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Well ID: 34-089-21944 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Fallsbury Township | |
Operator Name: H & D DRILLING CO INC | |
Well Pad ID: | |
Farm/Lease Name: GRADEN THOMAS | |
License Status: Final Restoration | |
License Date: 2015-11-03 | |
Spud Date: 1962-06-27 | |
Spud Drilling Contractor: | |
Final Drill Date: 1962-07-27 | |
Well Total Depth: 3085.00 ft | |
Configuration: Vertical | |
Latitude: 40.220000 | |
Longitude: -82.260000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1962-06-27 | CHANGED STATUS FROM PR TO FR PER INSPECTOR BRANDON MITCHELL FACILITY REPORT DATED 3/6/2015 ON 3/12/2015 CM. |
Completed | 1962-07-27 | CHANGED STATUS FROM PR TO FR PER INSPECTOR BRANDON MITCHELL FACILITY REPORT DATED 3/6/2015 ON 3/12/2015 CM. |
Reached Total Depth | 1962-07-27 | CHANGED STATUS FROM PR TO FR PER INSPECTOR BRANDON MITCHELL FACILITY REPORT DATED 3/6/2015 ON 3/12/2015 CM. |
CO | 1988-06-07 | 994 LINCOLN OIL WELL SERVICE GeoDate 6/7/88 |
Unknown | 1988-06-07 | Issued Date 6/7/88 Expired Date 6/7/89 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Change of Owner | 2015-10-19 | Operator changed from 994, LINCOLN OIL WELL SERVICE to 401, H & D DRILLING CO INC |
APP | 2015-11-03 | Proposed Formations:CLINTON, Issued Date:11/3/2015, Expired Date:11/2/2017 12:00:00 PM, Drilling unit acres:150, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged/Abandoned | 2016-11-10 | CHANGED STATUS FROM PR TO FR PER INSPECTOR BRANDON MITCHELL FACILITY REPORT DATED 3/6/2015 ON 3/12/2015 CM. |
Record Last Modified | 2017-02-17 | CHANGED STATUS FROM PR TO FR PER INSPECTOR BRANDON MITCHELL FACILITY REPORT DATED 3/6/2015 ON 3/12/2015 CM. |
Construction Permit Expires | 2017-11-02 | CHANGED STATUS FROM PR TO FR PER INSPECTOR BRANDON MITCHELL FACILITY REPORT DATED 3/6/2015 ON 3/12/2015 CM. |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 900 Bbl | 28000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | LINCOLN OIL WELL SERVICE | 0.00 | 377.00 | 0 |
1985 | LINCOLN OIL WELL SERVICE | 0.00 | 183.00 | 0 |
1986 | LINCOLN OIL WELL SERVICE | 0.00 | 0.00 | 365 |
1987 | LINCOLN OIL WELL SERVICE | 0.00 | 0.00 | 360 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | LINCOLN OIL WELL SERVICE | Brine | 40 | 0 |
1985 | LINCOLN OIL WELL SERVICE | Brine | 22 | 0 |
1986 | LINCOLN OIL WELL SERVICE | Brine | 0 | 365 |
1987 | LINCOLN OIL WELL SERVICE | Brine | 80 | 360 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2090461568 | 2016-11-3 0:00: | DD | No Violations | |
-558976903 | 2015-3-6 0:00:0 | FR | No Violations | |
0558976903 | 2015-03-06 | Final Restoration | No Violations | This inspection was conducted as a final restoration status check. The location was inspected using coordinates from RBDMS. The well appears to have been plugged. No well or surface equipment was found. Inspection meets ORC 1509.072 requirements. Time of inspection: 10:00 AM. Weather: 23*F, Sunny, 6 snow |
2090461568 | 2016-11-03 | Drill / Deepen / Reopen | No Violations | H & D Drilling has moved in and rigged up. The well has been spudded. H & D Drilling is in the process of reopening this well to the Clinton Sand. Mark Donaker informed me that they hit an obstruction at approximately 120. It was revealed that when the well was plugged the 7 diameter casing was rotted off at that depth. H & D Drilling has attempted to get their tools inside the 7 but was unsuccessful. Mark Donaker said they will probably be plugging the well. |
For data sources see[8]