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34-083-61448

Well Details

Well ID: 34-083-61448
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Country: United States
State: Ohio
County: Holmes
Municipality: Knox Township
Operator Name: W H PATTEN DRILLING CO
Well Pad ID:
Farm/Lease Name: HELEN WIGTON
License Status: Final Restoration
License Date: 2018-08-30
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 40.530000
Longitude: -82.180000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2018-08-30 Proposed Formations:CLINTON, Issued Date:8/30/2018, Expired Date:8/29/2020 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2019-01-09 UPDATE LOCATION PER DOGRM SURVEYOR 1/9/19 ALE.
Construction Permit Expires 2020-08-29 UPDATE LOCATION PER DOGRM SURVEYOR 1/9/19 ALE.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1998 W H PATTEN DRILLING CO 198.00 0.00 365
1999 W H PATTEN DRILLING CO 35.00 192.00 365
2000 W H PATTEN DRILLING CO 0.00 29.00 365
2001 W H PATTEN DRILLING CO 69.00 0.00 365
2002 W H PATTEN DRILLING CO 273.00 0.00 365
2003 W H PATTEN DRILLING CO 116.00 0.00 365
2004 W H PATTEN DRILLING CO 130.00 0.00 365
2005 W H PATTEN DRILLING CO 161.00 0.00 365
2006 W H PATTEN DRILLING CO 196.00 0.00 365
2007 W H PATTEN DRILLING CO 63.00 0.00 365
2008 W H PATTEN DRILLING CO 36.00 0.00 365
2009 W H PATTEN DRILLING CO 43.00 0.00 365
2010 W H PATTEN DRILLING CO 22.00 0.00 365
2012 W H PATTEN DRILLING CO 124.00 0.00 366
2013 W H PATTEN DRILLING CO 88.00 0.00 365
2014 W H PATTEN DRILLING CO 98.00 0.00 365
2015 W H PATTEN DRILLING CO 71.00 0.00 365
2016 W H PATTEN DRILLING CO 51.00 0.00 365
2017 W H PATTEN DRILLING CO 73.00 0.00 365
2018 W H PATTEN DRILLING CO 26.00 0.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1998 W H PATTEN DRILLING CO Brine 0 365
1999 W H PATTEN DRILLING CO Brine 0 365
2000 W H PATTEN DRILLING CO Brine 185 365
2001 W H PATTEN DRILLING CO Brine 198 365
2002 W H PATTEN DRILLING CO Brine 390 365
2003 W H PATTEN DRILLING CO Brine 0 365
2004 W H PATTEN DRILLING CO Brine 245 365
2005 W H PATTEN DRILLING CO Brine 130 365
2006 W H PATTEN DRILLING CO Brine 130 365
2007 W H PATTEN DRILLING CO Brine 147 365
2008 W H PATTEN DRILLING CO Brine 190 365
2009 W H PATTEN DRILLING CO Brine 166 365
2010 W H PATTEN DRILLING CO Brine 120 365
2012 W H PATTEN DRILLING CO Brine 192 366
2013 W H PATTEN DRILLING CO Brine 0 365
2014 W H PATTEN DRILLING CO Brine 220 365
2015 W H PATTEN DRILLING CO Brine 113 365
2016 W H PATTEN DRILLING CO Brine 197 365
2017 W H PATTEN DRILLING CO Brine 0 365
2018 W H PATTEN DRILLING CO Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1038871266 2018-8-15 0:00: PB No Violations
-1218451416 2018-8-13 0:00: PB No Violations
-1300940614 2018-8-7 0:00:0 PB No Violations
-1523527502 2018-10-17 0:00 FR No Violations
-382731266 2018-8-10 0:00: PB No Violations
-640042884 2018-8-17 0:00: PB No Violations
0034256661 2018-01-22 Production Wells No Violations Follow up for inspection 1690952392. I called Bill Patton of W H Patten Drilling Co and discussed the plugging of this well and that this violation remedy date is past due. The location of the well is in an area the is not easy to access and road conditions are making it hard to access. The remedy date has been extended to 3/06/2018.
0223150517 2018-08-09 Plug / Plug Back No Violations Plugging operations continue with the plugging of this well. Today the tubing was ran back in to the bottom to prepare to set the bottom hole plug.
0382731266 2018-08-10 Plug / Plug Back No Violations Plugging operations continue with the plugging of this well. Petroset Cementing Services Inc. was on site to set the bottom hole Clinton cement plug today.
0415534575 2018-08-08 Plug / Plug Back No Violations Plugging operations continue with the plugging of this well. Today the tubing was Steamed and cleaned to prepare it to run back in the well to set the bottom hole plug.
0640042884 2018-08-17 Plug / Plug Back No Violations Plugging operations on this well have concluded. They are in the process of removing the production equipment and reclaiming the well location.
1038871266 2018-08-15 Plug / Plug Back No Violations Plugging operations continue with this well. Today another 8.5 tons of prepared clay was washed in to finish plugging this well to ground level. The well was cut off 3 feet below the ground level and identification was added and the well was covered.
1081446534 2004-04-08 Production Wells No Violations WELL HAS PUMP JACK AND PRODUCTION LINES ON IT NEAR TANKS. WIFTON #1? WELL DOES NOT HAVE PROPER ID.
1126323135 2017-09-19 Production Wells No Violations There has been no change in the status of this well since the Compliance notice was written. I called Billy Patten of Patten Drilling Company and he stated he did not receive the notice. I called the office and they were sent to the wrong address. The remedy date is there fore extended until 3/21/2018
1218451416 2018-08-13 Plug / Plug Back No Violations Plugging operations continue with the plugging of this well. The 4 1/2 production casing was ripped at 1927 feet and pulled on 8/10/2018. Today a 7 inch precast plug was set at 827 feet on the 7 inch seat. They removed the production casing from location to prepare for the clay delivery to finish plugging this well.
1300940614 2018-08-07 Plug / Plug Back No Violations Matheny Well Service has moved in on this well to begin plugging operations. Today they pulled the rods and tubing from the well.
1536161247 2018-09-05 Final Restoration No Violations The area has been reclaimed, all the production equipment removed that was not associated with another well that was on the property. The area has been reseeded and is growing young vegetation.
1690952392 2017-07-24 Production Wells Violations Noted This well is listed as a Historic well, but has W H Patten Drilling Co identification on the pump jack and the tank batteries.. They have other wells in this location as well. This well needs to be registered, and produced or plugged. The pump jack is missing a motor and the well has not been produced for some time. The well owner/operator shall submit a written plugging schedule to Mark McCombs at 116 East High Street Mt Vernon, Ohio 43050-3402 within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
1692112371 2018-2-16 0:00: PL No Violations
1991129509 2018-08-14 Plug / Plug Back No Violations Plugging operations continue with the plugging of this well. Today they washed in 12.5 tons of prepared clay to continue with the plugging of this well.
223150517 2018-8-9 0:00:0 PB No Violations
34256661 2018-1-22 0:00: PW No Violations
415534575 2018-8-8 0:00:0 PB No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1690952392 US-OH-116761 2019-02-11 9-9-02 General Safety
1690952392 US-OH-116762 2019-02-11 NONE Well shall be plugged
1690952392 US-OH-116763 2019-02-11 NONE9 Failure to register/obtain or maintain bond/insurance

For data sources see[7]

References