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| Well ID: 34-089-21157 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Licking | |
| Municipality: Madison Township | |
| Operator Name: MORAN RONALD F | |
| Well Pad ID: | |
| Farm/Lease Name: BAKER | |
| License Status: Plugged and Abandoned | |
| License Date: 2006-04-06 | |
| Spud Date: 1954-12-09 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1954-12-14 | |
| Well Total Depth: 600.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.040000 | |
| Longitude: -82.320000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Original Spud | 1954-12-09 | |
| Completed | 1954-12-14 | |
| Reached Total Depth | 1954-12-14 | |
| CO | 1993-05-13 | 269 PHILLIPS MARGARET E |
| CO | 1993-05-13 | 565 MORAN RONALD F GeoDate |
| APP | 2006-04-06 | Proposed Formations:BEREA, Issued Date:4/6/2006, Expired Date:4/6/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
| Construction Permit Expires | 2007-04-06 | |
| Record Last Modified | 2014-07-10 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2006-09-11 | 578 | 587 | 0 |
| 578 | 587 | 0 | |
| 578 | 587 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| ACID | 0 | 50 Qts | 0 |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1993 | PHILLIPS MARGARET E | 0.00 | 0.00 | 0 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1993 | PHILLIPS MARGARET E | Brine | 0 | 0 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1401665923 | 2017-8-4 0:00:0 | FR | No Violations | 0.50 |
| -1640381894 | 2006-10-30 0:00 | PB | No Violations | |
| -1743919141 | 2019-11-26 0:00 | FR | No Violations | 0.10 |
| -2067280132 | 2012-2-9 0:00:0 | FR | No Violations | |
| -32944183 | 2006-10-10 0:00 | PB | No Violations | |
| -932130702 | 2017-9-21 0:00: | FR | No Violations | 0.50 |
| 0032944183 | 2006-10-10 | Plug / Plug Back | No Violations | Witnessed plugging with new Licking Co Inspector Will Ziegler. Spoke with Don , Tom and Hoss Nethers. Oil was bailed from hole before plugging began. 10 tons put in hole and all of the 6 inch was retrieved per phone discussion with Tom Nethers on 10/11/06. Due to weather/site location, plugging will continue next week. |
| 0932130702 | 2017-09-21 | Final Restoration | No Violations | The company was verbally advised to have the casing cut down below grade and the final restoration complete by 10/23/2017. An inspection will be conducted that week to check on the final restoration status. |
| 0977363158 | 2007-05-07 | Plug / Plug Back | No Violations | Jeff Fry and I inspected the well location. It appears that this well has been plugged. There is no visible well on the surface and there is clay and other indicators on location that would suggest that it has been recently plugged. I will inquire with Gary Nethers about this and have him fill out a plugging report if it is indeed plugged. |
| 1401665923 | 2017-08-04 | Final Restoration | No Violations | This inspection was conducted as a status check. The casing could not be found during the inspection. After speaking to the landowner I was advised that the casing has not been cut down. Another inspection will be conducted to find the casing and the company will then be notified to have it cut down below grade. Time of inspection: 8:45 AM. |
| 1502111477 | 2017-08-07 | Final Restoration | No Violations | This inspection was conducted as a status check. The casing was found and has not been cut down below grade. Time of inspection: 8:30 AM. Weather: 61*F, Overcast |
| 1640381894 | 2006-10-30 | Plug / Plug Back | No Violations | Jeff Fry and I stopped by this location today to check on the plugging operations. Nethers rig was on location but they were not there actively plugging. |
| 2067280132 | 2012-02-09 | Final Restoration | No Violations | During my inspection I completed a final restoration status check. The status on this well says it is a producing well but was in fact plugged. The casing has not been cut down below surface and there is oil field debris around the casing. Final restoration is not finished. |
| 977363158 | 2007-5-7 0:00:0 | PB | No Violations |
For data sources see[9]