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Well ID: 34-083-24627 | Loading map...
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Country: United States | |
State: Ohio | |
County: Knox | |
Municipality: Morgan Township | |
Operator Name: ARTEX OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: BRANSTOOL | |
License Status: Producing | |
License Date: 2014-10-15 | |
Spud Date: 2014-12-05 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2015-01-19 | |
Well Total Depth: 4532.00 ft | |
Configuration: Vertical | |
Latitude: 40.260000 | |
Longitude: -82.420000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2014-10-15 | Proposed Formations:KNOX, Issued Date:10/15/2014, Expired Date:10/14/2016 12:00:00 PM, Drilling unit acres:56, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2015-01-19 | |
Completion Report Received | 2015-06-29 | |
Construction Permit Expires | 2016-10-14 | |
Record Last Modified | 2017-10-23 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2015-11-02 | 4421 | 4455 | 52 |
4421 | 4455 | 52 | |
4421 | 4455 | 52 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2015-01-13 | ACID | 15 | 3000 Gal | 0 | Producers Service Corporation |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2015 | ARTEX OIL COMPANY | 19616.00 | 53.00 | 245 |
2016 | ARTEX OIL COMPANY | 22766.00 | 30.00 | 365 |
2017 | ARTEX OIL COMPANY | 12823.00 | 36.00 | 365 |
2018 | ARTEX OIL COMPANY | 6900.00 | 29.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2015 | ARTEX OIL COMPANY | Brine | 333 | 245 |
2016 | ARTEX OIL COMPANY | Brine | 601 | 365 |
2017 | ARTEX OIL COMPANY | Brine | 579 | 365 |
2018 | ARTEX OIL COMPANY | Brine | 470 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1770320129 | 2014-12-9 0:00: | DD | No Violations | |
-979135555 | 2014-12-12 0:00 | DD | No Violations | |
0275205746 | 2014-10-19 | Drill / Deepen / Reopen | No Violations | Inspected this new location today crop area is cleared off around the stake. Preparing to build location. |
0625898663 | 2014-12-06 | Casing String Witnessed | No Violations | The operator requested an inspection to witness surface casing cement. See the casing ticket for details. |
0979135555 | 2014-12-12 | Drill / Deepen / Reopen | No Violations | Drilling operations are ongoing, running 4 1/2 production casing today, Petroset Cementing Services Inc. on site to cement in the long string. |
1417786245 | 2014-12-05 | Administrative Inspection | No Violations | Contacted by operator with moring report: The Kilbarger Rig 1 was moved onto location on December 4, 2014 and drilling commenced at 6:30 pm. The hole for the surface casing was t 265 feet. The cementing of the surface casing is anticipated to be on Saturday monring. |
1418135568 | 2014-12-08 | Administrative Inspection | No Violations | Contacted by operator to report drilling is at a depth of 2157 feet. Drilling has been shut down due to artesian flow on the back-side of the 8 5/8 inch surface casing. The artesian flow started after the surface casing was set and cemented and as a result of heavy rain fall. The artesian flow was washing sand out from the casing and put the rig at risk of collapsing. The depth was estimated to be about 40 to 50 feet. The operator was granted authorization to fill the void with 9 bag grout. Contacted by the operator when the job was completed and reported the water was shut off with 5.5 cubic yards of 9 bag grout. Cement held at the surface. |
1421078694 | 2015-01-05 | Production Wells | No Violations | The location is being reclaimed, preparations are being made to stimulate this well with acid to bring it on line. |
1434122447 | 2015-06-12 | Preliminary Restoration | No Violations | This well is in production as a rabbit well. The area is reclaimed, crops planted, and the pits have been dusted in and closed. |
1658240802 | 2014-12-10 | Drill / Deepen / Reopen | No Violations | Drilling operations are ongoing, they are 3750 feet deep with the construction of the main bore of this well. |
1770320129 | 2014-12-09 | Drill / Deepen / Reopen | No Violations | Drilling operations are ongoing, they are 2795 feet deep with the construction of the main bore of this well. |
275205746 | 2014-10-19 0:00 | DD | No Violations | |
625898663 | 2014-12-6 0:00: | CS | No Violations | 5.00 |
For data sources see[9]