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Well ID: 34-089-22541 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Perry Township | |
Operator Name: SEIBERT JAMES G | |
Well Pad ID: | |
Farm/Lease Name: MILLS WILBUR | |
License Status: Producing | |
License Date: 1997-04-11 | |
Spud Date: 1967-08-08 | |
Spud Drilling Contractor: CO TOOLS | |
Final Drill Date: 1967-10-21 | |
Well Total Depth: 3007.00 ft | |
Configuration: Vertical | |
Latitude: 40.150000 | |
Longitude: -82.260000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1967-08-08 | 1165 SEIBERT CHARLES J GeoDate 8/8/67 |
Original Spud | 1967-08-08 | |
Completed | 1967-10-21 | |
Reached Total Depth | 1967-10-21 | |
Completion Report Received | 1968-01-02 | |
Unknown | 1997-04-11 | Issued Date 4/11/97 Expired Date 4/11/98 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1998-04-11 | |
Change of Owner | 2004-07-19 | Operator changed from 1165, SEIBERT CHARLES J to 7680, SEIBERT JAMES G |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | ||||
H2O | 0 | 2200 Bbl | 25000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2003 | SEIBERT JAMES G | 0.00 | 231.00 | 275 |
2004 | SEIBERT JAMES G | 0.00 | 228.00 | 365 |
2005 | SEIBERT JAMES G | 0.00 | 131.00 | 365 |
2006 | SEIBERT JAMES G | 0.00 | 76.00 | 365 |
2007 | SEIBERT JAMES G | 0.00 | 119.00 | 365 |
2008 | SEIBERT JAMES G | 0.00 | 249.00 | 365 |
2009 | SEIBERT JAMES G | 0.00 | 226.00 | 365 |
2010 | SEIBERT JAMES G | 0.00 | 125.00 | 365 |
2011 | SEIBERT JAMES G | 0.00 | 243.00 | 365 |
2012 | SEIBERT JAMES G | 0.00 | 62.00 | 366 |
2013 | SEIBERT JAMES G | 0.00 | 96.00 | 250 |
2014 | SEIBERT JAMES G | 0.00 | 51.00 | 365 |
2016 | SEIBERT JAMES G | 0.00 | 26.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2003 | SEIBERT JAMES G | Brine | 52 | 275 |
2004 | SEIBERT JAMES G | Brine | 61 | 365 |
2005 | SEIBERT JAMES G | Brine | 32 | 365 |
2006 | SEIBERT JAMES G | Brine | 0 | 365 |
2007 | SEIBERT JAMES G | Brine | 76 | 365 |
2008 | SEIBERT JAMES G | Brine | 110 | 365 |
2009 | SEIBERT JAMES G | Brine | 108 | 365 |
2010 | SEIBERT JAMES G | Brine | 47 | 365 |
2011 | SEIBERT JAMES G | Brine | 121 | 365 |
2012 | SEIBERT JAMES G | Brine | 23 | 366 |
2013 | SEIBERT JAMES G | Brine | 42 | 250 |
2014 | SEIBERT JAMES G | Brine | 51 | 365 |
2016 | SEIBERT JAMES G | Brine | 26 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-102873477 | 2014-4-11 0:00: | PW | No Violations | |
-1094498444 | 2017-12-5 0:00: | PW | No Violations | 0.50 |
-1273378131 | 2017-3-6 0:00:0 | PW | No Violations | |
-1408503313 | 2017-2-16 0:00: | PW | No Violations | 2.00 |
-1542425880 | 2015-6-1 0:00:0 | AM | No Violations | |
-158460912 | 2015-2-12 0:00: | PW | No Violations | |
-1728201744 | 2017-1-20 0:00: | PW | No Violations | |
-1915519537 | 2017-7-20 0:00: | PW | No Violations | 0.50 |
-209475828 | 2017-2-27 0:00: | PW | No Violations | 1.00 |
-393618525 | 2017-10-26 0:00 | PW | No Violations | 0.50 |
-43626847 | 2014-9-16 0:00: | PW | No Violations | |
-639104984 | 2016-6-16 0:00: | PW | No Violations | |
-817571469 | 2016-8-12 0:00: | PW | No Violations | |
-85697438 | 2017-11-14 0:00 | PW | No Violations | 0.50 |
-99140611 | 2014-6-5 0:00:0 | PW | No Violations | |
-998895234 | 2014-9-29 0:00: | PW | No Violations | |
0043626847 | 2014-09-16 | Production Wells | No Violations | This inspection was conducted as a compliance follow-up. The inspection revealed that a new plastic tank has been set in place at the bottom of the hill. The old 100 barrel tank has not been removed. The oil around the tank has been cleaned up. The dike has not been constructed yet. Photos were taken during inspection. Well is not in compliance. |
0085697438 | 2017-11-14 | Production Wells | No Violations | An inspection of the tank battery revealed that the stockpiled soil has not been spread on the area that the tank was located. An email was sent to Mr. Seibert on 11-1-2017 asking if any work has begun at the tank battery. Mr. Seibert replied that day saying he would ask his landowner who is helping him with the clean up and he would get back with me. Mr. Seibert has not contacted me since. Mr. Seibert will be contacted and advised to finish the clean up. Time of inspection: 2:00 PM. Weather: 48*F, Sunny |
0099140611 | 2014-06-05 | Production Wells | No Violations | This inspection was conducted as a compliance follow-up. I was accompanied by Northwest Region Supervisor Will Ziegler and Jeff Fry. The well owner Mr. Jim Seibert and landowner Mr. Jack Trumbull met us at the tank located near the well (p#0387). A remediation plan was discussed with Mr. Seibert. Mr. Seibert agreed to build a new tank battery at the bottom of the hill and set both 100 barrel tanks there. The area near the well (p#0387) will be remediated in place with lime. Mr. Seibert will work on getting p#0387 registered and production reports sent in. He was advised to place proper identification at both wells and tank battery and to make sure that brine is being hauled through a registered brine hauler. Mr. Seibert was advised to keep both wells shut-in until he is in full compliance. |
0102873477 | 2014-04-11 | Production Wells | No Violations | This inspection was conducted as a production well status check. The well was equipped with a pumping unit and motor. It was not pumping. Identification was not posted at the well. The tank battery consists of (2) 100 barrel tanks. One of the tanks is located near the well and the other is located at the bottom of the hill near Reform Rd. This well shares the tank battery with permit number 0387. Identification was not posted at the tank battery. It appears that water has been drained from the tank near the well over the hill in the past. The well owner, Mr. James Seibert, has been notified of inspection. Mr. Seibert was informed that proper identification is required at the well and tank battery. Mr. Seibert was also advised that it is illegal to drain brine water onto the ground and that the water shall be disposed of through a registered brine hauler with the State of Ohio. Photos were taken for documentation purposes. |
0158460912 | 2015-02-12 | Production Wells | No Violations | This inspection was conducted as a status check. I was accompanied by Jeff Fry. During the inspection we measured the dimensions of the tank battery dike. The dike dimensions measured approximately 170 barrels. The tank battery consists of (1) 100 barrel tank and (1) approximately 2000 gallon tank. The old 100 barrel tank is still on location. Identification has not been posted at the tank battery. A phone call will be placed to Mr. Seibert regarding this inspection. Time of inspection: 11:40 AM. Weather: 22* F, Snowing, 1 snow |
0209475828 | 2017-02-27 | Production Wells | No Violations | I returned to this well today to do a follow-up inspection on it. It appears the owner has started working on the location. There has been some contamination removed and placed on a blue tarp. I have taken pictures of my findings today for my supervisor. |
0217583522 | 2014-05-28 | Production Wells | No Violations | This inspection was conducted as a compliance follow-up. This well produces into a shared tank battery with permit number 0387. Identification was not posted at the tanks. The inspection revealed that brine appears to have been drained onto the ground from the 100 barrel tank near the well (p#0387). Stressed vegetation was observed around the well and tank location. Starting from the tank near the well to the tank at the bottom of the hill an area approximately 150 feet long by 10 feet wide has been extremely affected by brine kill. Several dead trees were observed in this area. The three inch valve on the tank near the well was in the open position with a three inch plug in it. A 1.25 plastic yellow line comes off the bottom of the tank and runs south approximately 75 feet and then runs over the hill towards the road (Reform Rd.). The yellow line is connected to a tee fitting that has a black plastic line coming off the middle outlet. It could not be determined if it is going to the tank at the bottom of the hill. The third outlet on the tee fitting had no valve and was open ended. It appears this has allowed brine to be drained onto the ground as there was a large area of stressed vegetation. The well operation is causing pollution and contamination. The well owner has failed to report production for 2013 on the well identified as the W & M Wills #1 (p# 0387). The well owner is also in violation for failure to register in regards to the W & M Wills #1 (p# 0387). Identification was not posted at the tanks. A phone call was placed to Mr. Jim Seibert at 10:42 AM and was informed of the inspection. Mr. Seibert stated that he was the owner of both wells on the Mills lease and he was advised to shut the wells in until further notice. A meeting will be set up with Mr. Seibert at the well to discuss well operations and a plan to resolve compliance issues. At this meeting it will be decided specifically what is required of Mr. Seibert in order for him to be in compliance a |
0266322771 | 2017-07-10 | Production Wells | No Violations | This inspection was conducted as a compliance notice follow-up. Mr. Seibert was advised via email on 6/9/2017 to clean up oil contamination around the old 100 barrel tank that is no longer in use and clean the sides of the 100 barrel tank inside the dike. The inspection revealed that nothing has been cleaned up. Four photos were taken of the tank battery. Mr. Seibert will be contacted again via email and will be asked when he can have the tank battery cleaned up. Time of inspection: 10:00 AM. Weather: 70*F, Overcast |
0393618525 | 2017-10-26 | Production Wells | No Violations | An inspection of the tank battery revealed that the stockpiled soil has not been spread on the area that the tank was located. Mr. Jim Seibert sent an email on 10/17/2017 stating that he would spread the remediated soil on 10/18/2017 and notify me when he was finished. Time of inspection: 8:45 AM. Weather: 28*F, Sunny |
0639104984 | 2016-06-16 | Production Wells | No Violations | Inspect tank battery as a compliance notice follow-up. The old 100 barrel tank has not been removed. The area around the tank has not been cleaned up. The identification at the tank only has permit #0387 labeled. A phone call was placed to Mr. Seibert regarding inspection. Mr. Seibert was given two weeks to be in compliance. Time of inspection: 12:45 PM. Weather: 81*F, Cloudy |
0658950100 | 2014-10-28 | Production Wells | No Violations | This inspection was conducted as a compliance follow-up. The 100 barrel tank near the well (p# 0387) has been moved to the bottom of the hill and set in the new tank battery location. The tank battery now consists of (1) 100 barrel tank and (1) plastic tank (unknown capacity). The dike wall was not complete. The old 100 barrel tank near the road has not been removed. Identification has not been posted. Mr. Seibert needs to place well (p# 0387) under his bond. Compliance issues have not been resolved. |
0817571469 | 2016-08-12 | Production Wells | No Violations | This inspection was conducted as a compliance notice follow-up. The tank battery was inspected. There was no change since previous inspection dated 6/16/2016. The identification was not correctly labeled with permit number 2541. The 100 barrel tank that is not in use has not been removed and the soil around that tank has not been cleaned up. The inspection revealed that brine is being drained onto the ground inside the dike from behind the 100 barrel tank where a 2 nipple fitting and valve was observed. There was no bull plug on the valve. The sample of soil was taken within 1 foot of the valve. The soil sample was tested with a High Range Quantab Titrator for Chlorides. This resulted in a 9.0 Quantab unit reading which is off the scale. An 8.6 Quantab unit reading on this particular scale equals 6,215 ppm for chlorides. I took 10 photos of the tank battery this date. Time of inspection: 12:20 PM. The tank battery is not in compliance. |
0861269810 | 2014-05-29 | Administrative Inspection | No Violations | A voicemail message was left for Mr. Jim Seibert requesting a meeting at the tank battery location. |
0998895234 | 2014-09-29 | Production Wells | No Violations | This inspection was conducted as a compliance follow-up. The inspection revealed no change in status from previous inspection. The new tank battery and dike has not been constucted. The well owner will be contacted about non-compliance. |
1081951765 | 2004-04-13 | Production Wells | No Violations | Inspection conducted at the request of Sherry Young. Inspection revealed well is capable of producing. The current land owner advised that he though the rods are stuck but he is using the well for domestic gas (when there is enough pressure. |
1094498444 | 2017-12-05 | Production Wells | No Violations | I inspected the tank battery location as a compliance notice follow-up. The stockpiled soil has been spread over the area that the 100 barrel tank was located. Pollution and contamination has been cleaned up. The violation has been resolved. Time of inspection: 2:15 PM. Weather: 46*F, Overcast |
1100017922 | 2004-11-09 | Production Wells | No Violations | Well has pump jack and is pumping. Recent work on lease rd. Talked to landowner, new tank set. He said Jim Seibert has done more work to upgrade this well than Charlie had done in eleven years.He is also using gas off of well. Follow up to consent agreement. |
1273378131 | 2017-03-06 | Production Wells | No Violations | I returned to this well today to do a follow-up inspection on the clean-up of this well. All of the contaminated soil has been cleaned up besides what is left in front of the tank that needs removed. I contacted James Seibert to talk with him about it and he said he is getting that part done next. I told him everything else looked good at this point. |
1408503313 | 2017-02-16 | Production Wells | No Violations | I was on location today to do a follow up on this well. There is still contamination around the tank and in the dike. The snow was covering up some of the ground so I could not see what has all been cleaned up and what has not been. I took new pictures of the location to send to my supervisor. |
1433246649 | 2015-05-19 | Production Wells | No Violations | Inspect tank battery as part of a compliance notice follow-up. No change in status. Identification has not been posted. The old tank is on location. A voicemail message was left for Mr. Jim Seibert at 10:00 AM. Time of inspection: 9:30 AM |
1484917489 | 2017-01-20 | Administrative Inspection | No Violations | I spoke with Mr. James Seibert owner of well at 7:30 am by phone about the violations at the tank battery. According to Mr. Seibert he has very little money to work with due to oil prices and the landowner has been pumping the well. I explained to Mr. Seibert that he could take the contaminated materials to an offsite location and treat the material. Mr. Seibert will submit a plan and timeframe on clean-up of contaminated materials first of next week. |
1522754602 | 2017-03-17 | Production Wells | No Violations | Inspect tank battery as a compliance notice follow-up. Clean up has begun at the tank battery. A plastic tarp was observed near the tank battery. Contaminated soil has been placed on the tarp and was covered with another tarp. The edge of the tarp had a berm to prevent run off. The clean up is not complete. Photos were taken during inspection. Time of inspection: 12:50 PM. Weather: 32*F, Overcast |
1526703223 | 2014-07-16 | Production Wells | No Violations | This inspection was conducted as a status check. I was accompanied by Jeff Fry. The inspection revealed that work has not begun regarding the compliance issues with this well. The well owner has until 8/29/2014 to resolve compliance issues. |
1542425880 | 2015-06-01 | Administrative Inspection | No Violations | A voicemail message was left for Mr. Seibert at 3:05 PM in regards to unresolved compliance notice. |
1666288604 | 2014-10-01 | Production Wells | No Violations | A phone call was placed at 8:46 AM to well owner Mr. Jim Seibert regarding non-compliance. Mr. Seibert stated that work should be finished by the end of next week. |
1704679614 | 2015-02-19 | Administrative Inspection | No Violations | A phone call was placed to Mr. Seibert at 8:25 AM regarding the inspection conducted on 2/12/2015. Mr. Seibert was advised to post identification at the wellheads and tank battery. Mr. Seibert said that he would have his landowner post identification. |
1728201744 | 2017-01-20 | Production Wells | No Violations | Inspect tank battery as a follow-up. No personnel present during inspection. The ditch was observed to check for any pollution or contamination run-off that may have impacted the ditch due to a large rainfall event that ocurred last night. No oil or sheen was observed on the water. Time of inspection: 10:30 AM. |
1793909346 | 2017-01-19 | Production Wells | Violations Noted | This inspection was conducted at 12:00 PM as a status check. I was accompanied by Inspector Justin Smith. The inspection revealed that a spill/release has ocurred at the tank battery. It appears that oil has run over the 100 barrel storage tank onto the ground. The dike may have contained the oil but it also appears that someone has taken buckets or shovels of the oil and dumped it in the weeds surrounding the tank battery location. Standing water inside the dike was tested with a Quantab titrator test strip for chlorides. This resulted in a 10.0 reading on the test strip which equals >6200 ppm chlorides on this test strip. The plastic brine storage tank within the dike did not have a bull plug in the valve on the front side of the tank. Brine may have been drained from this valve as there was an observed depression in the soil in front of the valve. The well owner will need to install a bull plug on the valve. Orange ribbon was placed around the tank battery location noting the extent of the oil that was dumped in the weeds. A ditch near the tank battery was observed for any impact that may have taken place due to the release. I did not observe a sheen or oil on the water. During the inspection the Emergency Response section was notified of this incident. A voicemail message requesting a return phone call was left for Mr. Seibert (614-620-3662) at 1:22 PM. At 5:00 PM I spoke to Mr. Seibert via phone conversation regarding this incident. Mr. Seibert was advised that clean-up would need to begin immediately. It was made clear that clean-up would consist of excavation of contaminated soil outside and within the dike. Excavated soil would need to be hauled to a landfill or land farmed where it could be remediated. Clean-up will be witnessed by an inspector. Mr. Seibert failed to notify ODNR in a timely manner of this incident in accordance with OAC 1501:9-8-02 Incident Notifications which took effect August 9, 2016. Several photos were taken of the tank battery locatio |
1810528311 | 2017-09-28 | Production Wells | No Violations | An inspection of the tank battery was conducted this date. The inspection revealed the stockpiled soil has not been spread as requested. A voicemail message was left for Mr. Seibert. Time of inspection: 10:45 AM. |
1842629339 | 2014-09-04 | Production Wells | No Violations | This inspection was conducted as a compliance follow-up. The inspection revealed that work has not started. Inspection reveals non-compliance. |
1915519537 | 2017-07-20 | Production Wells | No Violations | Inspect tank battery as a follow-up accompanied by Emergency Responder Jason Blocker. No changes since previous inspection. Time of inspection: 9:20 AM. Weather: 77*F, Sunny |
2048893317 | 2017-01-19 | Production Wells | No Violations | This Compliance Notice will be closed as of today; a new Compliance Notice will be issued for all outstanding Violations. |
2055949400 | 2017-08-24 | Production Wells | No Violations | An inspection of the tank battery was conducted today to follow-up on the compliance notice. No changes have been made since the previous inspection. The well owner will be advised to spread stockpiled soil where the abandoned tank was sitting and work it into the ground. A follow-up inspection will be conducted the week of 9/18/2017. Time of inspection: 12:05 PM. |
217583522 | 2014-5-28 0:00: | PW | No Violations | |
266322771 | 2017-7-10 0:00: | PW | No Violations | 0.10 |
658950100 | 2014-10-28 0:00 | PW | No Violations | |
861269810 | 2014-5-29 0:00: | AM | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1793909346 | US-OH-117901 | 2018-03-30 | 9-1-07 | Well operation causing pollution and contamination |
1793909346 | US-OH-117902 | 2018-03-30 | 9-9-02 | General Safety |
1793909346 | US-OH-117903 | 2018-03-30 | 9-9-05(A)9 | No SPCC dike/or failure to keep dike free of water or oil |
1793909346 | US-OH-117904 | 2018-03-30 | 9-9-05(D) | Failure to have required locks, bull plugs |
For data sources see[8]