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Well ID: 34-085-21266 | Loading map...
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Country: United States | |
State: Ohio | |
County: Lake | |
Municipality: Concord Township | |
Operator Name: DAVID OIL COMPANY LLC | |
Well Pad ID: | |
Farm/Lease Name: LOLA | |
License Status: Producing | |
License Date: 2008-02-27 | |
Spud Date: 2008-11-23 | |
Spud Drilling Contractor: GREAT PLAINS EXPLORATION LLC | |
Final Drill Date: 2008-12-03 | |
Well Total Depth: 3379.00 ft | |
Configuration: Vertical | |
Latitude: 41.660000 | |
Longitude: -81.290000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2008-02-27 | Proposed Formations:CLINTON, Issued Date:2/27/2008, Expired Date:2/26/2009 6:00:00 AM, Drilling unit acres:20.584, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2008-12-03 | |
Construction Permit Expires | 2009-02-26 | |
Completion Report Received | 2009-06-17 | |
Change of Owner | 2016-12-14 | Operator changed from 7909, JOHN D OIL & GAS COMPANY to 9836, DAVID OIL COMPANY LLC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2009-08-18 | 3172 | 3193 | 28 |
3172 | 3193 | 28 | |
3172 | 3193 | 28 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
GAS | 0 | 751 Mscf | 100000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2009 | JOHN D OIL & GAS COMPANY | 26534.00 | 0.00 | 168 |
2010 | JOHN D OIL & GAS COMPANY | 12827.00 | 0.00 | 365 |
2011 | JOHN D OIL & GAS COMPANY | 6340.00 | 0.00 | 365 |
2012 | JOHN D OIL & GAS COMPANY | 6639.00 | 0.00 | 366 |
2013 | JOHN D OIL & GAS COMPANY | 7303.00 | 0.00 | 365 |
2014 | JOHN D OIL & GAS COMPANY | 6704.00 | 0.00 | 365 |
2015 | JOHN D OIL & GAS COMPANY | 6653.00 | 0.00 | 365 |
2016 | DAVID OIL COMPANY LLC | 0.00 | 0.00 | 61 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2009 | JOHN D OIL & GAS COMPANY | Brine | 2780 | 168 |
2010 | JOHN D OIL & GAS COMPANY | Brine | 1980 | 365 |
2011 | JOHN D OIL & GAS COMPANY | Brine | 1200 | 365 |
2012 | JOHN D OIL & GAS COMPANY | Brine | 480 | 366 |
2013 | JOHN D OIL & GAS COMPANY | Brine | 320 | 365 |
2014 | JOHN D OIL & GAS COMPANY | Brine | 320 | 365 |
2015 | JOHN D OIL & GAS COMPANY | Brine | 240 | 365 |
2016 | JOHN D OIL & GAS COMPANY | Brine | 0 | 304 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1230841878 | 2017-12-13 0:00 | UP | No Violations | 0.50 |
-1411910014 | 2019-11-19 0:00 | UP | No Violations | |
-1907359627 | 2016-2-26 0:00: | UP | No Violations | 0.50 |
-310729679 | 2009-9-28 0:00: | PL | No Violations | |
0310729679 | 2009-09-28 | Preliminary Restoration | No Violations | Preliminary restoration was completed. Service rig was on the well. |
0676730784 | 2010-04-23 | Preliminary Restoration | No Violations | Preliminary restoration was completed and acceptable. |
1230841878 | 2017-12-13 | UrbanProduction Wells | No Violations | I inspected this well as a follow-up to a previously-issued compliance notice for the following deficiencies: The load lines were not locked and secure, there was no low-pressure relief valve, spark arrestor, or carbon filter, the wellhead enclosure was partially torn down. At the time of this inspection, I observed the following: The noted deficiencies remained. In addition, the unit ID signage remained not updated since the change in ownership in 2016. I had previously contacted the company about the deficiencies and they had reported various issues regarding lack of personnel and funds preventing them from being in compliance. |
1231249304 | 2008-11-25 | Drill / Deepen / Reopen | No Violations | cementing surface |
1355518282 | 2012-11-26 | UrbanProduction Wells | No Violations | The unit is comprised of a production wellhead fitted with a mechanical plunger lift, enclosed within a 6-foot wood, board-on-board fence. The |
1355858759 | 2012-11-26 | UrbanProduction Wells | No Violations | The unit consists of a 2-tank battery (TB) with mechanical seperator enclosed in a 8-foot wooden fence. The spacing is in accordance with the rule, and the valving and mechanicals are in good repair. I did not observe any signs of leaking product or gas vapors. The wellhead is fitted with a mechanical plunger lift. The tank battery dike is adequate. Locks and ID are good. No violations noted. |
1406653862 | 2014-07-29 | UrbanProduction Wells | No Violations | I inspected this producing unit as part of routine inspection activity. The well was completed in 12/03/2008. The unit is producing and production reports are current. Elements of the well consist of a production wellhead with standard valve assembly and mechanical plunger lift system. The wellhead is located down an access road which is a continuation of the residential driveway that serves 9546 Johnnycake. The access portion is graveled and in reasonable condition. There are no signs of leakage or problems at the wellhead. The aboveground storage tank battery is located via the same access road, and is 50 feet north of the wellhead. The battery is comprised of a total of 2 steel 140-barrel production tanks, and horizontal separator. Spacing from well to battery, and spacing of elements within the battery meet regulations. The battery is located in a separate board-on-board enclosure which is gated and locked. The load-outs are bull-plugged. The secondary containment at the battery appears well maintained. I did not observe any signs or evidence of leakage, spills, or problems. There is ID signage at the battery but is not visible from the outside. I notified John D Oil about the sign. |
1798792332 | 2017-06-16 | UrbanProduction Wells | No Violations | I inspected this well location as a follow-up to a previous inspection and associated Compliance Notice issued for missing locks and missing spark arrestor, low-pressure relief valve and carbon filter, and lack of exposed and gauged surface casing required under special permit condition. At the time of this inspection, these deficiencies remain. The company has pledged on a repeated basis to remedy the problems but have not acted as of this date. |
1907359627 | 2016-02-26 | UrbanProduction Wells | Violations Noted | I inspected this well as part of routine inspection activity. At the time of this inspection, I observed the following elements: a wellhead with mechanical plunger lift system and tank battery comprised of two 100-barrel steel tanks, and mechanical separator located in separate board-on-board enclosures. Enclosure gates were not locked or secure. The wellhead enclosure was observed to be partially torn down. Fittings and connections were bull-plugged but not locked. Low-pressure relief valve, spark arrestor, and carbon filter were not present. Fittings and c connections at the wellhead were secure and free from signs of leakage or problems. The 8.625-inch surface casing is exposed but not gauged as required under specific permit conditions. The owner must remedy the following by 04/01/2016: secure the load-line valves and enclosure gates with locks. Properly gauge the 8.625-inch surface casing as required by permit condition. Repair the wellhead enclosure. Fit the production tank with low-pressure relief valve, spark arrestor, and carbon filter as required. Contact Inspector Stephen Tompkins at 330-907-4647 with questions regarding this inspection. |
676730784 | 2010-4-23 0:00: | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1907359627 | US-OH-119187 | 2016-04-27 | FENCING (a-d) | |
1907359627 | US-OH-119188 | 2016-04-27 | LOCKS | |
1907359627 | US-OH-119189 | 2016-04-27 | TANKS (a-i) |
For data sources see[9]