018-10-23 | Production Wells | No Violations | Follow up inspection for compliance notice 2004341609. This well is being worked over and repaired and put back into production. The rods and tubing were pulled and repaired today. There were no issues to note during this inspection. |
0878760767 | 2018-03-13 | Production Wells | No Violations | Follow up inspection for 1575643656. Proper identification is still not posted at this well. I called and talked with George Camphire and he said he just got the notice and would have it up by weeks end. |
1535466638 | 2018-08-28 | Production Wells | No Violations | Follow up for inspection 2004341609. I talked with George Camphire and he said he is going to try and fix this well and get it back to producing again. I agreed to extend the notice remedy date to 10-29-2018 |
1575643656 | 2018-02-28 | Production Wells | Violations Noted | This well is a production well. There is not proper identification posted for this well. There needs to be proper identification posted at the well according to what the law requires to be in compliance with the law. |
1900899768 | 2018-03-15 | Production Wells | No Violations | Follow up for inspection 1575643656. Proper identification has been posted for this well. |
2004341609 | 2018-02-28 | Production Wells | Violations Noted | This well is a production well. The production reporting for this well indicate that there has not been anything produced for the past three (3) years. This well needs to be plugged for failure to produce. CAMPHIRE GEORGE E shall submit a written plugging schedule to Mark A. McCombs at 1656 Eagle Way Ashland Ohio 44805-within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. CAMPHIRE GEORGE E will be notified if the plugging schedule is approved or denied. |
2028424166 | 2018-10-25 | Production Wells | No Violations | This well has been put back into production. There is 100 pounds of gas pressure at the well head leaving to the sales line. The area has been cleaned up. There were no issues observed during this inspection. |
347258912 | 2018-10-23 0:00 | PW | No Violations | |
PL14568 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1575643656 | US-OH-115398 | 2018-03-08 | 9-9-05(A)10 | Failure to legibly identify well |
2004341609 | US-OH-120337 | 2018-03-08 | NONE | Well shall be plugged |
For data sources see[9]